SOURC S CE REPORT B: FINAL F REPOR R RT FOR PULSE ED OXY YGEN BIOSPA B ARGING G (POB BS) PILO OT TES ST Is ssued: Octob ber 2015 Prepared by: The LA LNAPL Workgroup p FINAL F REPOR R RT FOR PULSE ED OXY YGEN BIOSPA B ARGING G (POB BS) PILO OT TES ST ssued: Octob ber 2015 Is Prepared P by: The T LA LNAP PL Workgrou up AE ECOM 999 9 Town and Cou untry Rd., Orang ge, CA 92868 tel. 714.567.2430 GS SI Environmental Inc c. 2211 Norfolk, Suite e 1000, Houston, Texas 77098-4 4054 tel. 713.522.6300 October 2015 COMMENTS ABOUT THIS DOCUMENT? Submit any comments or suggestions directly to: Mr. Mike Wang Western States Petroleum Association 970 W. 190th Street, Suite 770 Torrance, CA 90502 (310) 324-8565 TO CITE THIS DOCUMENT: Los Angeles LNAPL Working Group, 2015. Final Report for Pulsed Oxygen Biosparging (POBS) Pilot Test. Western States Petroleum Association, Torrance, California. AUTHORS Charles Newell, Michal Rysz, Poonam Kulkarni, Rebecca Buthe, Brian Strasters, Kate Hamel, GSI Environmental Inc. Matt Himmelstein and Roy Patterson, AECOM LA LNAPL Workgroup Pulsed Oxygen Biosparge Pilot Test October 2015 FINAL REPORT FOR PULSED OXYGEN BIOSPARGING (POBS) PILOT TEST Table of Contents 1.0 EXECUTIVE SUMMARY 1 1.1 1.2 1.3 1.5 PILOT TEST OBJECTIVES (SECTION 2.0) PILOT TEST DESIGN (SECTION 3.0) PILOT TEST OPERATION (SECTION 4.0) PILOT TEST PERFORMANCE SUMMARY (SECTION 6.0) 1 1 2 5 2.0 PILOT TEST OBJECTIVES 1 2.1 2.2 2.3 TECHNOLOGY OVERVIEW APPROACH: PUSH THE TECHNOLOGY OBJECTIVES AND PERFORMANCE METRICS 1 1 2 3.0 PILOT TEST DESIGN 4 3.1 3.2 3.3 3.3.1 3.3.2 3.3.3 3.3.4 3.3.5 3.3.6 POBS OVERVIEW PRE-TEST DESIGN ACTIVITIES POBS TEST DESIGN GEOLOGY, HYDROGEOLOGY AND LNAPL DISTRIBUTION BIOSPARGING WELL LAYOUT WELL DESIGN KEY DESIGN PARAMETERS OXYGEN DELIVERY SYSTEM PLANNING LEVEL MASS BALANCE ANALYSIS 4 5 6 7 7 7 8 9 10 4.0 PILOT TEST OPERATION 11 4.1 4.2 4.3 4.4 4.5 4.6 4.7 STARTUP PHASE INCREASED GAS INJECTIONS FIRST OXYGEN “DAYLIGHTING” EVENT FURTHER INCREASE IN GAS INJECTIONS ADDITIONAL DAYLIGHTING, SHORT CIRCUITING EVENTS VOLUME OXYGEN INJECTED MECHANICAL EQUIPMENT AND WELLS 11 11 11 12 12 12 12 LA LNAPL Workgroup iv Pulsed Oxygen Biosparging Pilot Test October 2015 5.0 PILOT TEST RESULTS 14 5.1 5.1.1 5.1.2 5.1.3 5.1.4 5.2 5.2.1 5.2.2 5.2.3 5.3 5.3.1 5.3.2 5.3.3 5.3.4 5.3.5 5.3.6 5.4 5.5 5.6 GROUNDWATER MONITORING DATA: DISSOLVED OXYGEN AND ORP DURING STARTUP AFTER TWO MONTHS SEPTEMBER INJECTION TESTS DISSOLVED OXYGEN DATA TO FEBRUARY 2013 GROUNDWATER MONITORING DATA: DISSOLVED CONSTITUENTS CONCENTRATION VS. TIME GRAPHS CONCENTRATION VS. TIME BAR CHARTS SUMMARY STATISTICS: BEFORE VS. AFTER CONCENTRATIONS FOR GROUNDWATER SOIL DATA FROM BEFORE- AND AFTER-TEST BORINGS VISUALIZATION OF SOIL DATA BEFORE AND AFTER AVERAGE CONCENTRATION STATISTICALLY SIGNIFICANT DECREASES AND INCREASES BEFORE-TEST CPT AND UVOST BEFORE VS. AFTER UVOST, CORE PHOTOGRAPHY, AND SOIL ANALYSIS BEFORE VS. AFTER CORE PHOTOGRAPHY AND PORE FLUIDS ANALYSIS MASS BALANCE ANALYSIS WITH INCREASING TPH CONCENTRATIONS STOICHIOMETRIC ANALYSIS OF OXYGEN INJECTION KEY QUESTIONS ABOUT THE MASS BALANCE ANALYSIS 14 14 14 14 15 16 16 16 17 20 20 20 22 23 23 24 26 29 30 6.0 PILOT TEST PERFORMANCE SUMMARY 32 6.1 6.2 6.3 6.4 6.5 6.6 6.7 CHANGE IN LNAPL MASS IN TREATMENT ZONES CHANGE IN APPARENT LNAPL THICKNESS AT WELLS IN TREATMENT ZONES CHANGE IN CONCENTRATION AND MASS DISCHARGE (MASS FLUX) IN TREATMENT ZONES CHANGE IN LNAPL MOBILITY CHANGE IN LNAPL COMPOSITION IN THE TREATMENT ZONES CONCENTRATIONS OF DO IN THE TREATMENT ZONES COST OF TREATMENT WHEN APPLIED TO FULL SCALE 32 33 33 33 34 34 34 7.0 REFERENCES 36 LA LNAPL Workgroup v Pulsed Oxygen Biosparging Pilot Test October 2015 LIST OF FIGURES Figure E.1. Pilot Test Layout Figure 3.1. Site Location and Layout Figure 3.2. Site NAPL Distribution Figure 3.3. Pulsed Oxygen Biosparging (POBS) System Pilot Test Focus Area Figure 3.4. Original Design for Biosparge Well Construction and CPT/ROST Characterization Data Figure 3.5. Pilot Test Layout with Biosparge and Monitoring Locations Figure 3.6 Conceptual POBS System Components Figure 4.1. Final Locations of POBS Injection and Monitoring Wells. Figure 4.2. Daily Injection Well Volumes for Injection Wells IW-1P (top), IW-2P (middle), and IW3P and IW-3R (bottom) in Units of SCF per day. Figure 5.1. Output from Downhole Sensor Over Four Days, Showing Injection Signal in Pressure and Conductivity, But Problem with DO and ORP sensors. Figure 5.2. Dissolved Oxygen and ORP After Two Months of Operation. Only IW-3P Showed Any Response to the Pulsing. Figure 5.3. Dissolved Oxygen Utilization Twelve Hours After Oxygen Pulse In One Injection Well Figure 5.4. Dissolved Oxygen in Groundwater: All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to February 2013. Figure 5.5. Benzene Concentrations in Groundwater vs. Time in All Wells (in µg/L) Figure 5.6. BTEX Concentrations in Groundwater vs. Time in All Wells (in µg/L) Figure 5.7. TPH Concentrations in Groundwater vs. Time in All Wells (in µg/L) Figure 5.8. Benzene in Groundwater: All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to August 2013 Figure 5.9. BTEX in Groundwater: All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to August 2013. Figure 5.10. TPH (All Fractions) in Groundwater: All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to August 2013. Figure 5.11. Summary Statistics for Benzene, BTEX, and TPH-All Fractions in Groundwater: All Injection (Blue color), Monitoring (Green), and Background (Yellow) Wells, June 2012 to August 2013. Figure 5.12. Soil Analysis Results for Benzene, BTEX, and TPH (all samples). Figure 5.13. Soil Data Posted on Triangle Chart, With Before-Test Concentrations on X-Axis and After-Test Concentration on Y-Axis. Figure 5.14. Cone Penetrometer (CPT) and UV Optical Screening Tool (UVOST) Logs. Figure 5.15. Cone Penetrometer (CPT), Before and After UV Optical Screening Tool (UVOST), and Core Photography for Borings MW-1 and MW-2. Figure 5.16. Cone Penetrometer (CPT), Before and After UV Optical Screening Tool (UVOST), and Core Photography for Borings MW-3 and MW-4. Figure 5.17. Before and After Test UV Optical Screening Tool (UVOST), and TPH-All Fractions Data for Borings MW-1 and MW-2. LA LNAPL Workgroup vi Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.18. Before and After Test UV Optical Screening Tool (UVOST), and TPH-All Fractions Data for Borings MW-3 and MW-4. Figure 5.19. Core Photography and TPH Data Figure 5.20. Core Photography and Two Before- and After-Test LNAPL Saturation Results LIST OF TABLES Table E.1.A Geometric Means of Before and After Constituent Groundwater Concentrations for Injection Wells Table E.1.B Geometric Means of Before and After Constituent Groundwater Concentrations for Monitoring Wells Inside Treatment Area Table E.2. Arithmetic Average Concentration Before and After Pilot Test Table 3.1. LNAPL Saturation and LNAPL Mobility Results from Core Analysis and Summary of Observed LNAPL Accumulation in Three Shallow and Two Deep Monitoring Wells. Table 3.2. Key Initial Design Parameters for the POBS System Pilot Test Table 3.3 Example Injection Pressure Parameters for the POBS Pilot Test System Table 4.1 Actual Injection Pressures with Fracture and Initial Design Pressure Table 5.1.A Geometric Means of Before, After, and Rebound Constituent Groundwater Concentrations for Injection Wells Table 5.1.B Geometric Means of Before, After, and Rebound Constituent Groundwater Concentrations for Monitoring Wells Inside Treatment Area Table 5.1.C Geometric Means of Before, After, and Rebound Constituent Groundwater Concentrations for Monitoring Wells Outside Treatment Area Table 5.2. Arithmetic and Geometric Averages of Before- and After-Test Soil Data. Table 5.3. Before and After Pore Fluids Analysis Data for Shallow Zone Table 5.4. LNAPL Mobility Test Results Using the Centrifuge Method Table 5.5. Arithmetic Average Concentration Before and After Pilot Test Table 5.6. Calculated Changes in Mass of Benzene, BTEX, and TPH Fractions Table 5.7. Revised Mass Removal Estimate for Benzene and BTEX Based on Change in Mass Fraction (assuming increase in TPH was due to sampling variability) Table 5.8. Volatilization Parameters for the BTEX Compounds vs. Percentage Removal LA LNAPL Workgroup vii Pulsed Oxygen Biosparging Pilot Test October 2015 1.0 EXECUTIVE SUMMARY 1.1 Pilot Test Objectives (Section 2.0) This Final Report details the results of a pulsed oxygen biosparging (POBS) pilot test for remediation of light non-aqueous phase liquid (LNAPL) that was conducted at the Shell Carson Terminal (Site) in Carson, California from June 2012 to June 2013. The pilot tests performed as part of the Los Angeles (LA) LNAPL Project tested post-conventional treatment technologies, which are defined as remedial technologies incorporated into site remediation after the initial LNAPL removal effort has been completed or the LNAPL has been determined to have low hydraulic recoverability (i.e., low LNAPL transmissivity). Key points regarding this Pilot Test are: The POBS technology sparges high concentration (~90%) oxygen into the treatment zone, which promotes biodegradation of most soluble organic contaminants, like benzene and BTEX (benzene, toluene, ethylbenzene, and xylenes), without the need for a soil vapor extraction system. This Pilot Test had the overall goal to “push” the technology (see Section 2.2) and test its ability to overcome difficult and/or novel applications in terms of: 1.2 - Applying POBS in a difficult hydrogeologic setting of a relatively thin (~5-footthick), potentially discontinuous, lower permeability sand/silty sand unit. - Treating submerged LNAPL as opposed to the more common application of POBS to treat dissolved plumes or even LNAPL plumes encountered at the water-table surface. - Designing the test in a way that an actual large-scale deployment of the POBS technology would be implemented, with large spacing (30 feet) between injection wells. - Pushing the technology and measuring performance between injection points (approximately 15 feet away) and not adjacent or close to the injection wells. The Pilot Test was designed to evaluate changes in mass, composition of LNAPL, concentrations in groundwater, and mass discharge of the dissolved plume; operational factors (such as how easy was the technology to implement); and cost (see Section 2.3). Pilot Test Design (Section 3.0) A Matrix Environmental Technologies Inc. onsite system was used for oxygen generation, storage, and delivery. Three injection wells were drilled in the triangular pattern shown in Figure E.1. Originally, two different transmissive units were targeted for treatment, but the planned treatment of the deeper unit had to be abandoned due to accumulation of several feet of LNAPL in the injection wells that would have been challenging to sparge safely with oxygen. Therefore, the scope of work for drilling the “P2” series of wells in Figure E.1 was not completed and no sparging or monitoring took place in the P2 zone (see Section 3.0). LA LNAPL Workgroup ES-1 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure E.1. Pilot Test Layout. Injection Wells (IW) were spaced 30 feet apart and Monitoring Wells (MW) were located at four locations within the test zone and two background locations. The Deeper unit wells (P2) were either not drilled or not used during the Pilot Test due to the accumulation of LNAPL in the wells. Note: Injection and monitoring wells are referenced by abbreviated names in this report, such as “IW1P” for well PB-IW-1-P and “MW-1” for well PB-MW-1-P. 1.3 Pilot Test Operation (Section 4.0) The POBS injection system experienced several operational difficulties during the 12-month testing period, as follows: High injection pressures were required to inject the oxygen in the treatment zone, demonstrating the difficulty of injecting into this type of formation. The lack of any dissolved oxygen (DO) change in the monitoring wells early in the test resulted in a decision to inject more oxygen than in the initial design parameters. The high injection pressures and/or large injection volumes, in turn, resulted in two daylighting events that required two injection wells to be abandoned. A short circuiting LA LNAPL Workgroup ES-2 Pulsed Oxygen Biosparging Pilot Test October 2015 event required one of these abandoned wells, well IW-3P, to be overdrilled and removed. In the end, three injection well related drilling events were performed during the test: (1) drilling of the three original injection wells; (2) drilling of injection well IW-3R to replace injection well IW-3P, and (3) overdrilling/removal of injection well IW-3P. Additionally, injection well IW-2P was taken out of service after seven months of biosparging and was not redrilled. An approximate total of 38,600 standard cubic feet (SCF) of oxygen were injected during the test. The longest running injection well with no operational problems (IW-1P) was able to support an average injection rate of 41 SCF per day during the year-long test. In general, the mechanical equipment functioned as designed during the test, requiring little maintenance; however, the relatively thin, heterogeneous formation made it difficult to inject oxygen in the subsurface. High DO concentrations were most apparent in the injection wells, and in one monitoring well where a short-circuiting event through the monitoring well screen was likely occurring. After about four months, small but statistically significant increases in DO (0.5 to 3 mg/L) were observed in the three working monitoring wells and (unexpectedly) in both background wells. The pattern of these increases suggests that after a year, the biosparging system was delivering low volumes of oxygen to the relatively large area represented by these wells. Over 90% of the dissolved phase benzene and BTEX compounds were removed from the high-oxygen zone around the injection wells (Table 5.1.A), with lower removals for TPH (~30%) which is consistent with the aerobic biodegradation process. Lower oxygen levels at the monitoring wells located away from the injection wells likely caused lower removals of benzene (40%) and toluene (45%) and some removal of xylenes (19%) and ethylbenzene (9%) (Table 5.1.B; overall reduction). The groundwater data were found to be log-normally distributed rendering the geometric mean concentration values meaningful for comparison. Rebound testing was conducted sixteen months after system shutdown and concentrations were compared to “After” concentrations at the wells. Some rebound occurred in the injection wells. Rebound did not affect the overall reduction in concentrations at these locations, and the overall reduction percentages were similar compared to the “Before” vs. “After” difference. LA LNAPL Workgroup ES-3 Pulsed Oxygen Biosparging Pilot Test October 2015 Table E.1.A Geometric Means of Before and After Constituent Groundwater Concentrations for Injection Wells Before Concentration (µg/L) Benzene BTEX TPH – All Fractions 795 2,737 46,659 After Concentration (µg/L) 16 154 32,061 Percent Reduction 98% 94% 31% Table E.1.B Geometric Means of Before and After Constituent Groundwater Concentrations for Monitoring Wells Inside Treatment Area Before After Concentration Concentration Percent (µg/L) (µg/L) Reduction Benzene BTEX TPH - All Fractions 883 2,625 54,919 638 2,124 34,269 28% 19% 38% Benzene concentrations in soil decreased slightly after the test (11% reduction using an arithmetic average). BTEX was unchanged (Table E.2). The mass fraction of both benzene and BTEX decreased by about 51% and 45% respectively during the test, which is statistically significant at the p=0.05 level. However, the majority of the reduction was due to toluene and benzene with no change in concentration of xylene or ethylbenzene This confirms that a significant composition change (removal of benzene and BTEX) did occur during the year-long test. The average concentration of the TPH-All Fractions increased by 82% before and after the test. This increase in TPH has two likely potential explanations: 1) an LNAPL inflow during the test, potentially due to the surging action of the oxygen pulses; and/or 2) random sampling variability. The Ultraviolet Optical Screening Tool (UVOST) and core photography data do not indicate LNAPL inflow (Figures 5.17 to 5.19). LA LNAPL Workgroup ES-4 Pulsed Oxygen Biosparging Pilot Test October 2015 Table E.2. Arithmetic Average Concentration Before and After Pilot Test Benzene (mg/kg) BTEX (mg/kg) TPH - ALL (mg/kg) GRO (mg/kg) DRO (mg/kg) Pre-Test Post-Test % Reduction 9.1 8.1 11% 86 86 0% 5,151 9,361 -82% 2,600 4,722 -82% 2,481 4,536 -83% Statistically Significant? Yes No No No No Notes: Negative % Reduction indicates an increase in average concentrations. GRO = Gasoline Range Organics, DRO = Diesel Range Organics Only two pairs of before and after LNAPL saturation data were available for analysis. These two pairs of LNAPL saturation data for MW-1 and MW-2 (Figure 5.20) either decreased or stayed the same (12.3% to 5.5% and 7.7% to 7.6%). The before and after soil samples generally showed an increase in TPH concentration (Figure 5.17 and 5.19); the