WP3 meeting 08/10/2014 Fabrication of test coil for D1 2m model Michinaka SUGANO KEK Purposes of test coil fabrication 1 To verify the following items - Toolings for winding (Mandrel, Forming block, …) Operation test for winding machine, hydraulic press, heater,… Design of end spacers, winding and measurement of coil end Confirmation of curing cycle (temperature profile and homogeneity, pressure) Practice for quality assurance electrical tests of coil (ground fault, cable resistance, turn-turn insulation,…) Once test coil fabrication is completed, it will be used for - Commissioning of coil size measurement - Practice for attaching voltage leads - 200mm-long mechanical model 1 Purposes of test coil fabrication 2 - Radiation resistant GFRP end spacers and wedges End spacers and wedges made of BT resin + S2 glass fibre were used for the first time End spacers were machined in house Can newly developed hard GFRP end spacers be accommodated to the cable by curing ? - Curing with radiation resistant cyanate ester adhesive Curing temperature around 200oC is needed, while it should not influence on contact resistance between the strands (lower than melting point of Stabrite coating) To consider compromised heat treatment condition and check if bonding strength is strong enough even for single layer coil 2 Coil structure Cable: NbTi MB cable with APICAL and PIXEO insulation supplied by CERN Coil configuration: - Single layer coil - 44 turns, 4 coil blocks - Coil length: 2020 mm (between the end saddles) - 2D cross-section for HX-hole of 50 mm (old version) Ramp box Center post Pole shim (GFRP) Wedge(GFRP) Mandrel MP shim(GFRP) Pushing bar 3 Coil end - Coil end shape was slightly modified based on the result of practice winding Practice winding The cable angle was inclined too much and large gap between the cable and end spacer remained End spacer was re-designed to accommodate to the inclined cable (but further modification for the 2m-model coils should be needed) Lead end Return end 4 Layer jump 2D cross-sections of the layer jump Coil layer at the straight section A Pole turn Collar layer at the lead end B C Ramp box was designed in such a way that the layer jump turn go out uprightly Ramp box C B A 5 Coil winding Winding machine Tensioner Feeder Winding mandrel Measurement of cable positions and angles Turn table Winding tension: Started from 40.9 kgf, decreased by 0.25 kgf/turn 6 Fitting of end spacer to cable Gap between the end saddle and the cable remained We checked if the gap can be closed after curing 7 Preparation for curing SUS liner + Midplane shim Pushing bars Alignment pin SUS protective liner 8 Transfer of coil into forming block Pushing the coil into the groove by screwing the bolts Forming block Insertion tooling The coil was successfully inserted to the forming block using the alignment pin and jigs 9 How much should coil be compressed in curing ? Final size of coil is determined by yoking Pressure applied to coil Curing: 50 MPa Yoking: 100 MPa (max) 80 MPa From the results of 10 stack measurement (22 cables), coil after curing should be larger by 0.9 mm than the final size Gap Curing pressure Pushing bar 0.9mm-thick shim Mandrel Forming block 0.9 mm-thick shims were inserted and coil was compressed until the gap was closed 10 Curing press 90 ton hydraulic rams x3x7 over the length of 2m-coil Longitudinal load (5.2 tonf) Hydraulic ram Thickness gauge Vertical load was applied incrementally until the gap was closed 11 Determination of curing pressure 1 2 3 Forming block Mandrel 4 5 Check by Fuji paper 6 Gap Coil pressure: 50 MPa Pressure pattern by pushing bars Gap was closed at hydraulic pressure of 23 MPa Pressure in curing 12 Configuration of heater and thermometers Form-block Mandrel Used for heater control Heater (Both sides) Thermocouples 1m-long cartridge heater Heaters in mandrel 4 in forming block 2 in winding mandrel Thermocouples 10 in forming block 5 in winding mandrel 2 at cartridge heater for mandrel Heaters in forming block 13 Consideration for heat treatment profile Heat treatment condition for cyanate ester Recommended curing pattern given by the company: 150oC x 4h + 180oC x 4h + 220oC x 4h Adopted