HQ coils: History & Performance F. Borgnolutti November 14th 2012 2nd HiLumi Collaboration Meeting Frascati Outline • HQ Coil Design • Main issues met during HQ coils fabrication • HQ Coil production summary (coil 1 to coil 20) • Tests results • Next generation of HQ coils (starting from coil 21) • Summary 11/14/2012 HQ Coils: History & Performance 2 HQ Coil Design Coil main parameters: • 120 mm aperture diameter • 1 m long • 20 turns in L1 / 25 turns in L2 • 87 m of cable/coil • Cable: o o o o o 35 strands Width = 14.75 mm Mid-thickness = 1.375 mm Keystone angle = 0.75 º Insulation thickness = 100 um Magnet Expected Performance: • Short Sample gradient of 214 T/m @ 1.9 K • “ “ 195 T/m @ 4.4 K • Nominal Ramp rate 20 A/s H. Felice et al., “Design of HQ – A High Field Large Bore Nb3Sn Quadrupole Magnet for LARP”, IEEE trans. On Applied Supercond. VOL. 19, NO. 3, JUNE 2009 11/14/2012 HQ Coils: History & Performance 3 Status of the HQ coil production • From May 2009, 20 HQ Coils have been fabricated • 5 tests involving 9 coils (coil 1 to coil 9) have been performed in a quadrupole structure at 4.4 K (HQ01a-b-c-d-e ) o HQ01e has been tested a second time (HQ01e-2) at CERN at both 4.4 K and 1.9 K. Horizontal “side shims” are placed here • 3 tests involving 3 coils (coil 12, 13 and 15) have been performed at 4.4 K in the mirror structure (individual coil test, HQM01-02-04) 11/14/2012 HQ Coils: History & Performance G-10 and Kapton midplane shims Long High-Field Quad 120 mm bore – Length T Side “ear” Stainless Skin Iron Mirror Block Iron Yoke 4 Main issues met during the coils fabrication Coil expansion/contraction Coil 3 in the reaction fixture, after reaction Broken strands in coil 10 (post reaction) Sign of high radial compression Corrective13 actions COIL • Implementation of an axial gap (0.76 mm for coil 3 to 13, 3.2 mm from coil 14) • Reduction of the strand diameter from 0.8 mm to 0.778 mm (Starting coil 14) • Cable reduced by: 3.8 % azimuthally 2.6 % radially Some concern The coils still spring out from the reaction fixture (~2mm, half of what before making room for cable expansion) • Coil springing out of the reaction fixture Is the room left for expansion suitable? Coil 20 The pole gap in coil 17 stayed open Effect of the braided insulation? Problem during winding (winding tension)? 11/14/2012 HQ Coils: History & Performance 5 Main issues met during the coils fabrication Pole gap in the coils before and after reaction 0.14 IL and OL Pole Gap [inch] 0.12 0.1 L1 Gap after curing L2 Gap after curing 0.08 GAP L1 after reaction GAP L2 After reaction 0.06 0.04 0.02 0 13 14 15 16 17 18 19 20 21 Coil # The pole gap seems optimum since it is at the limit of closing totally after reaction 11/14/2012 HQ Coils: History & Performance 6 Main issues met during the coils fabrication Weak electrical insulation between the coil and the coil parts (saddles, spacer,…) • • Recurrent insulation issues between the coil and the parts within the coil Weak insulation between the coil and the trace (arcing between the trace and the coil) Corrective actions • Decrease coil compaction and increase insulation thickness under the trace • Starting coil 17: Coating of the coil splice block and saddles parts ( 5 mils coating thickness) • From coil 21: All the parts are fully coated with 10 mils ALO3 coating (10 mils coating thickness, voltage breakdown > 1 kV) Some concern • • The tolerance we ask for the flat surface of the pole pieces is 9 mils ±1 mil (0.23 mm ± 0.024 mm), but the tolerance for the pole piece of coil 21 was found between 6 and 9 mils (0.15 - 0.23 mm) what is acceptable for the field quality? What happen when the coil is energized and pulls on the coating (debonding?)