Loss Prevention Bulletin 235 February 2014 | 5 Incident Rapid carbon steel corrosion and HF acid leak Dave Bridger Summary In 2005, the carbon steel piping of an acid relief neutraliser (ARN) on an HF alkylation plant on a refinery rapidly corroded (within one hour), releasing a solution of NaF, FeF2 and HF acid. The ARN, which was connected to the refinery flare system, was only designed for coping with neutralising HF vapours, not liquid HF. The incident resulted in the release of approximately 1.1 tonnes of liquid anhydrous HF (AHF) to the ARN during the HF tanker offloading process. The investigation identified the cause of the incident being the piping downstream of the liquid HF discharge line connected to the offloading HF delivery tanker. The intended purpose of this piping (as per procedure) was to enable final residual HF vapours to be vented to the ARN at the conclusion of the HF tanker offloading process. This procedure to vent the residual HF vapours at the end of the HF tanker offloading had been successfully used previously, without incident, for decades. However, on this occasion the delivery tanker was not quite empty and as such caused discharge of HF liquid to the ARN. Fortunately, the ARN liquid seal was maintained (using make-up water) during the incident and as such no loss of containment of refinery flare gases occurred. The HF acid strength was maintained below 5% using a large amount of water feed. The incident caused a significant amount of liquid HF to attack the carbon steel pipework. No noticeable pH drop was recorded at the refinery interceptors in spite of fluoride levels peaking at 200 ppm in wastewater. There were a number of lessons learned from the incident but the most significant finding was that the piping pathway, as recommended in API RP751, allowed a significant discharge of liquid HF to occur during the HF tanker offloading operation2. API RP751 stipulates, “There should be a connection from the unloading line to the acid scrubber (ARN) for venting after unloading”. API RP751 also stipulates that the aforementioned connection can also be used for “emergency depressurisation” purposes. In such an event, it is foreseeable for liquid HF to be routed via the ARN. The ARN, however, is not designed to cope with liquid HF discharge from the HF tanker during the offloading operation. It is therefore of paramount importance that all procedures (and hardware) are thoroughly checked to ensure that liquid HF cannot be routed via the ARN, even during emergencies, unless the ARN is suitably designed to receive the liquid HF load. A simple three-way plug valve is recommended for the © Institution of Chemical Engineers 0260-9576/14/$17.63 + 0.00 purpose of making suitable adjustment to the system. This valve can be retrofitted to the HF tanker offloading systems. This should enable safe depressurisation (either routine or emergency) of the system to the flare via ARN through an EDV. Keywords: Acid relief neutraliser, HF, corrosion, API RP751 Background HF acid was delivered to the refinery in an ISO container tanker holding 16 tonnes of liquid HF. It was offloaded into a 45 m3 capacity onsite storage vessel using a nitrogen assisted blow-egg via a “dip pipe” located inside the HF tanker. This is often referred to as “the unloading line”. By design, the liquid HF must enter the storage vessel’s vapour space (as shown in Figure 1). This arrangement ensures that no liquid HF can ever backflow to the tanker and thus cause it to overload. The procedures concerning the offloading of HF acid tankers were reviewed previously1. The level measurement instrumentation on the HF storage vessel had been problematic for years. There had been frequent failures and loss of confidence in the instrumentation, and as such, it was no longer used. This status became an accepted norm by the operators and instead they simply relied on the operation of try-cocks only. Even so, the most recent revision of the offloading procedures still referred to monitoring via the use of the level instrument. As such an alternative fall-back procedure for offloading HF in an emergency was not available. The atmospheric try-cocks had therefore been used to estimate whether there was sufficient ullage in the vessel to receive HF acid (with sufficient coarse accuracy). Try-cocks have recently being phased out as unacceptable practice by the HSE and are considered inadequate in measuring tonnes of HF acid transferred from the tanker. Furthermore, there was no weighbridge to weigh HF at the tanker offloading gantry. This was largely due to cost, because HF offloading only took place between six to nine times per year. The relevant sections of the plant associated with this incident are shown in Figure 1. The entire acid relief neutraliser (ARN) was built from Monel to minimise corrosion attack from HF acid. For information, the lower sections of the ARN are not expected to experience low pH conditions. As such some lower sections of some ARNs are constructed using carbon steel. The circulating caustic (neutralising) system associated with ARN is always invariably made of carbon steel piping. 