reason for this trend is unknown. Insufficient LNAPL data collection and the heterogeneity of the soil analysis prevent any statistically significant conclusions. Benzene removed: between 3.6 – 6.5 kilograms (51% removal) BTEX removed: between 30 - 55 kilograms (45% removal), equivalent to 170 to 310 gallons of pure BTEX per year from a five-foot saturated interval. The Natural Source Zeon Depletion Test (NSZD) at the Shell facility measured 1700 gallons of LNAPL degraded per acre per year, but was measuring the degradation of many LNAPL components in the entire soil column. A mass balance estimate suggests that 1.9% to 10.6% of the oxygen delivered to the treatment zone was consumed for biodegradation of BTEX. Our analysis detailed in Section 5.6 suggests that there is no evidence of LNAPL inflow, losses attributable to volatilization were not significant, and the soil sampling data accurately show a reduction in the mass fraction of benzene and BTEX during the test. 1.5 Pilot Test Performance Summary (Section 6.0) Overall the key Pilot Test results are: It was difficult to inject into the thin, heterogeneous unit, and several daylighting events (oxygen channels emerging at the surface) made operation of the biosparge system difficult during the year-long test. Units where LNAPL is present and can accumulate in the injection wells may be difficult or impossible to biosparge like the deep wells in the Pilot Test. Submerged NAPL makes the applicability of this technology difficult to assess prior to drilling. LA LNAPL Workgroup ES-5 Pulsed Oxygen Biosparging Pilot Test October 2015 The mass fractions of benzene and BTEX in soil were reduced by 51% and 45% respectively during the year-long test, a statistically significant change. This confirms that the expected composition change* (preferential removal of BTEX compounds as opposed to removal of LNAPL mass) was established by the oxygen biosparge system during the test. It would likely take several more years of biosparging to reduce the benzene and BTEX mass fractions by 90%. * The ITRC LNAPL Framework document (ITRC, 2009) also uses the term “LNAPL Phase Change” as well as composition change. LNAPL Phase Change is defined as “Reliance on or application of a technology that indirectly remediates the LNAPL body via recovery and/or in situ destruction/degradation of vapor or dissolved-phase LNAPL constituents.” LA LNAPL Workgroup ES-6 Pulsed Oxygen Biosparging Pilot Test October 2015 2.0 PILOT TEST OBJECTIVES 2.1 Technology Overview This Final Report details the results of a POBS pilot test for remediation of LNAPL that was conducted at the Shell Carson Terminal (Site) in Carson, California from June 2012 to June 2013. All the pilot tests performed as part of the Los Angeles (LA) LNAPL Project tested post-conventional treatment technologies, which are defined as remedial technologies incorporated into site remediation after the initial LNAPL removal effort has been completed or the LNAPL has been determined to have low hydraulic recoverability (i.e., low LNAPL transmissivity). The oxygen biosparging remediation method can refer to a variety of different oxygen delivery approaches, such as: Low flow rate, continuous addition of air; Low flow rate, continuous addition of high concentration (~90%) oxygen; High flow rate, but limited duration (pulsed) sparging of air; and High flow rate, but limited duration (pulsed) sparging of high concentration oxygen. The technology identified for pilot testing at the Site was the last delivery approach: high flow rate pulsed sparging of high concentration (~90%) oxygen. By using a high flow rate, the zone of airflow (or zone of influence [ZOI]) for biosparging can approach the zone of airflow that is experienced during conventional air sparging, while minimizing the phase transfer (volatilization) of volatile organic compounds (VOCs) that occurs with constant air injection. Biosparging in this manner is intended to promote the degradation of hydrocarbons by increasing the activity of naturally occurring microorganisms. This technology has several different names, including Oxygen Pulse Injection System (OPIS) (Shell Global Solutions, 2007). 2.2 Approach: Push the Technology This Pilot Test had the overall goal to “push” an existing remediation technology, POBS, and test its ability to overcome difficult and/or novel applications in terms of the hydrogeological setting, source location, injection well spacing, and performance monitoring of the system, as described below: Apply POBS in a difficult hydrogeologic setting of a relatively thin (~5-foot-thick), potentially discontinuous, lower permeability sand/silty sand unit. In the LA LNAPL Literature Review document (LA LNAPL Workgroup, 2011) this type of hydrogeologic setting was defined as a “Type III – Granular Media with Moderate to High Heterogeneity.” This type of setting is different than the typical larger, thicker sand units in which many sparging systems are installed. Determine the ability of the POBS technology to treat submerged LNAPL as opposed to the more common application of POBS to treat dissolved plumes or even LA LNAPL Workgroup 1 Pulsed Oxygen Biosparging Pilot Test October 2015 water-table LNAPL. Submerged LNAPL is defined as “LNAPL that is found well below the water table due to a historical release, followed by a rising water table. Most submerged LNAPL is in the residual form, and conventional floating LNAPL conceptual models do not apply. Submerged LNAPL is found in the LA Basin at sites with older, historical releases of LNAPL due to rising water table since the 1950s” (LA LNAPL Workgroup, 2007). At this site, the submerged LNAPL in the treatment zone was located approximately 24 feet below ground surface and 17 feet below the water table. A successful project that employed “deep air sparging” (Klinchuch et al., 2007) provided some support for applying POBS to deeper units. Design the test in a way that an actual large-scale deployment of the POBS technology could be evaluated with large spacing (30 feet) between injection wells. For example, guidance developed by Shell suggested wells on 5-foot centers for barrier designs and wells on 10-foot centers for areal treatments (Shell Global Solutions, 2007). This spacing would not be practical for large treatment areas (tens or even hundreds of acres) of treatment zone containing submerged LNAPL. For this test, 30-foot spacing between injection wells was used. Again, the deep air sparging project by Klinchuch et al., (2007) indicated that larger spacings could be successful, but in a different hydrogeologic setting. Push the technology and measure performance between injection points (approximately 15 feet away) and not adjacent or close to the injection wells. The goal was to determine the ability of the POBS system to distribute the oxygen, and therefore the zone of biodegradation, throughout the treatment zone. If the POBS system was successful at meeting these four challenges, then the POBS technology could provide a potential method to treat relatively large areas of submerged LNAPL in Type III heterogeneous formations, after issues such as safety, access, cost, and performance are evaluated. 2.3 Objectives and Performance Metrics The objective of the Pilot Test was to evaluate whether oxygen biosparging is a viable option for remediation of residual LNAPL, and to estimate optimal operating parameters and system requirements identified during a prior engineering evaluation performed to identify potentially feasible technologies for remediation of LNAPL. The success of the technology was evaluated in terms of technical feasibility and cost effectiveness. Performance metrics that were considered for technology assessment include: Change in LNAPL mass in treatment zones; Change in apparent LNAPL thickness at wells in treatment zones; Change in mass discharge (mass flux) from treatment zones; Change in LNAPL mobility; LA LNAPL Workgroup 2 Pulsed Oxygen Biosparging Pilot Test October 2015 Change in LNAPL composition in treatment zones; Change in benzene concentrations in treatment zones; Concentrations of dissolved oxygen (DO) and carbon dioxide (CO2) and oxidationreduction potential (ORP) in treatment zones; Cost of treatment when applied to full scale operation; and Selected sustainability metrics (energy use, carbon footprint). RESULTS: Pilot Test Objectives The POBS technology sparges high concentration (~90%) oxygen into the treatment zone, which promotes biodegradation of most soluble organic contaminants, like benzene and BTEX, without the need for a soil vapor extraction system. The Pilot Test had the overall goal to “push” the technology and test its ability to overcome difficult and/or novel applications in terms of the hydrogeological setting, source location, injection well spacing, and performance monitoring of the system The Pilot Test was designed to evaluate changes in mass, composition of LNAPL, concentrations in groundwater, and mass discharge of the dissolved plume; operational factors (such as how easy was the technology to implement); and cost. LA LNAPL Workgroup 3 Pulsed Oxygen Biosparging Pilot Test October 2015 3.0 PILOT TEST DESIGN The Site is located in Carson, California (Figure 3.1). The conditions at the Site have been thoroughly delineated and documented during previous assessments and remediation activities. Recent reports that document Site conditions include the Light Non-Aqueous Phase Liquid (LNAPL) Recovery Pilot Test and Recovery Modeling Report (Geosyntec, 2008a), Supplemental Light Non-Aqueous Phase Liquid (LNAPL) Recovery Pilot Test and Recovery Modeling Report (Geosyntec, 2008b), Light Non-Aqueous Phase Liquid (LNAPL) Investigation (Geosyntec and URS, 2007), and the Site Assessment Report, Former Process Area (Brown and Caldwell, 2007). Details of the conditions pertinent to this work plan are provided below. The Site-wide LNAPL distribution, as characterized in 2007 and 2008, is shown on Figure 3.2. In figure 3.2, “Heavy, Drowned HC” represents a submerged heavier petroleum hydrocarbon LNAPL. Cone penetrometer test/rapid optical screening tool (CPT/ROST) characterization data from location PA11 (Figure 3.3) have indicated that the bulk of the LNAPL within the Pilot Test focus area is encountered in two intervals located between approximately 23 and 25 feet below ground surface (ft bgs) and 43 and 47 ft bgs. LNAPL pore fluid saturations, estimated from nearby Area 6 characterization data, ranged from nondetect (<0.1%) to 12.9%. The potentially biodegradable fraction of the LNAPL (11%) was estimated based on soil concentrations of volatile and semi-volatile constituents in samples collected in the vicinity of location PA11. These laboratory results were obtained from previous site characterization reports (Geosyntec and URS, 2007; Geosyntec, 2008a). The POBS technology is a “composition change technology” (see note on page E-5 about “phase change” vs. “composition change” terminology) that allows treatment of aerobically biodegradable LNAPL fractions within the treatment zone. Treatment was targeted at constituents dissolved in groundwater and present within the LNAPL. Because the soluble/biodegradable fraction was characterized as relatively small, POBS was not expected to reduce overall LNAPL mass significantly. 3.1 POBS Overview The initial design variables for the Pilot Test were an injection volume necessary to occupy 10% pore volume per week (based on Leeson et al., 2002); pulsed sparge events at flow rates of approximately 15 to 20 standard cubic feet per minute (SCFM) (based on Leeson et al., 2002); and oxygen injection rates greater than 15 SCFM (Shell Global Solutions, 2007). These design variables were changed following system start-up based on the response of the subsurface to oxygen injection. The Pilot Test design consisted of three oxygen biosparging injection wells installed in a triangular pattern at 30-foot spacing in the vicinity of CPT/ROST location PA11 (Figure 3.3). Initially, two different zones were planned to be tested: a shallower, thin, less permeable zone found approximately 8 feet below the general potentiometric surface shown in nearby monitoring wells (approximately 23 ft bgs) and a thicker, relatively more permeable zone found approximately 32 ft below the general potentiometric surface (approximately 47 ft bgs) LA LNAPL Workgroup 4 Pulsed Oxygen Biosparging Pilot Test October 2015 (Figure 3.4). However, the significant accumulation of recoverable LNAPL in the first wells drilled in the deeper zone led to the decision to test only the upper zone. The injection well spacing for the Pilot Test is 30 feet and was chosen based on the following rationale: Bass et al. (2000) evaluated the performance of air sparging at 49 sites, and reported that the “successful systems” were spaced an average of 28.6 ft apart. The 30-foot spacing chosen for the Pilot Test is close to the average spacing of successful air sparging projects in the Bass et al. (2000) study. The presence of confining units in the heterogeneous hydrogeologic setting at the Site, like other facilities in the LA Basin, is believed to promote lateral movement of the oxygen (Leeson et al., 2002). A common default value of 10-foot spacing for oxygen biosparge projects (Shell Global Solutions, 2007) and 15-foot spacing for air sparging projects (Leeson et al, 2002) would not likely be cost effective for large-scale, wide-spread areal treatment of residual LNAPL, as somewhere between 200 and 450 wells per acre would be required. For 30-foot spacing, only 50 wells per acre would be required. Note that Leeson et al. (2002) allow for pilot tests to establish the “smallest well spacing that is not cost-prohibitive” and Shell Global Solutions (2007) allows for evaluation of other well spacings. Because the Western States Petroleum Association – Los Angeles (WSPA LA) LA LNAPL Project is focused on both cost and performance, the scalable spacing option (30 ft between wells) was selected for this Pilot Test. The estimated ZOI from a previous air sparging test conducted at the Site was reported at 22 feet (URS, 2007). (In theory, injection wells can be spaced at two times the ZOI; however, in practice the ZOIs of adjacent wells typically overlap to some degree.) Oxygen was generated onsite from ambient air with a Matrix Environmental Technologies Inc. pressure swing adsorption (PSA) oxygen generation system on loan from Shell, which has been successfully implemented at other sites for the remediation of BTEX and oxygenate-impacted groundwater. The generated oxygen was stored in a reservoir tank until delivered to the injection wells. The system is capable of generating approximately 50 standard cubic feet per hour (SCFH) of oxygen. 3.2 Pre-Test Design Activities In August 2012, two shallow injection wells, two shallow monitoring wells, two deep injection wells and two deep monitoring wells were drilled. Soon after completion, 21 to 27 feet of LNAPL accumulation was observed in all four deep wells. After reviewing safety and operational issues, it was decided to abandon the deeper unit and just perform the Pilot Test in the shallow unit. LA LNAPL Workgroup 5 Pulsed Oxygen Biosparging Pilot Test October 2015 Curiously, soil samples tested for NAPL fluids information (saturation, mobility) did not indicate any significant differences between the shallow zone (where there was no LNAPL accumulation) and the deeper zone (where there was over 20 feet of LNAPL accumulation) (Table 3.1). Table 3.1. LNAPL Saturation and LNAPL Mobility Results from Core Analysis and Summary of Observed LNAPL Accumulation in Three Shallow and Two Deep Monitoring Wells. NAPL Pore Fluid Saturations Location* Shallow Unit IW-1P MW-2P MW-1P Deep Unit MW-2P2 MW-1P2 Well Data LNAPL Accumulation in Unit (feet) Depth (ft bgs) NAPL Saturation (%PV) Average NAPL Saturation (%PV) 23.25 23.55 23.15 6.4 7.7 12.3 8.80 0 feet in Three Wells 43.35 5.8 8.15 21.8 to 27.3 feet in Two Wells Fluid Sat. After Centrifuge 1000xG (%PV) Change in Saturation (%PV) 42.25 10.5 Free Product Mobility Location Depth (ft bgs) Initial Fluid Sat. (%PV) Shallow Unit MW-1P 23.30 9.5 9.20 Deep Unit MW-1P2 42.40 10.0 9.60 *Notes: bgs = below ground surface. %PV = percent of pore volume. -0.3 -0.4 In May 2012, a “pre-test” injection test was performed. Compressed nitrogen from a cylinder was injected into both wells to evaluate if oxygen could be injected into the formation at pressures below 45 pounds per square inch gauge (psig). Injection pressures in the shallow zone were high (16.8 psig required to get 20 SCM nitrogen flowrate) and above the potential fracture pressure but considered acceptable to continue for reasons discussed in Section 3.3.4. 