? Coil 20 could give an answer.. 11/14/2012 HQ Coils: History & Performance 7 Main issues met during the coils fabrication Cable mechanically unstable (new issue?) • Popped strands may cause strand and insulation damages: o For instance, coil 18 had a lot of inter-turn shorts because of popped strands Strands popping out when winding the L2 (unfavorable winding direction) • It seems that only the second generation of cable was affected (starting coil 14): o Smaller strand diameter (from 0.8 mm to 0.778 mm) o Introduction of a core (8 mm*25 um) o 2 pass cable (cable fabrication, annealing, re-rolling) to 1 pass cable (strand annealing, cable fabrication) Which of these modification contributes to make the cable mechanically less stable? Maybe a combination of the three… 11/14/2012 HQ Coils: History & Performance 8 HQ Coil production summary Coil Number 1 2 3 RRP 54/61 4 5 6 7 8 RRP 108/127 9 10 RRP 54/61 11 108/127 (Ti) 1 turn less in L1 & L2 to provide room for cable expansion 12 13 15 19 20 108/27 (Ti) (cable width = 14.75, cable mid-thickness = 1.375 mm, keystone = 0.75º Cable with stainless steel core (8 mm*25 um) L1-RE key fully Original ends design Revised end design coated (10 mil) Wire annealed (185ºC) cable fabrication Cable fabrication annealing (200ºC) re-rolling (2 pass cable) All the parts (end saddles, poles pieces, spacers) are left uncoated 11/14/2012 18 3.2-3.3 mm axial pole gap Cable without a core H. Felice et al., “Impact of coil compaction on Nb3Sn LARP HQ Magnet”, IEEE trans. On Applied Supercond. VOL. 22, NO. 3, JUNE 2012 17 108/127 (Ta) 0.778 mm diameter strand 0.76 mm axial pole gap Tested in HQ01 16 RRP 54/61 RRP 108/127 (Ta doped) 0.8 mm diameter strand (cable width = 15.15 mm , cable mid-thickness = 1.437mm) No axial pole gap 14 Not tested Broken strands Turn to turn short Tested in Not mirror tested Structure Good but not used HQ Coils: History & Performance Weak electrical insulation (1 pass cable) Will be tested in HQ02 Gap did not close End saddles are coated with ALO3Wrong twist applied to L2 Will not be used matrimid Cyanateester 9 Magnet test results Limiting coil is underlined HQ01 HQM • • RRP 54/61 RRP 108/127 Coil Number Tested at Max gradient @ 4.4 K [T/m] % Iss a 1-2-3-4 LBNL 157 79 Coil 2 damaged (arcing) b 1-4-5-6 LBNL 153 77 First quench, then c 1-5-7-8 LBNL 138 70 No training, Intrinsic damage in coil 1 d 5-7-8-9 LBNL 170 86 (4.5 K) e 5-7-8-9 LBNL 170 86 (4.5 K) e-2 5-7-8-9 CERN 184 (2.2 K) 85 (4.5 and 1.9 K) 01 12 FNAL 82 (4.6 K) 77 (2.2 K) Increased azimuthal space made for coil azimuthal expansion (5.4% / 4.6%) 02 13 FNAL 91 (4.6 K) 89 (2.2 K) The coil has one turn less in each layer Azimuthal space (7.6% / 6.3%) 04 15 FNAL 98 (4.6 K) 94 (2.2 K) Reduced coil compaction (new strand) Azimuthal space (6.8%/6.8%) Comment Pre-load increased wrt HQ01-d Tested at Cern S. Caspi et al., “Test results of 15 T Nb3Sn quad. Magnet HQ01 with 120 mm bore for the LHC lumi. upgrade”, IEEE trans. On Applied Supercond. VOL. 22, NO. 3, JUNE 2012 M. Marchevsky et al., “Quench performance of HQ01, a 120 mm bore Larp quad. For the LHC upgrade”, IEEE trans. On Applied Supercond. VOL. 22, NO. 3, JUNE 2012 R. Bossert et al., “Optimization and test of 120 mm LARP Nb3Sn quad. Coils using magnetic mirror structure”, IEEE trans. On Applied Supercond. VOL. 22, NO. 3, JUNE 2012 G. Chlachidze et al., “Test of optimized 120mm Larp Nb3Sn quad. Coil using magnetic mirror structure”, IEEE trans. On Applied Supercond. VOL. 22, NO. 3, JUNE 2012 11/14/2012 HQ Coils: History & Performance 10 Next generation of HQ coils 6 7 RRP 108/127 8 9 10 11 12 13 14 15 16 17 18 19 20 21 22 23 24 RRP RRP 108/127 (Ta 108/127 Ti (Ta) 54/61 doped) (Ta) ? ? ? ? RRP 54/61 Ti 0.8 mm diameter strand No axial pole gap 0.778 mm diameter strand 0.76 mm axial pole gap 3.2-3.3 mm axial pole gap Cable without a core Cable with stainless steel core Original ends design Revised end design Cable fabrication annealing (200ºC) rerolling (2 pass cable) All the parts (end saddles, poles pieces, spacers, are left uncoated HQ01 25 26 ? ? 