6 | Loss Prevention Bulletin 235 February 2014 Figure 1: HF acid unloading arrangements and the incident leak point at the ARN In the early years, operators would monitor the completion of the HF offloading procedure by observing the excessive vibrating movement of the flexible hose connected to the HF tanker. Even to this day, some HF suppliers still follow such practice. In the early 1990s, to combat flexible hose failures, the refinery adopted the use of flexible hard piping spirals (no obvious movement under two-phase flow conditions) for gantry connection. The experienced operators then changed from observing vibrating hose movement to listening for the check valve chattering (see F in Figure 1) indicating the endpoint of HF offloading. This was not explicit in any operational offloading procedures. The offloading procedure recommended using nitrogen to its maximum available pressure of 4 to 5 barg to minimise tanker-offloading time. This practice typically allowed offloading to be completed within 1½ hours. When the HF tanker was considered empty, the procedure was to vent and depressurise the tanker to the flare via the ARN. This was to remove residual vapours from the tanker before it returned to its supplier. The aforementioned procedure simply required valve E to the storage to be fully closed and valve D to the ARN fully opened for about five minutes. Typically, 5% wt sodium hydroxide (NaOH) solution is the maximum strength required to prevent sodium fluoride (NaF) crystallisation and fouling of the flare system. The ARN had approximately six tonnes of 5% caustic, capable of neutralising approximately 150 kg of HF vapour. The strength of the caustic was routinely monitored and altered as required. The top temperature of the ARN was also monitored and this was linked to a high process alarm. HF upon neutralisation with caustic releases heat as does HF dilution in water. Thus, an increase in temperature of the ARN indicates HF acidic gas flow. As an aside, the refinery HF alkylation is never allowed to operate without there being ARN in service. The incident This was the first time that the operator involved had offloaded an HF tanker unaccompanied. Therefore he vigilantly followed the procedure to ensure nothing would go wrong. Nonetheless, although the procedure advised that the “ideal offloading pressure (of N2 in the tanker) needed to be 4 to 5 barg”, the operator decided to be more cautious (i.e. more safe for his first time use) and use the nitrogen at a lower pressure setting. The level indication on the acid storage vessel was (as usual) not operational at the time of the HF offloading. The operator was aware that this was quite normal and he disregarded its need to monitor the transfer (according to the procedure). Unfortunately, he did not have (from his peer training) the information related to the noisy flapper in check valve F as the alternative indication of an empty HF tanker. The transfer of HF acid to on-site storage therefore proceeded without incident (albeit, very slowly). The inexperienced gantry operator was in radio contact with the main control room. After almost two hours of offloading time and close to the end of his shift, it was questioned whether the tanker was empty or not. Given the unusually long duration of the offloading activity, he was advised that “the tanker must be empty” (without any secondary confirmations required © Institution of Chemical Engineers 0260-9576/14/$17.63 + 0.00 Loss Prevention Bulletin 235 from observing the noisy flapper valve). Given that it was not normal to leave the HF tanker offloading part way through any shift changeover and with daylight rapidly diminishing, it was agreed to vent the tanker via the ARN as per normal procedure. It is understood that a large number of other issues occurred during the day prior to that final decision to depressure the tanker, resulting in a warmer than normal ARN. In fact, the high alarm at 35oC was already active (though this was not considered an issue, given the alarm was sometimes active on hot summer days). A quick pH test showed the circulating caustic was still alkaline and as such it was acceptable to vent the HF tanker. As the night shift settled in to make their pre-plant checks, they quickly realised that the ARN temperature was very high (84oC), with inflexion having occurred from 43oC. It was later determined that the 41oC increase in temperature was consistent with the heat given off from dilution of 1.1 tonnes HF with 6.6 tonnes of water (the 1.1 tonnes was calculated from level change within the ARN during the incident). Furthermore, operators in the work’s yard were reporting odour of HF in the air (odour threshold of HF at 0.04 to 0.13 ppm). The onsite HF detectors did not activate at that time because the high alarms at TLV TWA were set to function at 3 ppm. It was later learnt that some detectors did reach 10ppm level for a few minutes some hours later. When the operators finally detected liquids flowing out of holes in the piping (see Figure 1), and observing a declining level in the ARN sump, they quickly realised that there could be a release of refinery flare gases. Hence, the water make-up to the ARN was fully opened while operators donned PPE to enable entry to site and isolation of the ARN caustic circulation valves. The amount of carbon steel of the caustic circulation system was about half that required to consume all 1.1 tonnes HF. Figure 2: Storage pressure inflexion indicating HF tanker is empty © Institution of Chemical Engineers 0260-9576/14/$17.63 + 0.00 February 2014 | 7 Nonetheless, a significant amount of hydrogen gas was generated (indicated by the loss of capacity by the refinery flare gas recovery compressor). While the theoretical HF strength could have been as high as 14%, reaction with plant steel and dilution with water, etc, likely resulted in the effluent to drains being less than 5%wt HF acid. There was ultimately massive dilution within the refinery waste water systems. This was confirmed by an undetectable decrease of wastewater pH at the refinery interceptors, in spite of fluorides peaking at 200 ppm. Investigation outcome Details of the actual incident investigation were extensive, albeit at times contradictory. It became apparent that the procedure for offloading an HF tanker was flawed even if it was followed cautiously by an inexperienced operator. The absence of level indication on the HF storage vessel should have been of sufficient enough concern to stop using the procedure and request an updated version. Another HF tanker was unloaded using full available nitrogen pressure (limited by design typically to 5 