3.3 POBS Test Design The area identified for the Pilot Test is located in the central portion of the Former Process Area of the Site in the vicinity of CPT/ROST location PA11 (Figure 3.3). The location was chosen after a thorough screening of CPT/ROST characterization data, and evaluation of specific geologic conditions and LNAPL distribution data. Selection criteria considered LA LNAPL Workgroup 6 Pulsed Oxygen Biosparging Pilot Test October 2015 include the presence of submerged LNAPL (inferred from ROST response and nearby groundwater depth data), LNAPL occurrence in relatively coarser-grained soils, and a thickness of affected soils of approximately 4 feet or greater. Of the 368 CPT/ROST records evaluated, location PA11 was selected from approximately six onsite locations that best satisfied these criteria. 3.3.1 Geology, Hydrogeology and LNAPL Distribution The general stratigraphy and subsurface LNAPL distribution, as interpreted from CPT/ROST data at location PA11, are shown on Figure 3.4. The presence of LNAPL is indicated by the ROST signature at distinct depths down to approximately 47 ft bgs. Soils in this interval include sands, silts and clays, with the water table at approximately 16.6 ft bgs. 3.3.2 Biosparging Well Layout The layout of the Pilot Test and original locations of biosparging and monitoring wells are shown on Figure 3.5 with final well locations shown on Figure 4.1. The conceptual system design is shown on Figure 3.6. The biosparge pilot system consisted of one PSA oxygen generation system supplying oxygen to the three injection wells. Four monitoring locations within the treatment area, together with one upgradient, one downgradient, and one crossgradient monitoring well pair (Figure 3.5) were installed for the purpose of monthly groundwater monitoring for VOCs and CO2 and more frequent sampling and DO and ORP distribution monitoring during the Pilot Test. 3.3.3 Well Design Biosparge wells were installed at three locations using a hollow-stem auger drill rig. The original design with both shallow and deep injection wells is shown in Figure 3.4. The injection wells were spaced 30 ft apart as shown on Figure 3.5. Each biosparge well was constructed with a 2-inch diameter casing and screen. Consistent with Shell Global Solutions (2007) Oxygen Pulse Injection System (OPIS) Design and Installation Guidance Document, each well had: A 2-foot length of 0.010-slot screen; A 5-foot length (minimum) sump below the slotted screen; Sand pack from the bottom of the sump to 1 ft above the screen; A bentonite seal from the top of sand pack to 1 ft above the water table; and Bentonite-cement grout from the top of the bentonite seal to the ground surface. In compliance with Shell’s requirements for subsurface investigations, approximately the top 10 feet of soil was removed using an air knife and then replaced to verify that utilities were not present at the location. The injections and monitoring wells were screened between 23 and 25 ft bgs in a thin sand within a predominantly fine-grained horizon and targeted the approximately 5-foot-thick upper treatment zone. LA LNAPL Workgroup 7 Pulsed Oxygen Biosparging Pilot Test October 2015 The current water table level at the site is estimated to be approximately 16.6 feet bgs, corresponding to injection depths of between 6.4 and 8.4 feet below the water table (upper well). The oxygen injection points were set at the bottom of the treatment zones. As shown on Figure 3.5, the study area included a total of seven locations for groundwater monitoring, including four locations within the treatment area, one upgradient location, one downgradient location, and one cross-gradient pair. Each of the four monitoring locations within the treatment area included a well with a 4-inch diameter well screen and casing. This well diameter allowed monitoring of DO and ORP using a downhole optical DO meter. 3.3.4 Key Design Parameters Key design parameters for the Pilot Test are summarized in Table 3.2. The values listed for these parameters represent planning-level estimates that were used during the startup phase of the Pilot Test. Table 3.2. Key Initial Design Parameters for the POBS System Pilot Test taken from POBS Work Plan (LA LNAPL 2010). Parameter Sparge well spacing Design zone of oxygen influence (ZOI) Injection depth Value 30 ft 15 ft 23 to 25 ft bgs (Upper wells) Initial oxygen volume delivered to formation per week Oxygen volume delivered per well per week 10% of pore volume in treatment zone 106 SCF (Upper Wells) Oxygen volume delivered per well per day 15.1 SCF (Upper Wells) Injection flow rates 15 to 20 SCFM Injections per day per well ~1 (Upper wells) Calculated fracture pressures (Pfracture) 16.8 psig (Upper wells) Injection duration ~1 minute per injection LA LNAPL Workgroup 8 Basis See Section 3.2 From well spacing; see URS/GSI 2010. Site stratigraphy and ROST data in vicinity of Pilot Test location Derived from oxygen demand data in Leeson et al. (2002) Pressure corrected injection volumes Daily injections necessary to deliver oxygen volume equivalent to 10% weekly saturation USACE (2008); NFESC (2001); Leeson et al. (2002); Shell Global Solutions (2007) Starting design parameter from Shell experience; 60-gallon oxygen storage tank GSI and AECOM; based on injection depths Injection flow rates and injection volumes Pulsed Oxygen Biosparging Pilot Test October 2015 Injection Pressure In general, guidance documents indicate that the fracture pressure should not be exceeded during sparging system operation due to formation fracturing in the immediate vicinity of the injection wells (NFESC 2001; Leeson et al., 2002; USACE 2008). The initial injection pressures calculated for the startup phase (with a 30% safety factor, SF) are shown in Table 3.3. However field experience from sparging systems indicates that to induce gas flow and achieve flow rates greater than 10 SCFM it may be necessary to exceed the calculated fracture pressures (personal communication with T. Peargin, 2010). Therefore a contingency plan was made that if flow is not achieved at Pmax,initial or if oxygen distribution is not adequate at this pressure, the injection pressures would be increased incrementally until satisfactory oxygen profiles are established. Table 3.3 Example Injection Pressure Parameters for the POBS System Pilot Test Sparge Well Injection Depth(1) (ft bgs) Pmin (psig) Upper 23 2.75 (1) Depth to top of injection screen (feet below ground surface) Pfracture (psig) 16.8 Pmax-initial (Pfracture with 30% SF – psig) 11.8 Flow Rate Proper gas flow rate is important so that gas distribution is maximized for biodegradation without causing gas-stripping of constituents. Flow rates during pulsing reported in the literature for biosparging projects typically range from less than 5 SCFM to approximately 40 SCFM (USACE, 2008). The most relevant biosparging guidance documents recommend a target flow rate of approximately 20 SCFM for pilot tests (NFESC, 2001; Leeson et al., 2002). For this test, the design flowrate was established at 15 to 20 SCFM, but with the understanding that actual flowrates in the field would be controlled by the injection pressure and the ability of the formation to accept the oxygen. Sparge Frequency and Duration The original sparge frequency for the startup phase of the Pilot Test was planned for one pulse per day for the upper wells. System parameters such as DO, and ORP (measured daily during Month 1 and monthly afterwards), and groundwater VOC and CO2 concentrations (collected monthly), were used to evaluate system performance. The Workplan envisioned that the sparging frequency, injection rate, and injection volumes could be modified based on field measurements. 3.3.5 Oxygen Delivery System A Matrix Environmental Technologies Inc. onsite system was used for oxygen generation, storage, and delivery. The system consisted of a trailer housing all essential aboveground components, including a PSA oxygen generator, a manifold, solenoid valves and pressure gauges for monitoring each injection line. Additionally, a totalizing flow meter was installed to monitor the total volume of oxygen injected. To mitigate potential safety risks, a flame LA LNAPL Workgroup 9 Pulsed Oxygen Biosparging Pilot Test October 2015 arrester was installed at each of the injection well heads. The generated oxygen was stored in a reservoir tank (the tank capacity was increased during the test) and the pulses were regulated using timer-activated solenoid valves. High-density polyethylene (HDPE) or Duraplus artery lines were used for oxygen delivery between the oxygen storage tank and biosparge wells. 3.3.6 Planning Level Mass Balance Analysis A planning level analysis of the removal of LNAPL VOCs based on the Air Sparging Design Paradigm (Leeson et al., 2002) and a first order decay rate was conducted to estimate the expected LNAPL remediation “glide path” envelopes for the treatment. To generate a range of removal estimates, the first order decay rate (determined from input parameters) was adjusted by ± 50% during the analysis. Parameters such as LNAPL VOC mass fraction, and LNAPL density were obtained from previous site investigation reports (Geosyntec, 2007; Geosyntec 2008). LNAPL saturation was determined during sampling performed by AECOM (formerly URS) in August 2011. To account for uncertainties inherent to biosparging systems regarding oxygen distribution, additional oxygen demand and utilization for aerobic degradation, an oxygen utilization factor of 50% was assumed in the analysis (i.e., one-half of the total oxygen mass delivered was assumed to be used in biodegradation reactions). The preliminary estimates of the mass removal during the initial 12 months of the pilot system operation indicated that for the upper treatment zone: Approximately 66% of the initial BTEX mass present in the LNAPL could be removed, and Removal could range between 42% and 80% of the initial BTEX mass. These estimated removal rates were based on the assumption that about 16,500 SCF of oxygen would be injected. RESULTS: Pilot Test Design Planned treatment of the deeper unit had to be abandoned due to several feet of LNAPL accumulation in wells that would have been challenging to sparge safely with oxygen. A field study for gas injection was conducted to evaluate planning estimates against realworld conditions. A “Glide-Path” was established to evaluate data during the test so that operations changes could be made if the results were below expectations. Initial design parameters (Table 3.2) were selected with the understanding that significant changes might be made during the Pilot Test based on field measurements. LA LNAPL Workgroup 10 Pulsed Oxygen Biosparging Pilot Test October 2015 4.0 PILOT TEST OPERATION 4.1 Startup Phase During the startup phase, higher injection pressures than the design values of 11.8 psig were required to introduce oxygen into the treatment zone (Table 4.1): Table 4.1 Actual Injection Pressures with Fracture and Initial Design Pressure Injection Well IW-1P IW-2P IW-3P Fracture Pressure (psig) Design Pressure (psig) 16.8 11.8 Actual Startup Pressure (psig) 18-21 28-29 16 Because of the difficulty in delivering gas to the treatment zone, the initial design of one pulse per day was changed to two ~10 SCF pulses separated by approximately 30 minutes during the startup phase of the test. This was done to allow the existing PSA oxygen generator to develop the required volumes and pressure to inject the calculated volumes. The change provided a theoretical delivery volume of 20 SCF oxygen per well per day (compared to the initial plan of 15 SCF per well per day). 4.2 Increased Gas Injections By August 2012, there had been little oxygen measured in the monitoring wells. Therefore, the Workgroup decided to increase the oxygen delivery to a total of six pulses per day, with pulse 1 and 2 separated by 30 minutes, then a wait of approximately 8 hours, then pulses 3 and 4 separated by about 30 minutes, then after a wait of approximately 8 hours, pulses 5 and 6 separated by about 30 minutes. Each pulse had a theoretical delivery volume of about 10 SCF. The arrangement was necessitated by the equipment’s ability to produce and store pressurized oxygen. 4.3 First Oxygen “Daylighting” Event In August 2012, approximately 2 months after startup and after gas injections had been increased, well IW-3P appeared to create “daylighting” of the oxygen pulse. When this well was operated, technicians observed fluids and dirt escaping from the surface under the chat cover. Operation of this well was terminated and a replacement well, IW-3R, was drilled and put into service in December 2012. Because of drilling constraints, and the desire not to intersect any channels from the treatment zone to the surface that were associated with IW3P daylighting, the IW-3R replacement well was installed approximately 7 feet east of IW-3P (Figure 4.1, Note: IW-3R = “PB-IW-3PR” in figure). Additionally, the borehole was not cleared using an air knife, further reducing the potential for near-surface short circuiting. The area of the site where the POBS was installed has had significant demolition activities over time and no active structures were expected to be present. Surface geophysics were conducted to clear the borehole. The Workgroup does not recommend installing wells LA LNAPL Workgroup 11 Pulsed Oxygen Biosparging Pilot Test October 2015 without subsurface clearance at any site where there exists a potential for buried utilities and other structures. 4.4 Further Increase in Gas Injections In December 2012, due to perceived poor distribution of oxygen and a design review meeting by experts from Shell Global Solutions, the Workgroup increased the theoretical delivery for each of the 6 pulses per day to approximately 30 SCF (180 SCF oxygen per well per day) after increasing the oxygen reservoir tank size. In practice, the amount of oxygen going into each well varied considerably over time due to the dynamics of the injection pressure required to overcome the resistance to gas flow in the treatment zone. Figure 4.2 shows the estimated daily gas delivery volumes to each of the injection wells over time. 4.5 Additional Daylighting, Short Circuiting Events In December 2012, six months after startup, injection well IW-2P daylighted gas and was taken out of service and not redrilled. In February 2013, gas from the IW-3R appeared to be short circuiting to the surface around the abandoned IW-3P. IW-3P was overdrilled in April 2013, allowing two more months of sparging from well IW-3R. 4.6 Volume Oxygen Injected Over the course of the test, the three injection wells were able to deliver these volumes of oxygen: 15,700 SCF to IW-1P 9,140 SCF to IW-2P 13,760 SCF to IW-3P and IW-3R 38,600 SCF TOTAL from all injection wells The average daily volume injected (excluding downtime due to daylighting or short circuiting) were: 4.7 41 SCF/day to IW-1P 44 SCF/day to IW-2P (while in operation) 63 SCF/day to IW-3P and IW-3R Mechanical Equipment and Wells In general, the mechanical equipment (controllers, solenoids, oxygen generator, tankage) worked well during the test, requiring little routine maintenance. The pulsed operation of the system, coupled with the fine grain size of the formation resulted in the silting of the injection wells at various times during the test duration. Each LA LNAPL Workgroup 12 Pulsed Oxygen Biosparging Pilot Test October 2015 well was constructed with a 5-foot sump to minimize silt blocking off the well screens, but this still occurred and silt was removed on several occasions. RESULTS: Pilot Test Operation The POBS injection system experienced several operational difficulties during the 12month testing period. In general, the mechanical equipment worked well during the test, requiring little routine maintenance. But the relatively thin, heterogeneous formation made it difficult to inject oxygen in the subsurface. The lack of any DO change in the monitoring wells early in the test resulted in a decision to inject more oxygen than in the initial design parameters. Injection gas volumes were increased over the initial design values at the start of the test, and were increased once again in December 2012. High injection pressures were required to inject the oxygen in the treatment zone, demonstrating the difficulty of injecting into this type of formation. The high injection pressures and/or large injection volumes, in turn, resulted in two daylighting events that required two injection wells to be abandoned. A short circuiting event required one of these abandoned wells, well IW-3P, to be overdrilled and removed. Typical well clearance procedures may result in the creation of short-circuiting pathways. In the end, three injection well related drilling events were performed during the test: (1) drilling of the three original injection wells; (2) drilling of injection well IW-3R to replace injection well IW-3P, and (3) overdrilling/removal of injection well IW-3P. Additionally, injection well IW-2P was taken out of service after seven months of biosparging and was not redrilled. A total of 38,600 SCF of oxygen were injected during the test. The longest running injection well with no operational problems (IW-1P) was able to support an average injection rate of 41 SCF per day during the year-long test. For pulsed sparging in fine grained lenses, silting will likely take place in the injection wells. Wells should be constructed with an adequate sump and appropriate well screen and sand pack, and field time should be estimated to check for, and remove silt accumulation. LA LNAPL Workgroup 13 Pulsed Oxygen Biosparging Pilot Test October 2015 5.0 PILOT TEST RESULTS 5.1 Groundwater Monitoring Data: Dissolved Oxygen and ORP Considerable resources were devoted to measuring DO and ORP in the injection and monitoring wells during the first three months after startup. Optical DO probes (In-Situ RDO Oxygen Sensors) were installed in two wells in an attempt to observe oxygen pulses and the subsequent decay from biodegradation and other processes. 