5 ? 4 Delivery July 2013 RRP 54/61 3 Delivery mid-March 2013 2 Delivery January 2013 1 Delivery may 2013 Coil Number Wire annealed (185ºC) cable fabrication (1 pass cable) End saddles are All the parts are fully coated coated with AlO3 (10 mils / 254 um) HQ02 HQ03 Goal: to have a consistent set of coils for HQ03 and to have LHQ coils consistent with HQ03 coils 11/14/2012 HQ Coils: History & Performance 11 Summary • The pole gap in the coils allowing longitudinal contraction seems optimized (~3.2 mm) o The issue of coil 17 (pole gap which did not close) seems to be related to a mistake made during winding • Next generation of HQ coils (starting from coil 21) will implement most of the features of HQ02 coils. In additon they will have: o All the part fully coated with 10 mils of ALO3 coating o The coil will be made in a consistent way (the goal is to have all the coils identical) o We are putting effort in order to get fabrication constitency between HQ and LHQ coils • We are constantly trying to improve the coil fabrication process: o Constant evolution of the coil fabrication travelers (tight collaboration between BNL, LBL and FNAL) o Upgrading and improving the winding tooling (thigh collaboration with FNAL) •Are the radial and azimuthal room left for expansion suitable? • There are still unanswered question regarding the coating of the coil parts: o Acceptable tolerance for the coating thickness to ensure good field quality? o Unkown regarding the coating to coil interface. • Cable mechanically unstable: o Second generation cable is less mechanically stable – several possible causes, need to understand also also in support of QXF cable 11/14/2012 HQ Coils: History & Performance 12 Back Up Slide 1 Coil 17 : a mistake made during winding? Overall length layer 2 before/after Curing (from RE end saddle to LE splice block) Overall length coil layer 1 before/after curing (from RE end saddle to LE splice block) 46.9 46.9 Before L1 curing 46.8 After L2 Curing After L1 Curing 46.7 length [inch] length [inch] 46.8 Before L2 curing 46.6 46.5 46.7 46.6 46.5 46.4 46.4 46.3 46.3 46.2 15 16 17 18 19 20 21 46.2 15 coil number 11/14/2012 16 17 18 19 20 21 coil number HQ Coils: History & Performance 13 Back up slides: Presentation made by H. Felice at the 1st HiLumi collaboration meeting HQ01 series Overview Coils Test HQ01a HQ01b HQ01c HQ01d HQ01e 1-2-3-4 April 2010 1- 4 -5-6 June 2010 1 -5-7-8 Oct. 2010 5-7-8-9 April 2011 5-7-8-9 July 2011 180 170 160 9 coils (54/61 or 108/127 RRP) 5 tests at 4.4 K at LBNL Gradient (T/m) 150 HQ01a – 157 T/m – 79 % Iss – unusual ramp-rate HQ01b – 153 T/m – 77 % Iss – electrical failure HQ01c – 138 T/m – 70 % Iss – unusual ramp-rate HQ01d – 170 T/m – 86 % Iss - mechanical limit HQ01e – 170 T/m – 86 % Iss 140 130 120 HQ01a HQ01b HQ01c - regular training HQ01c - 30 to 50 A/s or profile HQ01d HQ01e 110 100 90 80 0 2 4 11/16/2011 6 8 10 12 14 16 18 Quench # 20 22 24 26 28 30 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 15 Overview of HQ01 coil fabrication 11/16/2011 Coil Strand Cable Core Magnet Note 1 54/61 992R No HQ01 a-b-c (LBL) Limiting coil 2 54/61 992R No HQ01 a (LBL) Electrical failure 3 108/127 991R No HQ01 a (LBL) Limiting coil 4 108/127 1000R No HQ01 a-b (LBL) 