CONSTRUCTION OBSERVATION REPORT STEGNER FARMS PIT SLURRY WALL Prepared for: HALL-IRWIN CONSTRUCTION 3026 4th Avenue Greeley, Colorado 80631 Prepared by: ROCKY MOUNTAIN CONSULTANTS, INC. Premiere Building 825 Delaware Avenue, Suite 500 Longmont, Colorado 80501 RMC Job No. 19-0636.059.00 August, 2000 TABLE OF CONTENTS Page INTRODUCTION .............................................................................................................................. 1 PROJECT DESCRIPTION................................................................................................................ 1 CONSTRUCTION SUMMARY.......................................................................................................... 2 QUALITY ASSURANCE TESTING................................................................................................... 3 DISCUSSION .................................................................................................................................. 4 General ................................................................................................................................. 4 Desanding Operation ............................................................................................................ 4 Sloughing of Overburden Soils ............................................................................................. 5 Slurry Wall Test Holes........................................................................................................... 6 CONCLUSIONS AND RECOMMENDATIONS................................................................................. 6 List of Tables Table 1 Materials Quality Control Program, Soil/Bentonite, Slurry Trench Cut-Off Wall Table 2 Table 3 Table 4 Stegner Farms Pit Slurry Wall Test Summary Stegner Farms Pit Slurry Wall Areas of Concern Stegner Farms Pit Slurry Wall Results of Slurry Wall As-Built Geotechnical Investigation List of Figures Figure 1 Figure 2 Figure 3A Figure 3B Figure 4 Slurry Wall Vicinity Map As-Built Slurry Wall Test Hole Locations Slurry Wall Summary Logs Slurry Wall Summary Logs Slurry Wall Photos List of Appendices Appendix A Appendix B Appendix C Appendix D Daily Construction Logs Sand Content and Filtrate Analysis S-B Backfill Gradation Trench Depth Worksheets C:\WINNT\Profiles\Colby\Desktop\Construction.rpt.doc INTRODUCTION This report summarizes construction observation results for the on-site and laboratory quality assurance testing conducted during the construction of the Stegner Farms Pit slurry wall. Information contained within this report was collected as part of the construction related engineering services that were provided by Rocky Mountain Consultants, Inc. (RMC) throughout the slurry wall construction. The slurry wall was constructed by Hall-Irwin Construction under a contract with Camas Colorado Inc. Camas Colorado Inc. is preparing to mine gravel aggregate at the site. Upon completion of the mining operations, control of the site will return to the current property owners, John Stegner and Gary Stegner. Construction began on the slurry wall lining project at the Stegner Farms Pit in early April 2000. The construction consisted of lining a proposed gravel pit with approximately 7,500 feet of soilbentonite slurry wall. The goal of the slurry wall liner is to minimize hydraulic interaction between the proposed gravel pit and the surrounding alluvium. The reduction in hydraulic interaction will aid mining efficiency in two ways: 1) by reducing dewatering requirements during mining operations, and 2) by reducing drawdown effects on neighboring wells. Upon completion of the mining activities, the final goal of the slurry wall construction is to provide a low permeability liner for a below grade water storage reservoir. The slurry wall was constructed using a design/build approach. The scope of RMC’s work during construction included on-site quality control and observation of the slurry wall construction. The scope of our work did not include groundwater monitoring or future reservoir design. Hall-Irwin Construction supplied labor, equipment, and materials to construct the slurry wall. PROJECT DESCRIPTION The site is located east of LaPorte, Colorado and is bounded by County Road 54G (old U.S. Highway 287) along the north side, Taft Hill Road along the east, and Brookhill Road along the west. The southern boundary of the project site is parallel to and approximately one-quarter mile south of County Road 54G. The site is more particularly described as being located in Section 33, Township 8 North, Range 69 West of the 6th Principal Meridian, Larimer County, Colorado, as shown on Figure 1. Prior to slurry wall construction activities, the site was agricultural land. The Taylor and Gill Ditch runs parallel to and just south of the