barg1). The profile of that offloading is attached as Figure 2. The information from the offloading was used to update the unloading procedure. It took approximately one hour for breakthrough of nitrogen to on-site storage (as shown by the “inflexion” of pressure), indicating that it was possible to unload a tanker with the working instruction modified accordingly (with emphasis on maintaining full 4 to 5 barg nitrogen pressure inside the tanker at all times). The pressure trend was monitored by the control room. The pressure inflexion is explained by an increased volumetric flow, for a given pressure drop, down the same pipeline of liquid HF vs vapour HF+N2 mix. Furthermore, the information about listening for the noisy flapper was also included. However, 8 | Loss Prevention Bulletin 235 February 2014 the most important issue concerning the procedure was a statement related to the certainty of the tanker being empty, and not to depressurise the ARN if uncertain. The updated procedure was issued to enable tanker unloading to continue until the facility could be modified. The ultimate latent failure was the existence of a rogue pathway for liquid HF to be sent directly to the ARN. The preferred fix to prevent recurrence of this, or associated incidents, is to eliminate any liquid HF pathway to occur via the ARN. As such the Emergency Depressure Valve (EDV) (shown in Figure 1) was developed as a project to achieve this objective. Most importantly, this investigation appears to indicate that the existing facility was considered acceptable in accordance with API RP7512. This permits “a connection to be made from the offloading line to the acid scrubber (ARN)” recommending its use for “venting HF vapours after unloading”. However, of more serious concern is the additional statement in API RP751 that the line can also be used for “emergency depressuring”. On the contrary, this incident clearly establishes that “emergency depressuring” of HF tanker is considered potentially unsafe if it still holds liquid HF. This is unless the ARN is suitably designed to cope with taking liquid HF to the calculated maximum in the event of emergency depressurisation. There was no evidence of ARN and its associated HF offloading arrangements, including how the system was set up to cope with accepting liquid HF from the HF tanker in an emergency venting scenario, ever being suitably HAZOPed. Such a HAZOP would likely have highlighted the inadequacy of the emergency depressurising arrangements for the HF offloading line. Conclusion The ultimate learning from this incident is to routinely check all procedures (and associated hardware) for potential errors. Many of the procedures were used, over many years, if not decades, without incident (therefore inferred as 100% “proven”). However, as this incident shows, they may contain latent faults (in association with hardware issues). Figure 1 is a very simplified process flow schematic of an otherwise myriad of pipes within the plant. It is essential to trace the process engineering flow schemes on-site to be absolutely certain that HF liquid cannot be sent to the ARN, unless it is suitably designed to receive it. In the interim period, prior to plant modification, the same procedure was able to be updated using the physical science of trending on-site storage pressure in the event of uncertain level measurement (via the storage pressure inflexion). Nonetheless, positive isolation of valve D, offering access to the rogue route is considered essential. A simple threeway plug valve fix (see Figure 1) is presented for retrofitting HF tanker unloading systems to enable safe routine and emergency depressuring (EDV) to flare via the ARN to take place. This can be considered for retrofitting at any other site. Positive isolation with spectacle blind (spade) at the refinery in question was considered necessary (ie instead of piping disconnection), since that piping path was used routinely for shutdown decontamination of the plant, etc. API RP751 This incident raises the question of whether Appendix G in API RP7512 should be suitably modified to prevent liquid HF inadvertently being routed via the ARN, including emergency depressurisation situations during HF tanker offloadings: Appendix G —Design Features of an Acid–Truck Unloading Station, states “There should be a connection from the unloading line to the acid scrubber for venting after unloading and for emergency depressuring”. The event described in this article would suggest that some modification of the above statement is needed to safeguard against a situation where, for whatever reason, liquid HF finds its way via the unloading line into the ARN. In this accident, liquid HF found its way into the ARN, via the HF unloading line, because the means of knowing that the HF tanker was empty were not sufficiently robust. The amount of HF discharged was limited to 1.1 tonnes only. However, if valve ‘D’ (Figure 1) was fully opened with full N2 pressure inside a partially unloaded tanker, then there was a potential to discharge a much greater quantity (10 tonnes or more) of liquid HF via the ARN. Emergency depressurisation of the tanker via the unloading line to the ARN could clearly also result in an unplanned discharge of liquid HF. It is thus proposed that API RP751 be appropriately revised to ensure that the ARN system is suitably designed to cope with liquid HF (as well as its disposal) including any emergency depressurisation scenario. The application of the above should also be subject to a HAZOP study. References 1. Loss Prevention Bulletin, Anatomy of HF acid tanker unloading, Issue 232, August 2013. 2. American Petroleum Institute Recommended Practice, API RP751, for “Safe Operation of Hydrofluoric Acid Alkylation Units”, third edition, June 2007. © Institution of Chemical Engineers 0260-9576/14/$17.63 + 0.00
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