5 108/127 1000R No HQ01 b-c-d-e (LBL) 6 108/127 1000R No HQ01 b 7 108/127 1000R No HQ01 c-d-e (LBL) 8 54/61 996R No HQ01 c-d-e (LBL) 9 54/61 996R No HQ01 d-e 10 54/61 996R No Not impregnated 11 108/127 (Ti) 1010R No Not tested 12 54/61 1012 SS - 25 mm HQM01 FNAL Special coil 13 54/61 1008 No HQM02 FNAL Special coil H. Felice - 1st HiLumi/ LARP Collaboration Meeting (LBL) Electrical failure (LBL) Broken strands 16 HQ01b Electrical breakdown possible causes • Extensive mechanical analysis performed ruled out the participation of the support structure • Autopsy of coil #6 revealed origin of the short in the interlayer pointed out end design weakness both Lead end and Return end Lead end View of the return end • Review of the coil fabrication process: high compaction • Combination of these effects => electrical failure in HQ01b 11/16/2011 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 17 High compaction: a common symptom of HQ01 coils • 9 coils tested in HQ01 : same observations during fabrication very high compaction after reaction tendency to spring out of the reaction fixture (unlike TQ/LQ) Coil 3 • Broken strands in coil 10 observed post-reaction • Some corrective actions taken to reduce the compaction reduction of the radial build-up of material in the cavity Coil 7 Coil 10 11/16/2011 • Coil / cavity size mismatch post reaction? Nb3Sn formation? • Not seen in TQ/LQ H. Felice - 1st HiLumi/ LARP Collaboration Meeting 18 Dimensional changes during heat treatment Meas. performed at LBNL by J. Krishnan Study on unconfined cables axial contraction: 0.1 to 0.3 % thickness increase: 1.4 to 4 % width increase: 1.5 to 2 % Study on sections of LQ - TQ and HQ coils Thickness LQ and TQ: 5.6 and 6% of increase HQ: only 1 to 2 % of increase Width LQ and TQ => 1 to 2 % of increase HQ => 1 % of increase 11/16/2011 Meas. Performed at FNAL D. Bocian, M. Bossert width H. Felice - 1st HiLumi/ LARP Collaboration Meeting 19 What is different in HQ? • Comparison of the coil fabrication tooling between TQ/LQ and HQ consistency with a constant cavity size at each step of the fabrication • Comparison of the coil cross-sections difference in the nominal design insulation 125 mm in LQ Effective insulation: 86 mm thick 100 mm in HQ Creating a buffer of 80 mm per turn in LQ ~ 6% of LQ cable thickness Creating a buffer of 30 mm per turn in HQ ~ 2% of HQ cable thickness More room in the cavity required for radial and azimuthal expansion 11/16/2011 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 20 Accounting for axial dimensional changes • Axial tension in the conductor ~ 5MPa => Relaxation due to winding tension • Contraction during reaction • Axial gaps in the pole pieces during winding Modulus (MPa) Young modulus measured on various HQ unreacted cables: Modulus (MPa) Modulus vs. Stress for 100lb Cycle 32500 27500 1000R 22500 1010R 17500 1014S 1014R5 1014P1 12500 1014P2 7500 2500 3 13 Stress (MPa) Stress (MPa) Axial contraction due to reaction estimated to be 2 to 3 mm/m 11/16/2011 Winding relaxation estimated to 1mm/m 23 Measured by Brett Collins Total gap size 3 to 4 mm/m H. Felice - 1st HiLumi/ LARP Collaboration Meeting 21 Test Coils “Compaction theory” tested with test coils • Increase of the azimuthal space in the cavity • Still radial compaction • Unusual coil size => FNAL mirror test Rodger Bossert & Guram Chlachidze Coil 12 – 54/61 – cored cable • By adjusting mid-plane shimming ~3 % per turn of additional space • Assembled and tested in FNAL HQM01 Limited by mid-plane turn Improved performance at 150 A/s => 82 % Iss 11/16/2011 Coil 13 – 54/61 – no core • By removing the mid-plane turn in both layers ~5 % per turn of additional