southern site boundary. The Cache La Poudre River is located approximately one-half mile south of the project site. The ground surface across the site falls from an elevation of approximately 5045 feet in the northwest corner to approximately 5030 feet in the southwest corner. The slope of the ground from northwest to southeast is a somewhat consistent 0.5 percent across the site. The project area is located approximately one mile east of the eastern flank of the Rocky Mountain Front Range. Regional geologic mapping of the area (Colton, 1978) indicates the near surface bedrock at the site is the lower shale member of the Pierre Shale Formation. Regionally, the lower 1 shale member is described as being comprised of dark olive-gray bentonitic shale. Bedrock at the site is overlain by alluvium regionally mapped as the Post-Piney Creek Alluvium. The site is in an alluvial plain setting. Both the ground surface and bedrock surface slope gently to the southeast in the general direction of flow of the Cache La Poudre River. Geotechnical test holes were drilled along the proposed slurry wall alignment prior to construction. Observed drill cuttings, soil types and depth to bedrock measurements were used as reference during construction. Test hole locations and summary logs are presented on Figures 2 and 3. Depth to bedrock and total trench depths observed during construction are illustrated on the as-built construction drawing (Plate 1). The natural site stratigraphy generally consists of three main units: 1) near surface sandy, silty clay; 2) sand, gravel and cobble alluvial deposits; and 3) claystone and shale bedrock. Depth to bedrock is variable at this site. Bedrock depths ranged from 13 to 22 feet with most of the variations encountered along the north and south sides of the project. Along the east and west sides of the project, bedrock depth was less variable ranging from 15 to 17 feet. The slurry wall as-built dimensions are as follows: an average total width of two feet, total trench depth from 16 to 27 feet with an average value of approximately 19.6 feet, overall slurry wall length of 7,387 feet, and overall trench curtain area of approximately 145,000 square feet. The total area surrounded by the slurry wall is approximately 62.3 acres. CONSTRUCTION SUMMARY The typical slurry wall construction crew consisted of four to five men managed by one superintendent who oversaw and coordinated construction activities. Motor equipment used included a trackhoe excavator, Kamatsu PC400, which excavated the trench through a bentonite slurry; a smaller trackhoe that provided initial soil-bentonite backfill mixing and constructed the slurry mixing pond; one Caterpillar dozer that provided final soil-bentonite backfill mixing, trench backfilling, and slurry mixing pond construction; and a stand-alone pneumatic trailer for on-site storage of bulk bentonite. A slurry pump/desanding unit was at the site to clean the trench bottom and reduce sands suspended in the slurry. Prior to construction of the slurry wall, berms were constructed along the inside of the slurry wall alignment. These backfill berms consisted of overburden soils from on-site, as well as dry bentonite delivered from offsite. The dry bentonite was added at a rate of approximately 120 pounds per linear foot, or approximately 1.5 percent of the dry weight of the backfill soils. One slurry mixing/holding pond was constructed along the slurry wall alignment. A reservoir of slurry was produced by combining and mixing bulk bentonite powder with local groundwater using a conical static mixer. Once in the pond, the slurry was continuously circulated until thoroughly hydrated. The finished slurry product was pumped through four-inch high density polyethylene piping to the open trench section under construction. Pond recirculation and slurry delivery was accomplished using an eight-inch pump. 2 The soil-bentonite (S-B) backfill was composed of four components: 1) soil excavated from the trench, 2) high clay content soil material borrowed on-site, 3) slurry removed from the trench heading during excavation, and 4) dry bentonite applied at an approximate rate of 1.5 percent of the dry weight of the backfill soils. QUALITY ASSURANCE TESTING Resident engineering services were provided by RMC during the slurry wall construction. These services included extensive on-site construction observation, sampling, field testing of various slurry trench parameters, and the assimilation of as-built information. A daily log of construction progress was kept (Appendix A). A material quality control program was followed throughout the slurry wall construction. Test types, frequency, and specified values are summarized on Table 1. In order to provide the quickest possible testing result turn-around time, a testing laboratory was