5.1.1 During Startup During startup, the pressure, temperature and conductivity measurements from the In-Situ probes were successful at detecting the oxygen pulses. However, the ORP and DO data produce suspect results. For example, Figure 5.1 shows the flatline response of the dissolved oxygen and ORP sensors compared to the sawtooth pattern of pressure and conductivity during four days in July in one well. After consulting with the manufacturer it was determined that LNAPL could coat the sensor and disable the DO and ORP signals. It is possible that DO saturation did not increase in this well, and it is possible that small volumes of LNAPL coated and degraded the sensitivity of the instrument. 5.1.2 After Two Months DO readings using conventional surface field instruments were able to show the DO and ORP distribution in the injection and monitoring wells during groundwater sampling events. As shown in Figure 5.2, after two months of operation (August 2012), elevated DO was observed in injection well IW-3P, where DO had increased from 0.1 mg/L prior to start up to 6.9 mg/L. Very low DO was measured at all the other wells, however. 5.1.3 September Injection Tests In September 2012, Dr. Cristin Bruce, a pulsed oxygen biosparge expert from Shell, worked with the AECOM field team to evaluate the performance of the pulsing system. An optical DO sensor was carefully installed in injection well IW-1P and the well was sealed to allow for injections. The purpose of the test was to evaluate if oxygen was being transferred to the groundwater, and if it was persistent in the groundwater following the injection. Analysis of the data indicated that the water column was being forced from the well and oxygenated in at least the immediate vicinity of the well. A spike in DO concentrations following the injection, as groundwater reentered the well, showed that DO concentrations reached the expected level of saturation, 33 mg/L (Figure 5.3). Then, over the next twelve hours, the oxygen readings from the probe dropped consistently to 3 mg/L. The results from this test are consistent with oxygen being delivered to the subsurface (although potentially just around the injection well) and then being consumed by biodegradation processes (however no other data are available to confirm this conclusion). The results of this test indicated that oxygen distribution may be limited and that the high oxygen demand from the submerged LNAPL may be limiting the ability of oxygen to reach the monitoring points. LA LNAPL Workgroup 14 Pulsed Oxygen Biosparging Pilot Test October 2015 5.1.4 Dissolved Oxygen Data to February 2013 DO data were collected using surface DO meters at each well approximately weekly from the beginning of the test in June 2012 to February 2013, approximately four months before the test ended (Figure 5.4). These data did show DO increases in the injection wells, then declines as two of the wells (IW-2P and IW-3P) were taken out of service due to daylighting and short circuiting, respectively. Monitoring wells MW-1, MW-2, and MW-3 showed small but statistically significant increases in DO over the 12-month test. The highest concentrations were less than 3 mg/L, indicating some oxygen was being delivered to these wells but that it was likely being removed rapidly by biodegradation. No dissolved phase monitoring of well MW-4 was performed due the presence of LNAPL in the well. Interestingly, DO concentrations in the two background wells increased in the same pattern as the three monitoring wells: < 0.5 mg/L before the test, then slowly rising over the year test to the 1 to 3 mg/L level. This indicates that trace amounts of DO from the sparging system was reaching these wells which were originally envisioned as background wells. Monitoring well MW-2 showed a rapid increase in concentration in month 7, then a decrease back to low levels (between 1 and 2 mg/L). During this period injection well IW-3R began to short circuit to the original IW-3P, which had been taken out of service due to daylighting. Monitoring well MW-2 is located near IW-3R and IW-3P (Figure 4.1), which may explain the high DO concentrations observed in MW-2 during the short-circuiting event. One issue with the periodic DO readings is that these readings were not collected at the same time each day, relative to the injection period. Therefore, some readings were indicative of DO concentrations immediately after a pulse, while some were indicative of conditions after any spike of DO would have been consumed. These readings, on average, indicate trends in DO readings, but the use of downhole DO monitors (absent interference from LNAPL) are capable of providing a more sophisticated snapshot of the DO trends. RESULTS: Dissolved Oxygen, ORP, and Other Field Parameters High DO concentrations were most apparent in the injection wells, and in one monitoring well where a short-circuiting event through the monitoring well screen was likely occurring. After about four months, small but statistically significant increases in DO (0.5 to 3 mg/L) were observed in the three working monitoring wells and in both background wells. The pattern of these increases suggest that the biosparging system was delivering oxygen to the areas monitored by these wells. Optical DO sensors did not perform well in the startup phase. After conferring with the manufacturing, the presence of small amounts of LNAPL may have compromised the results. In a subsequent injection test conducted by a Shell POBS expert and the AECOM field team, the optical DO probes worked well in one test, but not in a second test in another well. Caution should be exercised if deploying optical DO sensors in wells with the potential for LNAPL presence. LA LNAPL Workgroup 15 Pulsed Oxygen Biosparging Pilot Test October 2015 5.2 Groundwater Monitoring Data: Dissolved Constituents 5.2.1 Concentration vs. Time Graphs During the 12-month testing period, reductions in benzene and BTEX concentrations were observed in groundwater, and remained low sixteen months after the system shutdown (Figures 5.5 and 5.6). Smaller reductions were observed for TPH-All Fractions (sum of Gasoline Range, Diesel Range, and Motor Oil Range) (Figure 5.7). In injection well IW-1P, which had the least operational problems, benzene concentrations were reduced by over two orders of magnitude, with the final concentration of 5 µg/L maintained for sixteen months after shutdown. The monitoring wells (circle symbols in Figures 5.5 through 5.7) showed much less reduction than the injection wells (triangle symbols). The TPH-All Fractions data showed a more muted response, with a very slow downward slope of concentrations on Figure 5.7. This is consistent with the original conceptual model for the POBS process, which targets composition change of the lighter components, such as the BTEX compounds, compared to the heavier compounds measured in the TPH analyses. Rebound testing was conducted 16 months after the post-test sampling event and is shown in Figures 5.5 – 5.7. 5.2.2 Concentration vs. Time Bar Charts The detailed temporal concentration vs. time records for every well is shown for Benzene (Figure 5.8), combined BTEX (Figure 5.9), and TPH-All Fractions (Figure 5.10). The detailed figures show the impact of operational changes on the individual wells at specific times. For example, reviewing these figures show: Injection well IW-1P had the highest reduction of any well for benzene and BTEX. This well had no operational problems during the test and delivered the most oxygen (15,700 SCF) and had the lowest initial benzene and BTEX concentrations of the three injection wells. Benzene and BTEX concentrations increased in Injection well IW-2P after it had to be shut down in month 7 (January 2013). High DO in MW-2 from the short-circuiting event resulted in a temporary anomalously low concentration of benzene and BTEX in month 8.5; Relatively little change in the background wells for benzene, BTEX, and TPH; Less fluctuation and little apparent change in the TPH-All Fractions data. Figure 5.11 shows the geometric means of the injection wells, monitoring wells, and background wells over time for benzene, BTEX, and TPH-All Fractions. The geometric means in this figure are for all the wells available for each specific sampling event, leading to the use of different number of wells for the different time periods if a well was not sampled LA LNAPL Workgroup 16 Pulsed Oxygen Biosparging Pilot Test October 2015 (due to the presence of LNAPL, for example) or if a well was abandoned (IW-3P). Therefore a different analysis using the same before- and after-test wells were used for the comparison in Table 5.1, as discussed in Section 5.2.3. Note the Post Test bars (far right in Figure 5.11) were taken two months after shutdown, and the rebound testing was taken sixteen months after shutdown. The injection wells show a dramatic reduction in benzene and BTEX concentrations over time, even sixteen months after the test was halted (i.e., rebound testing). TPH-All Fractions concentrations in the injection wells decreased somewhat, but fluctuated during the test with a significant rebound observed during post-test sampling and rebound testing. The background wells fluctuated over time, with two wells (MW-5 and MW-6) showing what appears to be rebound after the test (even though these wells were located relatively far away from the injection wells). 5.2.3 Summary Statistics: Before vs. After Concentrations for Groundwater Geometric means of Before Test (two months before test), After Test (last sample taken ranging from month 8.5 – 14), and Rebound Testing (month 30) were calculated and shown in Table 5.1. Additionally, a Test Percent Reduction was calculated using Before vs. After data, and an Overall Reduction was calculated using Rebound vs. Before data. For this analysis MW-7 was not used because After Test data were not available. Table 5.1.A Geometric Means of Before, After, and Rebound Constituent Groundwater Concentrations for Injection Wells Benzene Toluene BTEX Ethylbenzene Total Xylenes DIPE GRO TPH All Fract. DRO TPH Motor Before (µg/L) 795 674 2,737 102 809 287 11,899 46,659 26,543 4,076 GEOMEAN CONCENTRATIONS INJECTION WELLS (µg/L) Rebound After Test % (µg/L) (µg/L) Reduction 16 98% 42 22 97% 14 154 94% 163 9 92% 9 100 88% 92 67 77% 71 3,142 74% 3,409 32,061 31% 45,817 19,952 25% 34,192 5,536 -36% 45,817 Rebound vs. After 155% -35% 6% 4% -8% 6% 8% 43% 71% 43% Overall Reduction 95% 98% 94% 91% 89% 75% 71% 2% -29% -89% Notes: i) Before data from IW-1P, IW-2P and IW-3P used; ii) latest recorded values used for "After" and “Rebound” concentrations if unavailable; iii) Positive rebound percentage indicates increase in concentration compared to “After” value, while negative value shows decrease. LA LNAPL Workgroup 17 Pulsed Oxygen Biosparging Pilot Test October 2015 Table 5.1.B Geometric Means of Before, After, and Rebound Constituent Groundwater Concentrations for Monitoring Wells Inside Treatment Area GEOMEAN CONCENTRATIONS MONITORING WELLS INSIDE TREATMENT AREA (µg/L) Before After Test % Rebound Rebound (µg/L) (µg/L) (µg/L) Reduction vs. After 36,133 17,609 51% 18,293 7% 345 169 51% 153 -10% 7,079 3,471 51% 4,818 39% 47,111 24,310 48% 26,497 9% 471 261 45% 240 -8% 370 223 40% 334 50% 1,388 934 33% 1,054 13% 445 359 19% 391 9% 3,229 3,095 4% 2,659 -14% 89 81 9% 25 -69% DRO DIPE GRO TPH All Fract. Toluene Benzene BTEX Total Xylenes TPH Motor Ethylbenzene Overall Reduction 48% 56% 32% 44% 49% 10% 24% 12% 18% 72% Notes: i) Before data from MW-1, MW-2, MW-3 and MW-4 used; ii) latest recorded values used for "After" and “Rebound” concentrations if unavailable; iii) Positive rebound percentage indicates increase in concentration compared to “After” value, while negative value shows decrease. Table 5.1.C Geometric Means of Before, After, and Rebound Constituent Groundwater Concentrations for Monitoring Wells Outside Treatment Area Total Xylenes DRO TPH All Fract. GRO TPH Motor Benzene Toluene DIPE BTEX Ethylbenzene GEOMEAN CONCENTRATIONS MONITORING WELLS OUTSIDE TREATMENT AREA (µg/L) Rebound Before After Test % Testing Rebound (µg/L) (µg/L) (µg/L) Reduction Percent 473 343 28% 335 -2% 19,975 14,704 26% 16,125 10% 33,411 25,097 25% 25,155 0% 8,139 6,989 14% 5,821 -17% 2,774 2,700 3% 2,627 -3% 643 655 -2% 574 -12% 266 273 -3% 240 -12% 57 59 -4% 43 -26% 1,542 1,671 -8% 1387 -17% 57 187 -227% 112 -40% Overall Reduction 29% 19% 25% 28% 5% 11% 10% 24% 10% -96% Notes: i) Before and after data for MW-5 and MW-6 used ii) Positive rebound percentage indicates increase in concentration compared to “After” value, while negative value shows decrease. The groundwater data were found to be log-normally distributed rendering the geometric mean concentration values meaningful for comparison. The injection wells exhibited the expected percentage reduction versus chemical or chemical class in the before- and aftertest results. Benzene had the highest percent reduction (98%), followed by toluene, BTEX LA LNAPL Workgroup 18 Pulsed Oxygen Biosparging Pilot Test October 2015 and ethylbenzene in the injection wells. These results are consistent with the conceptual model as the aromatic compounds are seen to have degraded more readily than TPH. These data also show the high dissolved oxygen concentrations near the injection wells stimulated aerobic and intense biodegradation process that removed over 90% of the dissolved constituents. Rebound testing of the injection wells showed an increase in concentration of benzene (155%) compared to “After” concentration (from 16 µg/L to 42 µg/L). Rebound also occurred for DRO (71%), and TPH (43%). Average rebound percentage of all constituents in the injection wells was 29%, indicating some rebound in the injection wells. However, the overall percent reduction, taking rebound into account, remained high (71% to 98%) for all constituents except for TPH (All Frac. and motor) and DRO. The data for the monitoring wells within the treatment area have a different relationship than the injection well data, however. The TPH showed a greater reduction than the aromatic BTEX; the reason for this result is unknown. Among the BTEX compounds, only benzene and toluene were removed. The much lower dissolved oxygen concentrations at the monitoring wells were likely responsible for the much lower and more selective removals of hydrocarbon constituents from the dissolved phase (only 28% to 38% of the benzene, toluene, and TPH was removed). Rebound testing in the monitoring wells within the treatment area showed the highest rebound of benzene (35%), followed by GRO (28%). However, the average rebound percentage of all constituents was -2%, indicating no rebound and a continued decrease in concentrations. The overall percent reduction in the monitoring wells inside the treatment area ranged from 2% to 62% for all constituents except total xylenes, which increased by 10%. Monitoring wells outside of the treatment area did not exhibit any trends related to the treatment. Similarly, rebound testing indicated no rebound of concentrations. Overall percent reductions ranged from 5% to 29% for most constituents, with a 96% increase in ethylbenzene. RESULTS: Benzene, BTEX, and TPH in Groundwater Over 90% of the dissolved phase benzene and BTEX compounds were removed overall from the high-oxygen zone around the injection wells (Table 5.1.A), with lower removals for TPH (2%) which is consistent with the aerobic biodegradation process. Lower oxygen levels at the monitoring wells located away from the injection wells likely caused much lower removals of benzene (2%) and toluene (35%) and no removal of ethylbenzene or xylenes (Table 5.1.B). Better removal was associated with the injection well with the fewest operational problems and lowest initial concentrations (IW-1P, see Figure 5.8). In a few specific cases, high DO was correlated to reductions in benzene and BTEX (Figures 5.4, 5,8, and 5.9). Some rebound occurred in the injection wells. Rebound did not affect the overall reduction in concentrations at these locations, and the overall reduction percentages were similar compared to the “Before” vs. “After” difference. LA LNAPL Workgroup 19 Pulsed Oxygen Biosparging Pilot Test October 2015 5.3 Soil Data From Before- and After-Test Borings 5.3.1 Visualization of Soil Data Thirteen paired before- and after-test data provided unexpected results: minimal changes in benzene and BTEX, and significant increases in soil TPH-All Fractions data. The data showed considerable variability, with the before- and after-test borings near MW-1, MW-2, and MW-3 having lower benzene and BTEX concentrations than MW-4, and MW-4 having the highest TPH-All Fractions sampling results (Figure 5.12). In nine of 13 samples, the TPH-All Fractions concentrations increased. At all four borings, the highest concentration present at any depth interval was an after-test sample (Figure 5.12). Figure 5.13 shows a “triangle plot’, where the concentration of a constituent in the beforetest sample is used for the X-axis, and the after-test concentration is used for the Y-axis. The resulting plots show changes, either reductions in concentration which fall below the black 45-degree line, or increases in concentration which fall above the black 45-degree line. This figure shows slight decreases for most benzene samples, and unexpected significant increases in TPH for most soil samples. 