pattern: 150oC x 4h + 180oC x 8h Heat treatment condition for PIXEO T > 190oC is necessary, but maximum temperature should be limited lower than 220oC (melting point of SnAg coating) Temperature (oC) Test with short sample cable and GFRP plate #3 #3 #1 #1 #2 #3: Adopted pattern, thinly painted #1: Adopted pattern, thickly painted #2: Shortened pattern (no plateau), thinly painted Leakage of adhesive after HT in thickly painted sample “Adopted pattern + thinly painted” was selected Elapsed time (hr) Heat treatment condition for curing 150oC x 4h + 180oC x 8h + >190oC x 0.5h 14 Heat treatment profile for curing Temperature 4h 8h 0.5h Pressure 190℃ Temperature 180℃ 150℃ 100℃ 90℃ Longitudinal press Time - Maximum temperature was selected to be 190oC - Vertical pressure was unloaded/reloaded during heat treatment - Longitudinal pressure was applied from the both ends of the coil 15 Actual temperature trend in curing Bonding of polyimide insulation 190oC 180oC 150oC NN N F-E M F-W M S SS Temperature profile to harden cyanate ester (150oC x 4h + 180oC x 8h) was obtained as expected Max. temperature could be controlled at 190 - 210oC (< 220oC) Expected temperature profile was realized 16 Coil after curing The gap between the end saddle and the cable was closed after curing Hard BT resin + S2 glass GFRP can be accomodated to the cable Bonding between the cable and the wedges is sufficiently strong Effectiveness of heat treatment profile is verified 17 Electrical tests after curing - No ground fault throughout winding and curing - No change of cable resistance (for 44 turn) After winding 242.9 mW Under curing pressure, before curing 242.5 mW After curing 242.2 mW - No damage of cable insulation checked by a bundle of fine Nb-Ti filaments - No turn-turn insulation failure at least up to 1 kV (Surge test) - Coil inductance: 2.3 mH Surge test Electrical soundness of the coil was confirmed 18 Issues to be modified 1 Protective liner The protective liner was plastically deformed after curing Slit for the layer jump Bottom surface of the ramp box Ramp box is slightly popping up Groove for the layer jump Protective liner Forming block Width of the groove should be made smaller Additional support is needed for the layer jump 19 Issues to be modified 2 There is a gap at the boundary of the end spacer and the cable The leads for the QPH could be damaged Approach 1: Modification of coil end shape To make the cable more upright by elongating the length of coil end Approach 2: Filling the gap with shoe 20 Preparation for coil size measurement Same system as CERN (Thanks to G. Kirby) - 50 ton hydraulic press Coil pressure up to 130 MPa Continuous measurement using the 5.4 m-long bench Two pushing bars each having 5 x 20mm-wide fingers Pushing bars with strain gauges 50 ton loading test for checking the support structure and calibration of load-strain relationship for pushing bars have been completed Measurement using the test coil will be carried out soon 21 Future plan Test coil fabrication - Coil size measurement: - Mechanical short model: Oct 2014 Dec 2014 2m-model magnet development - Coil winding: - Delivery of collar and yoke plates: - Instrumentation: - Collaring: - Yoking: Dec 2014 ~ Jan 2015 end of Jan 2015 Feb 2015 ~ end of Feb 2015 Mar ~ April 2015 Test station - Delivery of 15kA current leads: - Inspection by local government: - Commissioning: - Cold test of 1st model magnet: ~end of March 2015 May 2015 Jun 2015 Sep 2015 22 Summary - 2m-long test coil for D1 was wound and cured. - Radiation resistant BT resin + S2 glass GFRP spacers and wedges were used for winding for the first time. Fairly good fitting was confirmed between the spacers and the cable after curing. - Heat treatment up to 190oC for cyanate ester was tried and sufficiently strong bonding was confirmed. - Coil size measurement will be carried out soon. - Mechanical short model will be assembled using straight section cut out from the test coil. - We found some issued to be solved such as support of the ramp box and gap between the top of the cable and end spacer. Modification would be applied to the future 2m-long model coils. 23
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