set up on-site. Testing equipment included a mud balance, Marsh funnel, portable electric bench oven, electronic scale, portable sieve shaker, various sieves, wet washing apparatus, ambient temperature filter press, pH meter, sand content kit, and slump cone apparatus. General field results, listed by station/location, are presented on Table 2. Specific test results are shown in Appendices B and C. A rapid turn-around time of the test results allowed for near real time adjustments to the various slurry trench parameters throughout the project. Testing conformed with industry standards, including the American Petroleum Institute - Specifications 13A, the American Petroleum Institute Recommended Practice - Specifications 13-B-2, and ASTM C-143. Slurry viscosity, as measured using a Marsh funnel apparatus, and unit weight values, as measured using a mud balance, were maintained within the acceptable range (V 40 seconds-Marsh, S.G. = 1.03 gm/cc to 1.40 gm/cc). In a few instances the viscosity dropped below the 40 seconds-Marsh due to an excess of water in the slurry mix. These cases of low viscosity occurred at either the mixing pond or the discharge hose. The viscosities were corrected at these locations so that the slurry viscosity in the trench was maintained above the minimum acceptable levels. Filter cake formation of the slurry and filtrate loss were analyzed using an ambient temperature filter press assembly. Filter cake thickness and filtrate loss was generally within the acceptable range. The texture of the cake formation ranged from slightly sandy to very sandy. In a few instances the filtrate loss increased above the acceptable range (30 cc in 30 minutes@100 psi) due to a high sand content (20+ percent). This situation was corrected by replacing the high sand content slurry in the trench with fresh slurry from the slurry pond as quickly as possible. A sand content kit was used to measure the percent sand by volume suspended in the slurry. Sand content was found to range from six to greater than 20 percent. Slump cone, gradation, and moisture content test results on the S-B backfill material were used to control the backfill material properties. Test results in each of these areas were consistently within the acceptable range. In a few instances the slump test results fell outside the acceptable range of 3 two to six inches which resulted in construction directives which specified corrective actions that were carried out immediately. Corrective actions included addition/reduction of slurry added to backfill material and adjustments to the mixing operations. Visual inspection of excavated soils and bedrock were extensively conducted during trenching to detect when adequate bedrock was encountered. As the trenching progressed, the depth of the trench was periodically checked to determine if the bedrock key was maintained and not filling with sediment or other material (Appendix D). At the start-up of slurry wall construction, sedimentation of the trench bottom was observed beyond what was expected. To accommodate the excess sedimentation, the bedrock key was extended a minimum of four feet into bedrock instead of the three-feet specified in the design. Once desanding equipment was delivered to the site and desanding/trench cleaning operations commenced, the minimum bedrock key requirements reverted back to the three-foot minimum as specified in the design. The desanding equipment was then used to clean sediments from the trench slurry and trench bottom to maintain an effective three-foot bedrock key. Comparison of quality control requirements to the field testing and observations indicate that the project requirements were adequately met. Adjustments were made when required as indicated by test results and visual observations. DISCUSSION General Slurry wall construction began in early April 2000 and was completed in late June 2000. Construction was delayed temporarily on occasion due to mechanical breakdowns and poor weather. When necessary, field adjustments were made to the slurry wall alignment. The slurry wall alignment in the southeast corner of the property was rounded to avoid driving heavy equipment over the existing 42-inch City of Greeley water transmission line which parallels the south side of the project area. Other corners were rounded to allow room for the desanding equipment and to avoid property fencing. A portion of the alignment along the north-central area of the project was offset by approximately five feet to the south to avoid damaging existing trees and to allow room for the desanding equipment. The slurry wall as-built alignment is shown on Plate 1. Desanding Operation Slurry wall construction began at Station 0+00 without the use of a desander. Trench depth measurements indicated that sand was settling out of the slurry