5.3.2 Before and After Average Concentration Summary statistics using both arithmetic means and geometric means of all the paired data show the increase in TPH-ALL Fractions, TPH-GRO, and TPH-DRO (Table 5.2). These data are log-normally distributed, so: the geometric mean provides an indication of the change at any point in the test zone; the arithmetic average indicates the change in the cumulative concentration (mass) in the test zone. LA LNAPL Workgroup 20 Pulsed Oxygen Biosparging Pilot Test October 2015 Table 5.2. Arithmetic and Geometric Averages of Beforeand After-Test Soil Data. Note: positive percent reduction value is a reduction, negative is an increase. The following constituents and TPH fractions are not shown because more than 50% of the samples were nondetect Diisopropyl Ether (DIPE) Carbon Chain C6 Carbon Chain C23-C24 Carbon Chain C25-C28 Carbon Chain C29-C32 Carbon Chain C33-C36 Motor Oil Range (C28 to C36) LA LNAPL Workgroup Arithmetic Average (for evaluating change in mass) Toluene Benzene BTEX Ethylbenzene Xylenes, Total Naphthalene Carbon Chain C21-C22 Carbon Chain C9-C10 Carbon Chain C19-C20 Carbon Chain C11-C12 Carbon Chain C17-C18 TPH as Gasoline (C6-C12) TPH All Fractions (C6-C44) TPH Diesel Range (C13 to C28) Carbon Chain C13-C14 Carbon Chain C15-C16 Carbon Chain C7 Carbon Chain C8 Geometric Mean (for change at any point in tmt. Zone) Benzene Toluene Ethylbenzene BTEX Carbon Chain C21-C22 Xylenes, Total Carbon Chain C17-C18 Carbon Chain C19-C20 Carbon Chain C9-C10 Naphthalene TPH as Gasoline (C6-C12) Carbon Chain C11-C12 TPH All Fractions (C6-C44) TPH Diesel Range (C13 to C28) Carbon Chain C13-C14 Carbon Chain C15-C16 Carbon Chain C8 Carbon Chain C7 21 Before (mg/kg) 16 9.1 85.6 10.9 49.6 13.9 126 813 182 1,542 369 2,600 5,151 2,481 1,291 528 139 201 Before (mg/kg) 1.1 3.8 4.8 24.7 94 13.3 292 143 514 9.4 1,788 1,122 3,604 1,636 843 372 123 98 After (mg/kg) 13.7 8.1 85.6 11 52.8 19.2 188 1,343 313 2,682 647 4,722 9,361 4,536 2,365 1,037 337 564 After (mg/kg) 0.83 2.9 4.9 25.7 114 16.1 370 193 699 13.4 2,764 1,746 5,776 2,751 1,463 649 246 214 Percent Reduction 14% 11% 0% -2% -6% -38% -50% -65% -72% -74% -75% -82% -82% -83% -83% -96% -141% -181% Percent Reduction 25% 24% -2% -4% -21% -21% -27% -35% -36% -42% -55% -56% -60% -68% -74% -74% -100% -119% Pulsed Oxygen Biosparging Pilot Test October 2015 Benzene concentrations in soil decreased slightly during test, total BTEX concentrations stayed about the same, and TPH increased. The result of the increased TPH, however, is that the mass fraction of benzene and total BTEX dropped significantly during the biosparge test because the other compounds increased in concentration. When using the arithmetic averages: For benzene, the mass fraction dropped from 0.18% to 0.087% (a 51% reduction). For BTEX, the mass fraction dropped from 1.67% to 0.92% (a 45% reduction). However, the majority of the reduction was due to toluene and benzene with no change in concentration of xylene or ethylbenzene. For the remainder of the report, please note that any discussion of reduction in BTEX soil concentration is driven only by reduction in benzene and toluene. The reduction in benzene and BTEX mass fraction indicate that a composition change did occur due to the oxygen biosparging process. 5.3.3 Statistically Significant Decreases and Increases The decrease in concentration for the 13 paired samples were statistically analyzed using a Wilcoxon Signed-Rank Test. This non-parametric test indicated that: The decrease in benzene, while only 11% for the arithmetic mean, was statistically significant at the p=0.05 level. This is explained by the distribution of the paired samples: 11 of the 13 samples showed decreases in benzene, while only two showed an increase. Benzene was the only compound that showed a statistically significant decrease in concentration, but the TPH All Fractions data showed a p-value of 0.08 for a twotailed test, an almost statistically significant increase in concentration compared to the p=0.05 level. Both the decrease in benzene and BTEX mass fractions were statistically significant at the p=0.05 level, with p values of 0.01 and 0.03 respectively. In summary, the soil data show a statistically significant reduction in the mass fraction of both benzene and BTEX during the test, confirming a composition change did occur. While the increase in TPH concentrations in soil before and after the test was not statistically significant, it was large (55% increase). This may have been due to an actual inflow of LNAPL during the test (perhaps due to the surging from the oxygen pulses), or may have been just a low-probability (p = 0.077) result of soil sampling variability. Other before- and after-test data were analyzed to see if these data supported the hypothesis of significant LNAPL inflow into the test zone. LA LNAPL Workgroup 22 Pulsed Oxygen Biosparging Pilot Test October 2015 5.3.4 Before-Test CPT and UVOST The LA LNAPL POBS Pilot Test used a number of LNAPL characterization methods along with measurements of how groundwater and soil concentrations changed: The CPT tool provided information on the stratigraphy of the test area (Figure 5.14) and was the primary method to evaluate the thickness and composition of the aquifer media in the test zone. The UVOST test provided a semi-quantitative indication of the presence of LNAPL, via measurement of the fluorescence response of the polycyclic aromatic hydrocarbon (PAH) constituents in the LNAPL. The test area was selected in part based on the ROST (a precursor test to the more recent UVOST test) and CPT results from PA-11 (Figure 5.14), which showed a thick, permeable sand unit near the bottom of the boring (~ 50 feet bgs) and much poorer permeability in the shallow zone and a stronger ROST response in the deeper unit. However, when six CPT/UVOST borings were advanced in 2012, the opposite seemed to be the prevalent condition: more sand (yellow color in Figure 5.14) and higher UVOST response in the shallow unit compared to the deeper unit. This potentially shows some of the pitfalls in comparing ROST vs. UVOST and illustrates the variability of this very heterogeneous formation. In the end, there was significant accumulation of LNAPL in wells screened in the deeper zone (~45 to 50 feet bgs), but none or limited LNAPL in shallower wells (23-25 feet bgs). While the 2012 CPT results suggest this shallow unit was a contiguous sand unit in all six CPT logs, this unit was very difficult to sparge, with the Pilot Test experiencing several daylighting events due to pore permeability in the injection zone. 5.3.5 Before vs. After UVOST, Core Photography, and Soil Analysis Because the UVOST responds to PAHs, the UVOST is more useful for measuring the relative amount and distribution of a uniform LNAPL, but potentially less informative about compositional change processes that do not preferentially remove PAHs. In other words, reduction of benzene and BTEX from LNAPL may not materially change the UVOST response. Core photography has some of the same limitations, where a UV light is shined on a core section creating a white image on the core photograph wherever LNAPL is present. All four core locations had before- and after-test UVOST results which are shown along with the corresponding CPT logs and small insets of the core photography (Figures 5.15 to 5.18). In Figures 5.15 and 5.16, the blue image in the UVOST section (the right panel of each log) is the before-test UVOST response, and the colored, banded response is the after-test response. In general, the after-test UVOST response was lower than the before-test LA LNAPL Workgroup 23 Pulsed Oxygen Biosparging Pilot Test October 2015 response, suggesting some removal of PAHs from the test area. Interestingly, the most noticeable response was in MW-3 in the 12-15 foot bgs interval, which is in a clay unit and significantly higher than the injection zone from 23 to 25 feet bgs. A few intervals seemed to show a higher after-test response (e.g., MW-3 at 27 feet bgs, but this was atypical). The key treatment zone between 10 and 30 feet was expanded in Figures 5.17 through 5.19 to show the before- and after-test core photography and soil analysis. In figures, blue numbers on the left are the before-test TPH-All Fraction data, and the green values on the right are the corresponding after-test data. The after-test core photographs for MW-3 and MW-4 are shown in Figure 5.19; however, there are no corresponding before-test photos for these borings. Additionally, no core was recovered from boring MW-2 between 22 and 24 feet bgs. For the purpose of the analysis, samples immediately above and below the missing interval were paired with two before-test soil samples collected in the 22 to 24 foot bgs interval. The before- and after- soil values show increases in TPH-All Fractions in four of the seven samples with core photography, but no obvious increase in the white images in the core photography (Figure 5.19). However, the key 22 to 24 foot bgs interval is missing in the MW-2 core, leaving the MW-1 core as the key comparison. In the MW-1 core, there appears to be a much whiter image near the 24 to 25 foot interval, but the rest of the aftertest image has similar or even less white image than the before-test image. Therefore the hypothesis of inflow of LNAPL is not confirmed by the core photography. While MW-3 shows a very intense after image, the lack of a before-test image makes it difficult to interpret this observation. 5.3.6 Before vs. After Core Photography and Pore Fluids Analysis Methods such as the Dean-Stark test are used to measure LNAPL saturation, which is the percentage of the pore space filled with LNAPL. Two before- and after-test saturation measurements were taken and are shown in Figure 5.20. At the first pore saturation location (MW-1), the data showed that LNAPL saturation decreased from 12.3% of the pore space to 5.5% of the pore space at the 23 feet bgs depth (Table 5.3). The soil samples (Figures 5.17 and 5.19) taken from near this depth showed an increase in TPH-All Fractions from 5,500 mg/kg to 17,000 mg/kg at 23 feet bgs. At the second pore saturation location (MW-2), the two saturation samples were separated by about 0.5 feet, and showed little difference: 7.7% before vs. 7.6% after-test. The two nearest soil samples show a decrease from 13,000 mg/kg to 7,800 mg/kg and an increase from 10,000 mg/kg to 22,000 mg/kg, but these before-and-after sample intervals are separated by over a foot. The before and after soil samples generally showed an increase in TPH concentration, the reason for this trend is unknown. Insufficient LNAPL data collection and the heterogeneity of the soil analysis prevent any statistically significant conclusions. LA LNAPL Workgroup 24 Pulsed Oxygen Biosparging Pilot Test October 2015 Table 5.3. Before and After Pore Fluids Analysis Data for Shallow Zone Before Test Change After Test Depth (ft) Porosity (%) Before NAPL Saturation (%pv) MW-1 23.2 46.8 12.3 23.5 44.1 5.5 6.8 MW-2 23.6 46.3 7.7 24.1 46.7 7.6 0.1 MW-2 No sample 20.6 50.6 7.1 - MW-2 No sample 22.3 53.3 7.1 - Location Depth (ft) Porosity (%) After NAPL Saturation (%pv) Change (Before After) Shallow Zone LNAPL mobility using a centrifuge test was analyzed at one location before- and after-test (Table 5.4). A section of the soil core is measured for LNAPL saturation initially, then the remaining core is centrifuged at 1000 g to remove any mobile LNAPL. After centrifuging, the LNAPL saturation is measured once again. The mobility analysis was not supportive of the LNAPL inflow hypothesis. There was some, but not much mobile LNAPL before the test (mobile fraction of 0.3% of pore space) and zero afterward. This analysis suggested residual LNAPL was present at the MW-1 location after the test. Table 5.4. LNAPL Mobility Test Results Using the Centrifuge Method Before Test Location MW-1 Depth (ft) Dry Bulk Density (g/cc) Total Porosity (%) Initial NAPL Saturation (%pv) NAPL Sat. After Centrifuge 1000xG (%PV) Mobile LNAPL Fraction (%) 20-24.5 1.47 45.9 9.5 9.2 0.3 After Test Location MW-1 Depth (ft) Dry Bulk Density (g/cc) Total Porosity (%) Initial NAPL Saturation (%pv) NAPL Sat. After Centrifuge 1000xG (%PV) Mobile LNAPL Fraction (%) 19-23.9 1.46 46.0 7.9 7.9 0.0 In summary, the LNAPL Pore Fluids analysis did not show an influx of LNAPL, but the analysis was limited to a single comparison in two separate cores. The soil TPH data, in LA LNAPL Workgroup 25 Pulsed Oxygen Biosparging Pilot Test October 2015 general, showed a concentration increase suggesting a potential LNAPL inflow during the test. The LNAPL mobility analysis at core location MW-1 showed LNAPL mobility fell from 0.3% of pore space prior to the Pilot Test to zero mobile fraction after the Pilot Test. RESULTS: Soil Data Average benzene concentrations in soil decreased slightly before and after the test (11% reduction using an arithmetic average). This decrease is statistically significant at the p=0.05 level. Total BTEX was unchanged (Table 5.1). The average concentration of the TPH-All Fractions increased by 82% before and after the test (from 5150 mg/kg to 9360 mg/kg). Both GRO and DRO had similar increases (Table 5.2). These results were nearly as statistically significant as the benzene results above. The mass fraction of both benzene and BTEX decreased by 51% and 45% respectively during the test (Section 5.3.2). However, the majority of the reduction was due to toluene and benzene with no change in concentration of xylene or ethylbenzene. These decreases were statistically significant at the p=0.05 level. This confirms that a significant composition change (removal of benzene and BTEX) did occur during the year-long test. This increase in TPH has two potential explanations: 1) an LNAPL inflow during the test, potentially due to the surging action of the oxygen pulses; 2) natural variability during the soil sampling. The UVOST and core photography data do not indicate LNAPL inflow (Figures 5.17 to 5.19), and the subsequent data analysis (Section 6.4) was performed assuming this increase was just natural variability. Only two pairs of before and after LNAPL saturation data were available for analysis. These two pairs of LNAPL saturation data for MW-1 and MW-2 (Figure 5.20) either decreased or stayed the same (12.3% – 5.5% and 7.7% – 7.6%). The before and after soil samples generally showed an increase in TPH concentration (Figure 5.17 and 5.19), the reason for this trend is unknown. Insufficient LNAPL data collection and the heterogeneity of the soil analysis prevent any statistically significant conclusions. Key Figures: 5.12 to 5.20 5.4 Mass Balance Analysis with Increasing TPH Concentrations A mass balance analysis was performed using the arithmetic averages of the soil data (Table 5.5). LA LNAPL Workgroup 26 Pulsed Oxygen Biosparging Pilot Test October 2015 Table 5.5. Arithmetic Average Concentration Before and After Pilot Test Benzene (mg/kg) BTEX (mg/kg) TPH- ALL (mg/kg) GRO (mg/kg) DRO (mg/kg) Pre-Test Post-Test % Reduction 9.1 8.1 11% 86 86 0% 5,151 9,361 -82% 2,600 4,722 -82% 2,481 4,536 -83% Statistically Significant? Yes No No No No Notes: Negative % Reduction indicates an increase in average concentrations. GRO = Gasoline Range Organics, DRO = Diesel Range Organics First, a treatment volume was estimated by calculating the area of the green zone in Figure 3.5 of 2,885 square feet (0.066 acres), and treatment zone thickness of five feet, and a saturated soil bulk density of 1.9 grams/cm3. This resulted in a treatment volume of 534 cubic yards. The resulting before and after estimated contaminant masses are shown in Table 5.6. Table 5.6. Calculated Changes in Mass of Benzene, BTEX, and TPH Fractions Benzene (kg) BTEX (kg) TPH-All (kg) GRO (kg) DRO (kg) Before 7.1 66.4 3,995 2,020 1,924 After 6.3 66.5 7,260 3,660 3,518 Change -0.8 0.1 3,265 1,640 1,594 Note: BTEX, TPH-All, GRO, and DRO showed increases after test. A more detailed assessment of the mass balance was performed assuming a range of possible values for the mass of TPH during the test (Table 5.7) using the following approach: 1) The changes in the mass fraction are representative of the before and after conditions at the site. 2) The TPH didn’t change during the test, but there is a lower range estimate of the TPH mass (3,995 kilograms from the before data) and a higher range estimate (7,260 kilograms from the after data), consistent with Table 5.6. 