space Axial gap increased from 0.8 mm to 2 mm closed after reaction contraction of ~ 3mm/m • Assembled in HQM02 tested at FNAL 91 % of Iss at 4.6 K 89 % of Iss at 2.2 K H. Felice - 1st HiLumi/ LARP Collaboration Meeting 22 HQ02 coils: reduced compaction • A new series of HQ magnets: HQ02 • Main requirement: using the same tooling as HQ01 • Interlayer insulation increased to 500 mm • Accounting for dimensional changes and interlayer insulation Smaller cable with smaller strand => 0.778 mm => 14.8 mm x 1.375 mm Axial gap size 4 mm/m • All coils made with 108/127 conductor • Revision of the end parts design • New approach for the magnetic cross-section Reacted cable dimension based on some assumptions on cable dimensional changes Conductor alignment on the OD of the pole piece 11/16/2011 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 23 Overview of HQ02 coil fabrication Coil Strand Cable Core 14 108/127 1017 No 15 108/127 1020B SS / 8 mm / 25 mm 16 108/127 1020D SS / 8 mm / 25 mm Coil 14 post-reaction: limited protrusion ~1.5 / 2 mm Total axial contraction: 3.5 mm/m • Gap: ~4 mm/m • 0.5 mm/m post curing 11/16/2011 Status Magnet Completed To be tested in mirror Wound & cured To be tested in mirror / HQ02 To be tested in HQ02 Coil 15 post-curing: Total axial contraction: NA • Gap: 4 mm/m • 1 mm/m post curing Ongoing cored cable measurement to get reference numbers for cored cable dimensional changes H. Felice - 1st HiLumi/ LARP Collaboration Meeting 24 HQ persisting electrical weaknesses • Despite increased interlayer insulation • Despite outer layer end-shoe revision • Despite reduced compaction Coil Coil to island Coil to endshoe IL endshoe to OL endshoe Magnet 5 LE – 290 V HQ01 b-c-d-e 7 12.5 kW LE 700-800 V LE – high leakage current HQ01 c-d-e 8 RE – 7.6 kW HQ01 c-d-e 9 RE - 340 V HQ01 d-e 11 Not tested 12 20 kW LE 700-900 V LE – 500 MW HQM01 13 Dead short HQM02 14 LE IL(35 V) / OL (0.5 W) LE – 35 V Not tested Task force set up to address this issue Possible revision in HQ and LHQ 11/16/2011 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 25 Damaged insulation post-reaction Insulation fragmentation after reaction Possibly caused by the use of CTD binder Decision to stop using “precured” glass or Nextel ceramic for the interlayer insulation in the new generation of coils S-glass placed on the OD of the coil during reaction (combination of the brittleness and high compaction) Nextel ceramic interlayer insulation, not treated with binder 11/16/2011 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 26 Summary • 11 coils fabricated with the HQ01 design Observations: coil high compaction, electrical breakdown, somewhat limited performance Possible cause of limitations initial coil design – fabrication process: high compaction • 2 test coils with reduced compaction tested in FNAL mirror • HQ02 design implemented in coils 14 and 15 108/127 conductor, smaller cable, OL end-shoe revision Introduction of SS cored cable in all coils starting with coil 15 11/16/2011 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 27 Some open questions • Electrical weaknesses observed in almost all the coils Failure of the hipot coil to metallic components • Some insulation issues – compatibility with binder • Some uncertainties about the coil dimensional changes • Need to understand if the HQ somewhat limited performance come only from the coil high compaction urgency to get HQ02 coils ready for test • Ongoing investigation Dimensional changes in cored cables Task force for end-shoe redesign and improvement 11/16/2011 H. Felice - 1st HiLumi/ LARP Collaboration Meeting 28
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