3) All the calculated BTEX removal was caused by aerobic biodegradation via the oxygen biosparging. As shown in Table 5.7, the following mass removal ranges for benzene and BTEX were: Benzene: between 3.6 - 6.5 kilograms was removed (51% removal) BTEX: between 30 - 55 kilograms was removed (45% removal) LA LNAPL Workgroup 27 Pulsed Oxygen Biosparging Pilot Test October 2015 Note if the increase in TPH was due to LNAPL inflow, then the removal of BTEX would be close to the high range removals in Table 5.7 (6.5 kg of benzene, 55 kg of BTEX). Table 5.7. Revised Mass Removal Estimate for Benzene and BTEX Based on Change in Mass Fraction (assuming increase in TPH was due to sampling variability) LOW RANGE MASS REMOVAL ESTIMATE Before After Change TPH Mass Benzene Mass Fraction (kg) (%) 3995 0.18% 3995 0.087% 0 0.09% BTEX Mass Fraction Benzene Mass (%) (kg) 1.67% 7.1 0.92% 3.5 0.75% BTEX Mass (kg) 67 37 30 Before After Before-After 7260 0.18% 1.67% 12.8 121 7260 0.087% 0.92% 6.3 67 0 0.09% 0.75% 6.5 55 3.6 HIGH RANGE MASS REMOVAL ESTIMATE TPH Mass Benzene Mass Fraction BTEX Mass Fraction Benzene Mass BTEX Mass (kg) (%) (%) (kg) (kg) The removal can be converted to an equivalent value in units of gallons of LNAPL removed per acre per year, assuming the test area was about 0.066 acres and the test lasted about a year: between 138 and 253 gallons (of only BTEX) per acre per year from a five-foot saturated interval. In comparison, the Natural Source Zone Depletion pilot test indicated a NSZD depletion rate on the order of 1700 gallons per acre per year at the Shell facility. However, this may not be an appropriate comparison, as the Biosparge removals were focused on BTEX compounds in the saturated zone, vs. removal of potentially more compounds for the NSZD process, in both the saturated and unsaturated zone. It is likely that the calculated volume of removed BTEX is in addition to, or a minor component of, mass degraded through NSZD. In addition, one member of the LA LNAPL project team hypothesized that the presence of wells in the test area may present a pathway for recharge of LNAPL at the top of the water column, as the vast majority of LNAPL in this area is trapped in submerged lenses. This could explain the increase in TPH concentrations in soil during the year-long biosparge test, an increase which was accompanied by statistically significant reductions in benzene and BTEX mass fraction in soil. LA LNAPL Workgroup 28 Pulsed Oxygen Biosparging Pilot Test October 2015 RESULTS: Mass Balance The treatment zone size was estimated to be 0.066 acres and 534 cubic yards. Lower range and higher range estimates of mass removal were calculated using the lower and higher mass estimates for TPH before and after the test. Benzene removed: between 3.6 – 6.5 kilograms (51% removal) BTEX removed: between 30 - 55 kilograms (45% removal), equivalent to 170 to 310 gallons of only BTEX per acre per year from a five-foot saturated interval. The Natural Source Zeon Depletion Test (NSZD) at the Shell facility measured 1700 gallons of LNAPL degraded per acre per year, but was measuring the degradation of many LNAPL components in the entire soil column. Key Table: 5.7 5.5 Stoichiometric Analysis of Oxygen Injection A planning level stoichiometric analysis of the amount of oxygen delivered to the test zone with a range for biodegradation capacity between 1 to 3 kilograms of oxygen required to degrade one kilogram of BTEX (see Wiedemeier et al., 1999) (the 3:1 ratio assumes no cell growth; 1:1 ratio assumes cell growth occurred during the test) is shown below: 38,600 SCF of oxygen added to treatment zone, equivalent to: 48,800 moles of oxygen, equivalent to: 1,560 kilograms of oxygen, equivalent to: The capacity to degrade 1,560 to 520 kilograms of aromatic hydrocarbons (BTEX) (assuming a 1:1 and 3:1 oxygen: BTEX stoichiometry). Then assuming the removal of BTEX (between 30 - 55 kg) was all due to biodegradation (no volatilization), and the range of BTEX mass removed in Table 5.7, then between 1.9% to 10.6% of the oxygen was consumed for BTEX biodegradation. RESULTS: Stoichiometric Analysis If the mass balance estimate based on LNAPL inflow is correct, then potentially 1.9% to 10.6% of the oxygen delivered to the treatment zone was consumed for biodegradation of BTEX. LA LNAPL Workgroup 29 Pulsed Oxygen Biosparging Pilot Test October 2015 5.6 Key Questions About the Mass Balance Analysis The mass balance analysis is discussed in a question/answer format below. If an LNAPL inflow did cause the before- and after-test increase in soil concentrations, why wasn’t this observed in the ROST, core photography, or LNAPL saturation/mobility data? Response: The simplest answer is there was no actual increase in TPH concentrations, but that the 55% increase was the result of sampling variability. The UVOST data is sensitive to polyaromatic hydrocarbons such as naphthalene, but naphthalene concentrations increased by 42% during the test (Table 5.2). So the observed reduction in UVOST signal does not correlate to the soils data for naphthalene. Similarly, the core photography is conducted using a UV light, which is measuring the same general constituents as the UVOST. The limited LNAPL saturation data was inconclusive and did not contribute to answering this question. The only complete comparison of core photography to TPH data is at MW-1 (Figure 5.19). This soil data overall shows about a 60% increase in TPH (average of 6,700 mg/kg before and 10,700 mg/kg after) for the bottom three samples with corresponding before- and aftercore photos. The bottom sample at 24.3 feet shows a noticeable increase in brightness. The other two appear to show higher response in the before photo, but this is fairly subjective. The core photography does not support the inflow theory. The LNAPL mobility test at MW-1 showed higher before LNAPL saturations with a very small mobile fraction (0.3%) before the test, and lower saturations with no mobility after the test (Table 5.5). These limited data do not support LNAPL inflow during the test. Overall, it is more likely that the increase in TPH was due to sampling variability, even though the increase in TPH concentrations was almost statistically significant. Are there any other data that suggest that LNAPL inflow occurred during the test? Response: Not really. First, LNAPL accumulation in all seven wells was tested throughout the test. In the beginning one monitoring well (MW-4) and one background well (MW-7) had LNAPL accumulations during startup and during each of the subsequent monitoring events. Then LNAPL appeared in monitoring well MW-3 in August 2013, two months after the test was completed, indicating mobile LNAPL had reached this well located in the very center of the test area. In December 2013 LNAPL was observed in IW-2P. The appearance of mobile LNAPL in these wells suggests that LNAPL inflow is possible in this area. But there was no observed LNAPL accumulation in the monitoring wells during the test, arguing against LNAPL inflow. LA LNAPL Workgroup 30 Pulsed Oxygen Biosparging Pilot Test October 2015 Second, the groundwater data (Table 5.1) show an increase for only one contaminant class: TPH Motor oil. This fraction is the least aerobically degradable, and increased by 12% during the test. Is the TPH data controlled by the one after-test sample collected at MW-4 at 22.5 feet bgs, where the TPH-All Fraction data increased from 3,000 mg/kg to 29,000 mg/kg? Response: This sample has a significant effect but not controlling effect on the mass balance. If this sample pair is removed, the TPH-All Fraction data still increases by 45% (5,330 mg/kg to 7,724 mg/kg), compared to the 82% increase in the complete database (5,131 mg/kg to 9,361 mg/kg). Is it possible that most of the removal of benzene and BTEX was from volatilization and not from aerobic biodegradation? In other words, this was more of an air sparging process than biosparging? Response: A typical three-well air sparging system would have delivered approximately 75,000 SCF of air to the subsurface in one week (Newell, 2012), assuming a 5 SCFM injection rate for each well and pulsing with 50% on-time. The POBS system for this Pilot Test only averaged about 700 SCF of gas injection per week. Therefore the amount of volatilization that would have occurred from this test would be much less (potentially 99% less) than an air sparging system. If volatilization is the primary method of removal, then there should be a trend of higher removal for compounds with higher Henry’s Law coefficient (which depends on how easy it is to remove chemicals from the dissolved phase) or the vapor pressure (which shows how easy it is to remove chemicals from the NAPL phase). However, there did not appear to be a correlation between the two volatilization parameters (Table 5.8) and removal (Table 5.2) for the BTEX compounds. As shown in Table 5.8, the highest values are in green with largest fonts, the lowest in red in small fonts, and don’t appear to show any correlation. Table 5.8. Volatilization Parameters for the BTEX Compounds vs. Percentage Removal Toluene Benzene Ethylbenzene Total Xylenes Henry's Law Coeff. (-) Vapor Pressure (mm Hg) Percent Removal in Soil (%) 0.26 0.22 0.32 0.29 3 95 10 7 14% 11% -2% -6% Finally, a mass balance was performed where the initial groundwater concentrations for the BTEX compounds were assumed to be in contact with the oxygen gas during the entire test, LA LNAPL Workgroup 31 Pulsed Oxygen Biosparging Pilot Test October 2015 and it was assumed that the oxygen volatilized these compounds out of the groundwater in proportion to their Henry’s Law coefficient. For example, 38,600 SCF is equivalent to about 1 million liters of gas. Assuming a concentration of 335 µg/L for benzene (using the geomean of both pre- and post-test injection and monitoring well data) and a unitless Henry’s Law coefficient of 0.22, the vapor phase concentration assuming complete equilibrium between the gas and water phases would be 1523 µg benzene per liter of gas. When multiplied together, the 1.09 million liters of gas could only strip about 1.7 kg. This calculation was repeated for the before-test BTEX compounds, and when combined, indicates that the 38,600 SCF of oxygen could have stripped only 5.43 kilograms of BTEX from the groundwater, less than the low range estimate of 30 - 55 kilograms in Table 5.7. Through similar calculations, the vapor phase concentration of benzene partitioning from LNAPL using vapor pressure of benzene indicated only 1.0 kg of benzene would have been removed if all the injected gas was in equilibrium with LNAPL While there certainly was some volatilization that occurred, any stripped volatiles would have been either trapped as residual oxygen bubbles in the groundwater, which would then have been biodegraded, or carried to the water table by the oxygen channels. The presence of oxygen and volatile aromatic compounds here would likely mean biodegradation of volatiles in the vadose zone. In summary, it is very unlikely that any removal of volatile, aerobically degradable compounds would not have resulted in biodegradation except in the unusual circumstances of “daylighting” or short circuiting. RESULTS: Key Questions A number of questions regarding key elements of the data analysis and conceptual model are asked and discussed in this section. 6.0 PILOT TEST PERFORMANCE SUMMARY The POBS post-test analysis was designed to evaluate the effectiveness and cost efficiency of applying POBS full scale for LNAPL remediation. The test results were analyzed to present the following performance metrics: 6.1 Change in LNAPL Mass in Treatment Zones The before- and after-test soil data were used to determine the following changes in LNAPL mass, assuming that the increase in TPH concentrations were due to sampling variability (see Section 5.8): LNAPL Mass Change During Test: assumed no change (as TPH-All Fractions) Benzene removed: between 3.6 - 6.5 kilograms (51% removal) BTEX removed: between 30 - 55 kilograms (45% removal) LA LNAPL Workgroup 32 Pulsed Oxygen Biosparging Pilot Test October 2015 6.2 Change in Apparent LNAPL Thickness at Wells in Treatment Zones There was very little change in apparent thickness in the monitoring wells. Wells MW-4 and MW-7 had apparent LNAPL thickness after the first pre-test sampling event, and were not sampled during the test. No other major occurrences of LNAPL accumulations were observed in the monitoring wells. 6.3 Change in Concentration and Mass Discharge (Mass Flux) in Treatment Zones To calculate mass discharge, the change in the geomean for both the injection wells and the monitoring wells was performed, because the downgradient vertical control plane over which mass discharge is evaluated would intersect groundwater that flows by both the injection and monitoring wells. Before and after geometric mean concentrations for injection wells and monitoring wells within the treatment area showed that benzene concentrations dropped from 844 µg/L to 133 µg/L (84% reduction), and BTEX concentrations from 2,672 µg/L to 690 µg/L (74% reduction). The change in mass discharge is directly related to the change in dissolved phase concentrations. For this test, groundwater sampling was conducted two months before and two months after the year-long Pilot Test. Mass discharge is a function of the vertical area of flowing groundwater, groundwater Darcy velocity, and the dissolved phase concentration. Groundwater Seepage Velocity = average of 2.3 feet/year (URS/GSI, 2010) Saturated thickness = 5 feet Arbitrary width = 500 feet Porosity = 0.2 Geometric mean benzene concentration of injection wells and monitoring wells inside treatment area before the test = 844 µg/L Geometric mean benzene concentration of injection wells and monitoring wells inside treatment area after the test = 133 µg/L Using the above values, the mass discharge before the test would be 0.08 grams benzene per day, and the mass discharge after would be 0.012 grams benzene per day, an 84% reduction in mass discharge. 6.4 Change in LNAPL Mobility As a phase-change technology, the POBS technology is not expected to have a large effect on LNAPL mobility. The before-test LNAPL mobility testing using the centrifuge method indicated that 0.3% of the LNAPL was removable by centrifuging. The after-test data showed no mobility (i.e., 0% of LNAPL removed by the centrifuge). This is not likely due to any response of the LNAPL to the oxygen biosparging, however. LA LNAPL Workgroup 33 Pulsed Oxygen Biosparging Pilot Test October 2015 LNAPL in two monitoring wells were discovered right during startup (monitoring well MW-4 and background well MW-7). These wells were located to the northeast edge of the treatment zone and beyond. In August 2013, two months after project shutdown, LNAPL was observed in MW-3, indicating mobile LNAPL had entered the treatment zone. In December 2013, LNAPL was observed in injection well IW-2P for the first time. Overall the test data does not indicate that LNAPL mobility was changed by the POBS process. 6.5 Change in LNAPL Composition in the Treatment Zones As expected with a composition change technology, the soil data showed a substantial reduction in the mass fraction of benzene and BTEX in LNAPL during the test. For benzene, the mass fraction dropped from 0.18% to 0.087% (a 51% reduction). For BTEX, the mass fraction dropped from 1.67% to 0.92% (a 45% reduction). 6.6 Concentrations of DO in the Treatment Zones DO data (Figure 5.4) started low, then increased in the injection wells (up to > 14 mg/L in some wells), and finally showed small increases (< 3 mg/L) in the monitoring wells during the test. These results suggest that the biosparge test was being pushed to treat a zone with considerable organic load in the form of LNAPL, and that even a year of biosparging (with a significant increase in sparge volume over initial plans) did not allow high concentrations of DO to persist throughout the treatment zone 6.7 Cost of Treatment when Applied to Full Scale Planning level, ± 50% costs for construction of the POBS system are provided below, adjusted for only the treatment system. Matrix Oxygen Injection Systems provides these costs: Skid mounted systems from 12 to 64 injection points; capital cost from $48K to $105K. Injection point installation costs generally range from $350 for shallow overburden points and up to $1,000 for deep overburden or bedrock points. $0.15 to $0.24 per point per day for electricity 30% of wells need to be replaced each year These costs were used to construct a low-end cost estimate for a refinery-terminal setting. Each injection point was assumed to cost $1K with another $1K in associated trenching/piping and site work. A $105K skid for 62 points was assumed (the midpoint of the reported skid-mounted unit). Because of the high oxygen delivery rate used for this test, an O&M cost of $0.12 per point per day was assumed, double the high-end electricity cost to account for the high oxygen delivery rates used for this pilot test. To treat a 20-acre zone would require 1,233 injection points and 20 skids. To account for design/approvals costs, the capital cost subtotal was increased by 25%. LA LNAPL Workgroup 34 Pulsed Oxygen Biosparging Pilot Test October 2015 Based on the operational problems of this biosparging project, it was assumed that 30% of the wells would require replacement or extensive rework every year. The O&M on the skids and overall system would require 15% of skid capital cost every year (6.7 year replacement period). Normalizing to area, a planning-level low-range cost was estimated for a large scale deployment of the technology. The high end doubled to account for the potential difficulty in drilling/operating in a refinery environment and the difficulties with biosparging associated with this pilot test, and to acknowledge the very general, planning level nature of these cost estimates. Capital cost: Annual O&M Cost: $300K to $600K per acre $60K to $120K per acre Note these capital costs are on the low end of capital costs plus O&M costs for in-situ treatment of $1 million to $5 million per acre (e.g., Sale et al., 2008). However, this cost estimates assumes only one vertical transmissive interval (no more than 20 feet thick) being treated. Multiple vertical injection points designed to treat multiple transmissive layers would increase the per-acre costs. RESULTS: Performance Metrics Seven performance metrics outlined in the Pilot Test work plan are evaluated in this section: Change in LNAPL Mass; LNAPL Apparent Thickness; Groundwater Concentration/Mass Flux; LNAPL Mobility; LNAPL Composition; and DO. The seventh metric was a planning level capital and O&M cost to perform a large scale implementation of the technology in dollars per acre. LA LNAPL Workgroup 35 Pulsed Oxygen Biosparging Pilot Test October 2015 7.0 REFERENCES Brown and Caldwell. (2007). Site Assessment Report, Former Process Area, Shell Carson Terminal, Carson, California. Prepared for Regional Water Quality Control Board, Los Angeles Region, May 2007. Bass, D. H., Brown, R.A., and Hastings, N.A. (2000). Performance of air sparging systems: a review of case studies. Journal of Hazardous Materials 72: 101-119. Geosyntec Consultants and URS Corporation. (2007). Light Non-Aqueous Phase Liquid (LNAPL) Investigation. Shell Oil Products Carson Terminal, Carson, California. Prepared for Equilon Enterprises LLC. December 2007. Geosyntec Consultants. (2008a). Light Non-Aqueous Phase Liquid (LNAPL) Recovery Pilot Test and Recovery Modeling Report. Shell Oil Products Carson Terminal, Carson, California. Prepared for Shell Oil Products US. May 2008. Geosyntec Consultants. (2008b). Supplemental Light Non-Aqueous Phase Liquid (LNAPL) Recovery Pilot Test and Recovery Modeling Report. Shell Oil Products Carson Terminal, Carson, California. Prepared for Shell Oil Products US. August 2008. Klinchuch, L.A., Goulding, N., James, S.R., and J.J. Gies. (2007). Deep Air Sparging – 15 to 46m beneath the Water Table. Ground Water Monitoring & Remediation. 27(3): 118-126. Leeson, A., Johnson, P.C., Johnson, R.L., Vogel, C.M., Hinchee, R.E., Marley, M., Peargin, T., Bruce, C.L., Amerson, I.L., Coonfare C.T., Gillespie, R.D., and D.B. McWhorter. (2002). Air Sparging Design Paradigm, Batelle, Columbus, Ohio. Los Angeles LNAPL Working Group, 2011. Light Non-Aqueous Phase Liquids (LNAPL) Literature Review Version 1.0, Western States Petroleum Association, Torrance, California. Newell, C.J., 2012. Air Sparging. vs. Oxygen Biosparging, Memo to LA LNAPL Workgroup, Oct. 29, 2012. NFESC, (2001). Air Sparging Guidance Document, Technical Report TR-2193-ENV, Naval Facilities Engineering Service Center, Port Hueneme, California. Peargin, T. 2010. Personal Communication. Sale, T., C. Newell, H. Stroo, R. Hinchee, and P. Johnson, (2008), Frequently Asked Questions Regarding Management of Chlorinated Solvent in Soils and Groundwater, Developed for the Environmental Security Testing and Certification Program (ER-0530). http://www.gsi-net.com/Publications/papers2.asp Shell Global Solutions (US) Inc. (2007). Oxygen Pulse Injection System (OPIS), Design and Installation Guidance Document. November 2007 Update. URS Corporation. (2007) Soil Vapor Extraction and Air Sparge Pilot Test Report, Shell Carson Terminal. October 2007. LA LNAPL Workgroup 36 Pulsed Oxygen Biosparging Pilot Test October 2015 URS/GSI, 2010. Work Plan for Pulsed Oxygen Biosparging (POBS) Pilot Test, LA LNAPL Workgroup. USACE. (2008). In-Situ Air Sparging Engineering and Design Manual, EM1110-1-4005, US Army Corps of Engineers, Washington, D.C. 31 January 2008. Wiedemeier, T.H., Rifai, H.S., Newell, C.J., and Wilson, J.W., 1999. Natural Attenuation of Fuels and Chlorinated Solvents. John Wiley & Sons, New York. LA LNAPL Workgroup 37 Pulsed Oxygen Biosparging Pilot Test October 2015 FIN NAL RE EPORT FOR PU ULSED D OXYG GEN BIO OSPAR RGING (POBS) ( ) PILOT T TEST FIG GURES LA LN NAPL Workgrou up Figures-1 Pulsed Oxygen Biosparging Pilot Te est October 2015 Figure 3.1. Site Location and Layout LA LNAPL Workgroup Figures-2 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 3.2. Site NAPL Distribution LA LNAPL Workgroup Figures-3 Pulsed Oxygen Biosparging Pilot Test October 2015 LA LNAPL Workgroup Figures-4 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 3.3. Pulsed Oxygen Biosparging (POBS) System Pilot Test Focus Area LA LNAPL Workgroup Figures-5 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 3.4 4. Original De esign for Bio osparge Welll Constructio on and CPT T/ROST Charac cterization D Data (A) Double-nested biospa arging well installation in separatte boreholes, and (B) atigraphy and ROST delineation res sults in the vvicinity of the e proposed POBS pilot stra testt, and appro oximate well installation depths with hin the treattment zoness at location PA11 (5 ft well sumps not shown). s Du ue to LNAPL L accumulatio on in deepe er unit wells, bios sparging of the t deeper unit u was not conducted. LA LN NAPL Workgrou up Figures-6 Pulsed Oxygen Biosparging Pilot Te est October 2015 Figure 3.5. Pilot Test Layout with Biosparge and Monitoring Locations Note: Monitoring well and biosparge well locations will be used for pre and post test characterization. Nested biosparge wells (PB-IW) and monitoring wells (PB-MW) will be installed in the treatment zones within the Perched Zone (P) and lower Perched Zone (P2) at the site. LA LNAPL Workgroup Figures-7 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 3.6. Conceptual POBS System Components LA LNAPL Workgroup Figures-8 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 4.1. Final Locations of POBS Injection and Monitoring Wells. LA LNAPL Workgroup Figures-9 Pulsed Oxygen Biosparging Pilot Test October 2015 InjectionVolumePerDay (SCF) Figure 4.2. Daily Injection Well Volumes for Injection Wells IW-1P (top), IW-2P (middle), and IW-3P and IW-3R (bottom) in Units of SCF per day. Injection Well IW-1P 140 120 100 80 60 40 20 Injection Well IW-2P 140 Increase in injection volumes all three wells InjectionVolumePerDay(SCF) 0 120 100 80 60 Daylighting 40 20 InjectionVolumePerDay (SCF) 0 140 Injection Well IW-3P 120 Short Circuiting 100 80 60 Injection Well IW-3R Daylighting 40 20 0 LA LNAPL Workgroup Figures-10 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.1. Output from Downhole Sensor Over Four Days, Showing Injection Signal in Pressure and Conductivity, But Problem with DO and ORP sensors. LA LNAPL Workgroup Figures-11 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.2. Dissolved Oxygen and ORP After Two Months of Operation. Only IW-3P Showed Any Response to the Pulsing. LA LNAPL Workgroup Figures-12 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.3. Dissolved Oxygen Utilization Twelve Hours After Oxygen Pulse In One Injection Well PB-IW-1P ORP 35 DO Pressure Conductivity 5800 ORP (V)/DO (mg/L)/P (ft H2O) 30 Dissolved Oxygen Conductivity (mS/cm) 25 5750 20 15 10 5 0 10:30 -5 5700 13:30 16:30 19:30 22:30 -10 LA LNAPL Workgroup 1:30 4:30 7:30 10:30 5650 Figures-13 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.4. Dissolved Oxygen in Groundwater: All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to February 2013. (Note different Y-Axis scales for Injection vs. Monitoring/Background Wells) LA LNAPL Workgroup Figures-14 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.5. Benzene Concentrations in Groundwater vs. Time in All Wells (in ug/L) Benzene Groundwater Concentration Trends (All Wells) End of Pilot Test 100,000 Benzene Concentration (ug/L) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P 10,000 1,000 100 10 1 ‐2 0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30 Months Since Start of System Operation LA LNAPL Workgroup Figures-15 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.6. BTEX Concentrations in Groundwater vs. Time in All Wells (in ug/L) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P BTEX Groundwater Concentration Trends (All Wells) BTEX Concentration (ug/L) 100,000 End of Pilot Test 10,000 1,000 100 10 1 ‐2 0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30 Months Since Start of System Operation LA LNAPL Workgroup Figures-16 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.7. TPH Concentrations in Groundwater vs. Time in All Wells (in ug/L) TPH (All Fractions) Groundwater Concentration Trends (All Wells) TPH Concentration (mg/L) 100,000 10,000 PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P 1,000 End of Pilot Test 100 10 1 ‐2 0 2 4 6 8 10 12 14 16 18 20 22 24 26 28 30 Months Since Start of System Operation LA LNAPL Workgroup Figures-17 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.8. Benzene in Groundwater: All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to August 2013. LA LNAPL Workgroup Figures-18 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.9. BTEX in Groundwater: All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to August 2013. LA LNAPL Workgroup Figures-19 Pulsed Oxygen Biosparging Pilot Test October 2015 Figure 5.10. TPH (All Fractions) in Groundwater:All Injection (Tan color), Monitoring (Green), and Background (Grey) Wells, June 2012 to August 2013. LA LNAPL Workgroup Figures-20 Pulsed Oxygen Biosparging Pilot Test Geomean TPH-All Fract. Concentrations (ug/L) Geomean BTEX Concentrations (ug/L) Figure 5.11. Summary Statis stics for B Benzene, BTEX X, and TPH-All Fractions F in Groundwater: All Injecttion (Blue color), Monitoring M (Gree en), and Background (Ye ellow) Wells, Ju une 2012 to August A 2013. Geomean Benzene Concentrations (ug/L) October 2 2015 L LA LNAPL Workgro oup Figure es-21 Pulsed Oxyge en Biosparging Pilo ot Test October 2015 Figure 5.12. Soil Analysis Results for Benzene, BTEX, and TPH (all samples). NOTE: Each bar (either before or after) is shown at the actual depth the sample was collected. In most cases there are paired samples very near to one another, but the actual depth of each sample was used to plot on the y-axis of the graph. Soil Benzene Profile (MW‐1‐P) Screen Depth ( bgs) 0.8 23.0 1.50 24.0 1.80 0.82 0 39.6 23.0 23.5 35 44.7 20 30 40 50 60 70 80 90 100 32 100 200 0.470 0.230 400 5,000 10,000 15,000 20,000 39.1 3,900 21.0 10.4 2,500 21.5 23.5 22.0 22,000 41 Depth ( bgs) 1.0 23.0 22.5 39 23.0 23.5 24.0 22.0 10,000 22.5 13,000 23.0 23.5 24.0 0 24.0 1.5 63.5 24.5 7,800 24.5 10 20 30 40 50 60 70 80 90 100 24.5 0 50 100 150 Soil Concentra on (mg/kg) 200 250 300 350 400 450 500 550 0 5,000 10,000 Soil Concentra on (mg/kg) 16.0 20,000 25,000 30,000 20,000 25,000 30,000 Soil TPH Profile (MW‐3‐P) 16.0 6 4,700 5.0 18.0 18.0 15,000 Soil Concentra on (mg/kg) Soil BTEX Profile (MW‐3‐P) Soil Benzene Profile (MW‐3‐P) 0.2 0.220 30,000 Soil TPH Profile (MW‐2‐P) 63.8 1.0 25,000 Soil Concentra on (mg/kg) 21.5 22.5 17.0 1,800 0 500 20.5 21.0 0.8 16.0 17,000 4,400 Soil BTEX Profile (MW‐2‐P) Depth ( bgs) Depth ( bgs) 300 20.5 0 5,500 Soil Concentra on (mg/kg) Soil Benzene Profile (MW‐2‐P) 22.0 14,000 23.0 24.5 0 20.5 21.5 11,000 22.5 24.0 Soil Concentra on (mg/kg) 21.0 22.0 23.5 20 24.5 10 Screen 590 21.5 48 22.5 24.0 24.5 3.3 22.0 23.5 1.2 Post‐Test (mg/kg) 160 21.5 1.50 Pre‐Test (mg/kg) 21.0 1.6 Depth ( bgs) 0.12 22.0 22.5 Soil TPH Profile (MW‐1‐P) 20.5 21.0 0.10 21.5 Depth ( bgs) 20.5 Post‐Test (mg/kg) 21.0 Pre‐Test (mg/kg) Post‐Test (mg/kg) Screen Soil BTEX Profile (MW‐1‐P) Pre‐Test (mg/kg) 20.5 6,900 18.0 19.0 20.0 22.0 23.0 24.0 25.0 8.6 22.0 24.0 0.7 26.0 27.0 28.0 10.0 20.0 30.0 40.0 50.0 60.0 70.0 80.0 90.0 5,000 28.0 0 50 100 150 200 250 300 350 400 450 500 550 0 5,000 Soil Concentra on (mg/kg) Soil Benzene Profile (MW‐4‐P) 10,000 15,000 Soil Concentra on (mg/kg) Soil BTEX Profile (MW‐4‐P) Soil TPH Profile (MW‐4‐P) 16.0 16.0 1.13 0.225 18.0 0.043 20.0 18.0 1.33 20.0 64.0 22.0 60 24.0 312 22.0 461 24.0 46.0 26.0 522 26.0 39.0 28.0 355.0 28.0 10 20 30 40 50 60 Soil Concentra on (mg/kg) LA LNAPL Workgroup 70 80 90 100 1,8001,800 20.0 Depth ( bgs) Depth ( bgs) Depth ( bgs) 24.0 3,100 28.0 100.0 16.0 0 8,500 26.0 36.5 Soil Concentra on (mg/kg) 18.0 3,000 22.0 29 26.0 0.7 0.0 20.0 9 Depth ( bgs) 0.2 21.0 0.2 Depth ( bgs) Depth ( bgs) 20.0 3,000 22.0 29,000 24.0 3,400 26.0 4,800.0 28.0 0 50 100 150 200 250 300 350 Soil Concentra on (mg/kg) Figures-22 400 450 500 550 0 5,000 10,000 15,000 20,000 25,000 30,000 Soil Concentra on (mg/kg) Pulsed Oxygen Biosparging Pilot Test October 2 2015 Figure 5.13. Soil Data D Posted on Triangle e Chart, With h Before-Tesst Concentra ations on X-A Axis and After-Test A Co oncentration on Y-Axis. Results sho ow slight deccreases for m most benzen ne samples, and a large inc creases for m most TPH sa amples. Benzene In n Soil Before an nd After Pilot T Test AFTER TEST Concentration (ug/kg) AFTER TEST Concentration (ug/kg) BTEX In Soil Before an nd After Pilot TTest 100,0000 100,000 10,000 1,000 100 10 10 100 1,000 10,0 000 100,0001,000 0,000 BEFO ORE‐TEST Concentration (ug//kg) 1,000,0 000 1,000,0000 GRO In Soil Before and A After Pilot Test AFTER TEST Concentration (ug/kg) 1,000,000 10,0000 1,0000 1100 10 10 100,0 000 1000 1,000 10,0 000 100,0001,000 0,000 BEFO ORE ‐TEST Con ncentration (ug/kg) 1,000,0000 AFTER TEST Concentration (ug/kg) DRO In SSoil Before and d After Pilot Teest 100,0000 10,0 000 1,0 000 100 1 10 10 100 0 1,000 10,0 000 100,0001,000 0,000 BEFO ORE ‐TEST Conccentration (mgg/kg) 10,0000 1,0000 1100 10 10 1000 1,000 10,0 000 100,0001,000 0,000 BEFO ORE ‐TEST Con ncentration (ugg/kg) TPH In So oil Before and After Pilot Tesst 1,000,0 000 AFTER TEST Concentration (ug/kg) 100,0 000 10,0 000 1,0 000 100 1 10 10 100 0 1,000 10,0 000 100,0001,000 0,000 BEFO ORE ‐TEST Conccentration (ug//kg) LA LNAPL Workgroup Figures-23 Pulsed Oxygen Biosparging Pilot Te est October 2 2015 Figure 5.14. Cone Pen netrometer (CPT) and UV Optic cal Screening Tool T (UVOST) L Logs. (See Figu ure 5 for Locatio ons) MW-5 CPT PA-11 (2 2007) ROST/C CPT IW-1 UVO OST/CPT MW-3 UVOST/CPT U IW-2 UVOST/CPT MW-4 UVOST/CP PT MW-7 CPT T Sc creened Inttervals Key Points: nificant differenc ce between 200 07 ROST and CPT C Log (PA11) vs. 2012 UVOS ST, CPT Data (a all others) Sign No LNAPL accumu ulation noted in wells w screened in upper unit (see screen intervval symbols on each log) Gre eater than 20 fee et LNAPL accum mulation in wells s screened in de eeper unit. L LA LNAPL Workgro oup Figure es-24 Pulsed Oxyge en Biosparging Pilo ot Test October 2 2015 Figure 5.15. Cone C Penetrome eter (CPT) , Beffore and After UV U Optical Scree ening Tool (UVO OST), and Core e Photography ffor Borings MW W-1 and MW-2. (See Figure 5 for f Locations) L LA LNAPL Workgro oup Figure es-25 Pulsed Oxyge en Biosparging Pilo ot Test October 2 2015 Figure 5.16. Cone C Penetrome eter (CPT) , Beffore and After UV U Optical Scree ening Tool (UVO OST), and Core e Photography ffor Borings MW W-3 and MW-4. (See Figure 5 for f Locations) L LA LNAPL Workgro oup Figure es-26 Pulsed Oxyge en Biosparging Pilo ot Test October 2 2015 Figure 5.17. Before B and After Test UV Optica al Screening Tool (UVOST), an nd TPH-All Fractions Data for Boring gs MW-1 and MW-2.. M (See Fig gure 5 for Locattions) L LA LNAPL Workgro oup Figure es-27 Pulsed Oxyge en Biosparging Pilo ot Test October 2 2015 Figure 5.18. Before B and After Test UV Optica al Screening Tool (UVOST), an nd TPH-All Fractions Data for Boring gs MW-3 and MW-4. M (See Figure 5 for Locatio ons) L LA LNAPL Workgro oup Figure es-28 Pulsed Oxyge en Biosparging Pilo ot Test October 2 2015 Fig gure 5.19. Core e Photography and TPH Data L LA LNAPL Workgro oup Figure es-29 Pulsed Oxyge en Biosparging Pilo ot Test October 2 2015 Figure 5.2 20. Core Photo ography and Tw wo Before-and A After-Test LNAP L Saturation Re esults L LA LNAPL Workgro oup Figure es-30 Pulsed Oxyge en Biosparging Pilo ot Test APPEN NDIX 1: PILOT TEST D DATA ssued: Octob ber 2015 Is Prepared P by: The T LA LNAP PL Workgrou up AE ECOM 999 9 Town and Coun ntry Rd., Orange e, CA 92868 tel. 714.567.2430 GS SI Environmental Inc c. 2211 Norfolk, Suite e 1000, Houston, Texas 77098-4 4054 tel. 713.522.6300 Table of Contents 1.0 APPENDIX 1: PILOT TEST DATA 1 1.1 FLUID LEVEL MEASUREMENTS AND APPROXIMATE VOLUME OF FREE PRODUCT IN WELL CASING PRIOR TO WELL DEVELOPMENT DEPTH TO WATER AND LNAPL DATA GROUNDWATER MONITORING RESULTS GROUNDWATER MONITORING RESULTS (DISSOLVED OXYGEN) BEFORE AND AFTER SOIL RESULTS 1 2 3 7 8 1.2 1.3 1.4 1.5 LA LNAPL Workgroup Pulsed Oxygen Biosparging Pilot Test GSI Job No. G-3195-102 Issued: 8 August 2014 Page 1 of 1 FLUID LEVEL MEASUREMENTS AND APPROXIMATE VOLUME OF FREE PRODUCT IN WELL CASING PRIOR TO WELL DEVELOPMENT Biosparge Pilot Test Area, Carson Terminal WELL ID PB-MW-1P PB-MW-2P PB-IW-1P PB-IW-3P PB-MW-1P2 PB-MW-2P2 PB-IW-1P2 PB-IW-3P2 Screen Interval (ft BGS) 21-24 21-24 22-24 22-24 40-43 41-44 42-44 42-44 Depth to Product Depth to Water Depth to Depth to Water (ft BTOC) (ft BTOC) Product (ft BGS) (ft BGS) 17.19 14.2 17.45 14.5 15.25 14.8 15.07 14.6 18.5 40.28 15.5 37.3 18.54 45.61 15.5 42.6 16.08 43.4 15.6 42.9 15.9 42.65 15.4 42.1 BTOC = Below Top of Casing BGS=Below Ground Surface (approximate) Approximate Well Internal Approximate Volume Thickness of Diameter Volume of of Product in Well Product (ft) (inches) casing (gal/ft) Casing (gal) 4 0.653 4 0.653 2 0.163 2 0.163 21.8 4 0.653 14.2 27.1 4 0.653 17.7 27.3 2 0.163 4.5 26.7 2 0.163 4.4 GSI Job No. G-‐3195 Issued: 8 August 2014 Page 1 of 1 Depth to Water and LNAPL Data LA LNAPL Pulsed Biopsarge Pilot Test WELL ID PB-‐IW-‐1P PB-‐IW-‐1P2 PB-‐IW-‐3P PB-‐IW-‐3P2 PB-‐MW-‐1P PB-‐MW-‐1P2 PB-‐MW-‐2P PB-‐MW-‐2P2 DTP (BTOC) ND 16.08 ND 15.9 ND 18.5 ND 18.54 DTW (BTOC) 15.25 43.4 15.07 42.65 17.19 40.28 17.45 45.61 Pre Development DTP (BGS) DTW (BGS) ND 14.8 15.6 42.9 ND 14.6 15.4 42.1 ND 14.2 15.5 37.3 ND 14.5 15.5 42.6 LNAPL Tkns NA 27.3 NA 26.8 NA 21.8 NA 27.1 SCREEN INTERVAL (BGS) 22-‐24 42-‐44 22-‐24 42-‐44 21-‐24 40-‐43 21-‐24 41-‐44 WELL ID PB-‐IW-‐1P PB-‐IW-‐1P2 PB-‐IW-‐3P PB-‐IW-‐3P2 PB-‐MW-‐1P PB-‐MW-‐1P2 PB-‐MW-‐2P PB-‐MW-‐2P2 DTP (BTOC) ND 16.43 ND 16.42 ND 18.26 ND 18.78 9/12/2011 (Post Development) DTW (BTOC) DTP (BGS) DTW (BGS) 15.34 ND 14.8 43.78 15.9 43.3 15.13 ND 14.6 37.5 15.9 37 17.22 ND 14.22 46.36 15.26 43.4 17.58 ND 14.6 32.58 15.8 29.6 LNAPL Tkns NA 27.4 NA 21.1 NA 28.1 NA 13.8 SCREEN INTERVAL (BGS) 22-‐24 42-‐44 22-‐24 42-‐44 21-‐24 40-‐43 21-‐24 41-‐44 10/6/11 DTP (BGS) DTW (BGS) ND 14.9 15.9 45.9 ND 14.6 15.9 40.2 ND 14.3 15.3 43.4 ND 14 .6 15.8 32.4 LNAPL Tkns NA 30.0 NA 24.3 NA 28.1 NA 16.6 SCREEN INTERVAL (BGS) 22-‐24 42-‐44 22-‐24 42-‐44 21-‐24 40-‐43 21-‐24 41-‐44 WELL ID DTP (BTOC) DTW (BTOC) PB-‐IW-‐1P ND 15.35 PB-‐IW-‐1P2 16.43 46.41 PB-‐IW-‐3P ND 15.13 PB-‐IW-‐3P2 16.44 40.74 PB-‐MW-‐1P ND 17.25 PB-‐MW-‐1P2 18.28 46.41 PB-‐MW-‐2P ND 17.56 PB-‐MW-‐2P2 18.78 35.41 DTP= Depth to product DTW=Depth to water ND=Not Detected BGS=Below Ground Surface (approximate) NA=Not Applicable All measurements/thicknesses in feet LNAPL Tkns Incr 9/12/11 to 10/6/11 2.6 3.2 0.0 2.8 GSI Job: G-3195-102 Issued: October 2015 Page 1 of 4 GROUNDWATER MONITORING RESULTS Pulsed Biosparge System LA LNAPL - Shell Carson Terminal Non DATA ‐ Assume: 0.1 ug: Injection wells Monitoring wells inside treatment area Monitoring wells outside treatment area GW Benzene Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 170 220 200 20 61 6 2 2 5 6,300 1,100 2,600 2,400 330 110 260 505 150 470 150 150 110 280 4 580 310 450 705 340 250 320 260 220 460 320 430 330 180 16 110 250 650 190 140 190 240 290 220 170 12,000 510 520 530 600 490 380 380 510 440 810 830 780 970 530 590 560 840 750 14,000 91 15,000 260 GW Toluene Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 190 160 190 20 87 4 2 3 3 1,700 410 745 390 84 29 47 250 29 950 530 280 160 600 150 310 690 250 150 290 180 82 620 460 600 450 200 50 130 340 580 280 210 310 420 440 370 290 3,100 91 53 97 110 160 45 55 79 74 775 790 830 1,100 460 620 580 940 780 2,000 14 40 4,300 290 GW Xylenes Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 340 230 260 130 150 34 30 13 14 1,300 880 705 510 170 52 98 970 200 1,200 600 420 440 550 80 530 340 390 670 280 280 340 350 260 520 390 450 400 200 120 210 400 590 320 240 270 330 320 340 330 2,300 270 140 180 170 230 80 110 140 160 830 670 780 940 410 520 570 840 700 1,600 ‐ 280 4,900 390 GSI Job: G-3195-102 Issued: October 2015 Page 2 of 4 GROUNDWATER MONITORING RESULTS Pulsed Biosparge System LA LNAPL - Shell Carson Terminal Non DATA ‐ Assume: 0.1 ug: Injection wells Monitoring wells inside treatment area Monitoring wells outside treatment area GW Total Diesel Range Organics (DRO) Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 20,000 15,000 13,000 12,000 14,000 16,000 12,000 11,000 13,000 17,000 34,000 18,500 19,000 52,000 22,000 20,000 38,000 41,000 55,000 41,000 28,000 24,000 27,000 19,000 75,000 89,000 34,000 63,500 41,000 27,000 54,000 21,000 11,000 37,000 22,000 21,000 15,000 15,000 8,100 11,000 13,000 28,000 17,000 15,000 13,000 15,000 15,000 20,000 20,000 27,000 38,000 33,000 23,000 24,000 28,000 26,000 24,000 23,000 20,000 10,500 9,700 8,700 8,800 11,000 10,000 12,000 9,400 13,000 33,000 PB‐MW‐5‐P 47,100 43,500 31,300 31,400 37,600 33,600 31,900 32,300 26,700 PB‐MW‐6‐P 23,700 26,400 20,800 20,000 21,900 23,700 23,200 19,500 23,700 PB‐MW‐7‐P 94,000 Operation Time (months) ‐2 1 2 4 6 8.5 11 14 30 PB‐IW‐1‐P 28,400 21,900 19,000 15,020 20,400 22,440 16,500 15,480 17,190 PB‐IW‐2‐P 47,500 58,500 35,000 29,800 69,500 32,800 28,000 85,500 53,800 75,000 PB‐IW‐3‐P 75,300 51,900 35,400 29,300 35,700 24,900 104,000 4,000 22,000 GW Total Petroleum Hydrocarbons (TPH ALL) Concentration (μg/L) Well PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P 88,000 49,100 24,200 87,000 100,200 32,400 21,800 43,100 29,700 19,300 75,750 21,500 21,800 50,500 22,000 23,100 34,100 12,150 29,300 62,700 16,000 27,600 28,600 18,200 96,000 16,200 37,900 30,300 GSI Job: G-3195-102 Issued: October 2015 Page 3 of 4 GROUNDWATER MONITORING RESULTS Pulsed Biosparge System LA LNAPL - Shell Carson Terminal Non DATA ‐ Assume: 0.1 ug: Injection wells Monitoring wells inside treatment area Monitoring wells outside treatment area GW BTEX Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 768 657 699 172 319 49 35 20 26 9,368 2,406 4,083 3,314 592 195 424 1,802 386 2,850 1,352 872 736 889 104 1,880 839 1,260 2,315 963 764 1,046 890 641 1,730 1,226 1,580 1,255 611 191 477 1,063 1,940 822 622 829 1,075 1,149 1,010 862 17,760 971 923 1,037 1,190 1,080 695 755 1,019 834 2,448 2,373 2,489 3,170 1,470 1,818 1,763 2,740 2,308 17,639 439 24,970 942 GW Ethylbenzene Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 68 47 49 2 21 4 1 2 4 68 16 33 14 8 4 19 77 7 230 72 22 26 59 6 170 39 110 250 93 84 96 100 79 130 56 100 75 31 5 27 73 120 32 32 59 85 99 80 72 ‐ 2 360 100 210 230 310 200 190 210 290 160 33 83 99 160 70 88 53 120 78 39 28 770 GW Total Petroleum Hydrocarbons (TPH MOTOR) Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 4,500 3,300 2,900 2,300 4,400 5,700 3,700 3,800 3,500 3,500 9,500 5,000 4,000 14,000 9,100 5,300 9,500 8,700 4,300 4,000 3,400 2,100 3,100 4,700 3,400 4,400 2,800 3,550 3,800 3,800 3,100 2,600 1,800 3,300 2,800 2,500 2,100 3,800 2,000 2,000 3,000 2,900 3,000 2,600 2,900 2,600 3,400 5,400 3,800 10,000 2,700 2,800 2,500 2,700 3,600 3,300 2,600 2,700 2,300 2,850 2,700 2,900 2,400 3,800 3,700 3,300 2,700 3,000 12,000 15,000 11,000 3,600 GSI Job: G-3195-102 Issued: October 2015 Page 4 of 4 GROUNDWATER MONITORING RESULTS Pulsed Biosparge System LA LNAPL - Shell Carson Terminal Non DATA ‐ Assume: 0.1 ug: Injection wells Monitoring wells inside treatment area Monitoring wells outside treatment area GW Total Gasoline Range Organics (GRO) Concentration (μg/L) Well Operation Time (months) PB‐IW‐1‐P PB‐IW‐2‐P PB‐IW‐3‐P PB‐MW‐1‐P PB‐MW‐2‐P PB‐MW‐3‐P PB‐MW‐4‐P PB‐MW‐5‐P PB‐MW‐6‐P PB‐MW‐7‐P ‐2 1 2 4 6 8.5 11 14 30 3,900 3,600 3,100 720 2,000 740 800 680 690 27,000 15,000 11,500 6,800 3,500 1,700 2,700 38,000 4,100 16,000 6,900 4,000 3,200 5,600 1,200 9,600 6,800 6,300 8,700 5,700 3,300 5,600 5,000 3,400 8,800 7,600 6,200 4,400 3,200 2,050 3,000 2,200 7,000 4,200 4,200 3,400 4,200 4,700 3,900 3,800 50,000 6,400 7,700 5,800 4,700 6,000 4,300 5,300 6,600 4,400 10,350 14,000 9,200 8,800 7,100 10,000 7,900 7,400 7,700 49,000 PB‐MW‐5‐P 610 560 480 590 480 490 370 470 210 PB‐MW‐6‐P 5.3 6.7 5.7 7.5 21.0 6.9 4.0 7.4 9.0 PB‐MW‐7‐P 8,100 Operation Time (months) ‐2 1 2 4 6 8.5 11 14 30 PB‐IW‐1‐P 120 170 140 96 110 96 70 61 30 PB‐IW‐2‐P 600 530 725 670 210 43 130 190 110 14,000 PB‐IW‐3‐P 330 330 210 220 100 26 110 PB‐MW‐1‐P 1,100 600 660 1,200 550 320 560 320 110 81,000 4,700 GW DIPE Concentration (μg/L) Well PB‐MW‐2‐P PB‐MW‐3‐P 310 120 360 110 350 95 320 110 210 130 145 98 120 72 210 270 120 PB‐MW‐4‐P 7,500 10,000 GSI Job: G-‐3195-‐102 Issued: 8 August 2014 Page 1 of 1 GROUNDWATER MONITORING RESULTS (DISSOLVED OXYGEN) Pulsed Biosparge System LA LNAPL - Shell Carson Terminal INJECTION WELLS Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 PB-‐IW-‐1-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 DO (mg/L) 0.06 0.45 0.17 1.1 9.98 12.6 15 Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 PB-‐IW-‐2-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 DO (mg/L) 0.20 0.70 0.52 3.59 11.92 0.63 0 Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 PB-‐IW-‐3-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 DO (mg/L) 0.10 0.99 6.86 0.75 0.82 1.57 Injection wells Monitoring wells inside treatment area Monitoring wells outside treatment area MONITORING WELLS Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 PB-‐MW-‐1-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 PB-‐MW-‐4-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 DO (mg/L) Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 DO (mg/L) 0.23 Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 PB-‐MW-‐2-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 PB-‐MW-‐5-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 DO (mg/L) Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 DO (mg/L) Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 PB-‐MW-‐3-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 PB-‐MW-‐6-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 DO (mg/L) DO (mg/L) Date 6-‐Apr-‐12 3-‐Jul-‐12 2-‐Aug-‐12 3-‐Oct-‐12 7-‐Dec-‐12 22-‐Feb-‐13 6-‐May-‐13 2-‐Mar-‐13 2-‐Jun-‐13 PB-‐MW-‐7-‐P (DO) Months of System Operation -‐2 1 2 4 6 9 11 14 17 DO (mg/L) 0.39 GSI Job No. G-‐3195 Issued: 8 August 2014 Page 1 of 1 PRELIMINARY BEFORE AND AFTER SOIL RESULTS Pulsed Biosparge System LA LNAPL -‐ Shell Carson Terminal Summary Statistics Pre-‐Test Post-‐Test % Reduction Pre-‐Test Post-‐Test % Reduction Pre-‐Test Post-‐Test % Reduction Pre-‐Test Post-‐Test % Reduction Average Soil Concentrations (mg/kg): PB-‐MW-‐1 Ben BTEX TPH GRO DRO 1.2 29 5,265 2,501 2,711 8,348 3,461 4,737 0.7 34.8 47% -‐20% -‐59% -‐38% -‐75% Geomean Soil Concentrations (mg/kg): PB-‐MW-‐1 Ben BTEX TPH GRO DRO 0.79 17 2,555 1,139 1,319 0.56 18.6 3,987 1,560 2,334 29% -‐10% -‐56% -‐37% -‐77% Average Soil Concentrations (mg/kg): PB-‐MW-‐3P Ben BTEX TPH GRO DRO 0.4 14 3,600 1,619 1,930 0.4 17 6,800 3,105 3,630 5% -‐19% -‐89% -‐92% -‐88% Geomean Soil Concentrations (mg/kg): PB-‐MW-‐3P Ben BTEX TPH GRO DRO 0.3 11 3,523 1,608 1,767 0.3 12.4 6,644 3,060 3,514 1% -‐13% -‐89% -‐90% -‐99% DIPE 0.39 0.00 100% DIPE 0.028 0.001 96% DIPE 0.001 0.001 0% DIPE 0.00 0.00 0% Pre-‐Test Post-‐Test % Reduction Pre-‐Test Post-‐Test % Reduction Pre-‐Test Post-‐Test % Reduction Pre-‐Test Post-‐Test % Reduction Average Soil Concentrations (mg/kg): PB-‐MW-‐2 Ben BTEX TPH GRO DRO 0.8 40 3,600 1,619 1,930 10,767 5,164 3,630 0.8 46 -‐2% -‐16% -‐199% -‐219% -‐88% Geomean Soil Concentrations (mg/kg): PB-‐MW-‐2 Ben BTEX TPH GRO DRO 0.3 11 3,523 1,608 1,767 0.7 34.8 7,542 3,464 3,974 -‐102% -‐218% -‐114% -‐115% -‐125% Average Soil Concentrations (mg/kg): PB-‐MW-‐4 Ben BTEX TPH GRO DRO 36.7 278 2,733 1,763 853 33.0 272 11,867 7,580 4,124 10% 2% -‐334% -‐330% -‐384% Geomean Soil Concentrations (mg/kg): PB-‐M@-‐4 Ben BTEX TPH GRO DRO 8.7 57 2,638 1,620 838 4.7 60.2 6,304 4,274 1,857 47% -‐6% -‐139% -‐164% -‐122% DIPE 0.00 0.00 0% DIPE 0.00 0.00 0% DIPE 7.667 7.267 5% DIPE 0.51 0.49 5% BEFORE AND AFTER SOIL RESULTS Pulsed Biosparge System LA LNAPL -‐ Shell Carson Terminal GSI Job No. G-‐3195 Issued: 8 August 2014 Page 1 of 1 PRELIMINARY Original Data LOCATION NAME SAMPLE DATE SAMPLE DEPTH Benzene Diisopropyl Ether (DIPE) Ethylbenzene Naphthalene Toluene Xylenes,Total Carbon Chain C6 Carbon Chain C7 Carbon Chain C8 Carbon Chain C9-C10 Carbon Chain C11-C12 Carbon Chain C13-C14 Carbon Chain C15-C16 Carbon Chain C17-C18 Carbon Chain C19-C20 Carbon Chain C21-C22 Carbon Chain C23-C24 Carbon Chain C25-C28 Carbon Chain C29-C32 Carbon Chain C33-C36 Total Petroleum Hydroc.s (C6-C44) TPH as Gasoline (C6-C12) Diesel Range Organics (C13 to C28) TPH as Motor Oil (C29 to 3) LOCATION NAME SAMPLE DATE SAMPLE DEPTH Benzene Diisopropyl Ether (DIPE) Ethylbenzene Naphthalene Toluene Xylenes,Total Carbon Chain C6 Carbon Chain C7 Carbon Chain C8 Carbon Chain C9-C10 Carbon Chain C11-C12 Carbon Chain C13-C14 Carbon Chain C15-C16 Carbon Chain C17-C18 Carbon Chain C19-C20 Carbon Chain C21-C22 Carbon Chain C23-C24 Carbon Chain C25-C28 Carbon Chain C29-C32 Carbon Chain C33-C36 Total Petroleum Hydroc.s (C6-C44) TPH as Gasoline (C6-C12) Diesel Range Organics (C13 to C28) TPH as Motor Oil (C29 to 3) Units ug/kg ug/kg ug/kg ug/kg ug/kg ug/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg Units ug/kg ug/kg ug/kg ug/kg ug/kg ug/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg mg/kg PB-MW-1 10/26/11 21.3 97 < 51 790 760 < 51 650 < 15 < 15 < 15 23 47 51 24 < 15 < 15 < 15 < 15 < 15 < 15 < 15 160 NA NA NA PB-MW-1 10/26/11 22.4 1,500 < 200 12,000 19,000 4,600 30,000 < 75 320 510 2,000 3,000 2,900 1,000 650 290 200 99 < 75 < 75 < 75 11,000 NA NA NA PB-MW-1 10/26/11 23.2 1,500 620 7,500 14,000 5,700 20,000 < 25 66 110 680 1,500 1,200 740 410 290 220 140 87 66 27 5,500 NA NA NA PB-MW-1 10/26/11 24.2 1,800 930 8,500 6,300 6,700 15,000 < 25 29 80 440 1,200 1,000 610 340 240 180 100 71 59 28 4,400 NA NA NA PB-MW-2 10/26/11 21 < 940 < 940 8,700 19,000 9,900 20,000 < 25 31 72 570 1,200 1,200 430 270 77 67 < 25 < 25 < 25 < 25 3,900 NA NA NA PB-MW-2 10/26/11 22.1 1,000 < 430 8,000 20,000 8,900 23,000 < 100 170 330 1,700 3,100 2,800 990 650 280 190 < 100 < 100 < 100 < 100 10,000 NA NA NA PB-MW-2 10/26/11 22.9 1,000 < 410 7,000 19,000 8,900 22,000 < 120 260 410 2,200 3,600 3,500 1,200 810 370 230 < 120 < 120 < 120 < 120 13,000 NA NA NA PB-MW-2 10/26/11 23.6 NA NA NA NA NA NA < 100 170 300 1,600 2,800 2,600 920 620 310 210 100 < 100 < 100 < 100 9,600 NA NA NA PB-MW-3P 7/11/12 16.7 < 440 < 440 640 12,000 700 3,400 < 25 < 25 < 25 280 1,200 1,500 620 550 140 130 92 92 29 < 25 4,700 NA NA NA PB-MW-3P 7/11/12 20.4 < 420 < 420 2,000 < 4200 1,700 5,300 < 25 < 25 44 350 1,100 620 300 220 140 74 43 39 43 < 25 3,000 NA NA NA PB-MW-3P 7/11/12 25.3 730 < 430 5,800 13,000 6,100 16,000 < 25 < 25 82 500 1,300 630 270 170 88 41 30 < 25 < 25 < 25 3,100 NA NA NA PB-MW-4P 7/11/12 17.9 < 450 < 450 < 450 < 4500 < 450 < 900 < 25 < 25 10 220 700 560 200 77 31 18 < 25 < 25 < 25 < 25 1,800 NA NA NA PB-MW-4P 7/11/12 22.5 64,000 12,000 29,000 30,000 59,000 160,000 < 25 < 25 150 500 1,100 510 340 170 < 25 < 25 < 25 < 25 < 25 < 25 3,000 NA NA NA PB-MW-1 10/10/13 21.3 120 < 39 1,100 1,800 120 2,000 < 5.0 < 5.0 9 45 180 190 81 42 22 11 7 < 5.0 < 5.0 < 5.0 590 NA NA NA PB-MW-1 10/10/13 22.5 840 < 410 9,500 22,000 4,300 25,000 < 100 190 310 1,600 4,000 3,600 1,600 1,000 480 330 160 100 < 100 < 100 14,000 NA NA NA PB-MW-1 10/10/13 23.2 1,200 < 480 8,900 20,000 7,600 27,000 < 100 210 500 2,000 4,200 4,500 2,200 1,600 830 550 290 220 150 < 100 17,000 NA NA NA PB-MW-1 10/10/13 24.2 820 < 400 4,700 12,000 2,900 12,000 < 50 < 50 < 50 140 460 490 270 200 110 67 < 50 < 50 < 50 < 50 1,800 NA NA NA PB-MW-2 10/10/13 21 < 460 < 460 1,100 4,700 1,100 8,000 < 50 < 50 < 50 260 810 760 330 190 65 < 50 < 50 < 50 < 50 < 50 2,500 NA NA NA PB-MW-2 10/10/13 21.9 800 < 420 13,000 35,000 10,000 40,000 < 250 270 970 2,700 6,900 6,000 2,600 1,600 730 350 < 250 < 250 < 250 < 250 22,000 NA NA NA PB-MW-2 10/10/13 24.2 1,500 < 520 11,000 26,000 12,000 39,000 < 50 83 200 900 2,400 2,200 940 570 230 140 57 < 50 < 50 < 50 7,800 NA NA NA PB-MW-3 10/10/13 18.2 < 430 < 430 1,800 11,000 < 430 3,800 < 50 < 50 110 630 2,300 2,100 860 500 160 97 < 50 < 50 < 50 < 50 6,900 NA NA NA PB-MW-3 10/10/13 20.4 < 470 < 470 1,800 6,000 900 5,700 < 50 < 50 110 870 2,800 2,600 1,100 610 220 96 53 < 50 < 50 < 50 8,500 NA NA NA PB-MW-3 10/10/13 25.3 650 < 250 7,100 19,000 5,700 23,000 < 50 54 140 700 1,600 1,400 580 330 130 54 < 50 < 50 < 50 < 50 5,000 NA NA NA PB-MW-4 10/10/13 17.9 < 86 < 86 370 5,000 130 790 < 50 < 50 < 50 220 920 390 170 71 < 50 < 50 < 50 < 50 < 50 < 50 1,800 NA NA NA PB-MW-4 10/10/13 22.5 60,000 13,000 48,000 55,000 73,000 280,000 840 1,200 2,600 5,900 7,200 6,000 2,500 1,600 700 < 500 < 500 < 500 < 500 < 500 29,000 NA NA NA PB-MW-4 10/10/13 25.7 39,000 8,800 35,000 32,000 61,000 220,000 220 350 690 1,500 1,100 520 250 92 78 < 50 < 50 < 50 < 50 < 50 4,800 NA NA NA PB-MW-4P 7/11/12 25.7 46,000 11,000 51,000 < 46000 95,000 330,000 < 25 100 410 1,100 1,000 310 140 110 60 32 < 25 < 25 < 25 < 25 3,400 NA NA NA
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