and depositing on the bottom of the trench. A recommendation was made that desanding equipment be mobilized to the site. To allow work to proceed prior to mobilization of desanding equipment to the site, the trench was extended a minimum of four feet into bedrock, rather than the three feet specified in the design, allowing for approximately one foot of sedimentation and three feet of slurry wall bedrock key. In 4 addition, attempts were made to clean the bedrock key prior to beginning additional trenching each day. The excavator would track over the extent of open trench completed the prior day and scrape the bottom to remove any sediment which had accumulated. This trench cleaning was performed each day until trench side wall sloughing problems (discussed below) widened the trench at the surface to the extent that the track excavator could no longer track back over the open trench. Use of the excavator to clean sediment from the trench was no longer possible beyond Station 17+40 due to sloughing problems. Desanding equipment was mobilized to the construction site on May 3, 2000. The initial desanding equipment consisted of a submersible pump, tank reservoir, and screened shaker mounted to a reinforced steel sled with a diesel generator towed behind. This equipment was mobilized for use due to concerns regarding the settlement of sands from the slurry to the bottom of the trench. The equipment used was specifically manufactured for use in cleaning sand from the trench bottom and reducing the volume of sand suspended in the slurry. Due to malfunctions with the electrical system and the submersible pump, regular operation of the desander did not begin until May 17th near Station 27+00. During the initial operation of the desander, the submersible pump could not be lowered to the bottom of the trench without overloading the electrical components. As a result, sand was removed only from suspension within the trench slurry. Table 3 outlines areas where we suspect a significant amount of sediment has settled into the bedrock key as indicated by measuring trench depths with a weighted line marked at one-foot intervals. On May 26th, the initial desanding equipment was removed from the site and replaced with a smaller desanding unit which was easier to maneuver along the side of the slurry wall trench. The replacement desanding equipment was in operation on May 30th, the next working day. The replacement equipment consisted of similar, but smaller components, mounted on a smaller reinforced steel sled. On May 31st, the submersible pump impeller was replaced with a smaller impeller which allowed the pump to be lowered to the bottom of the trench without overloading the electrical components. From Station 42+25 to the end of the project at Station 75+03, the desanding equipment was felt to be effective in reducing the deposition of sand in the trench bottom. Sloughing of Overburden Soils In a few areas of the slurry wall alignment, sloughing of the overburden soils caused the surface of the trench to widen from approximately two feet to as much as ten feet in some areas (Figure 4). The overburden soils in some areas of the project thinned to approximately one to two feet thick. In addition, slopes of 0.5 to 1.0 percent in some areas of the site resulted in slurry levels along portions of the open trench periodically falling to as much as two to three feet below the ground surface. The combination of thin overburden and low slurry levels contributed to sidewall instability resulting in the observed sloughing. 5 In general, when the sloughing occurred at the point of trenching, the trenching hoe operator was able to clean out the overburden soil as it sloughed into the trench. Attempts were also made to keep the sides of the trench sloped so that overburden soil would not fall into the trench after completion of each trenching set. In a few areas, the overburden soil sloughed into the trench after trenching had been completed in the area and the trackhoe could no longer reach the sloughed material. Table 3 outlines areas where sloughing was observed in areas where the soil could no longer be cleaned from the trench. The presence of the sloughed material was confirmed by checking trench depths using a weighted line marked at one-foot intervals. Slurry Wall Test Holes Five test holes were drilled through the backfilled trench to investigate the as-built condition of the slurry wall with regard to the presence of sloughed overburden soils and sediment that may have settled into the bedrock key. Table 4 outlines the results of the investigation. TH-17 at Station 25+75 encountered approximately four feet of wet, clayey sands and gravels below the S-B backfill, but no material which resembled overburden soils. TH-18 at Station 40+50 encountered four feet of overburden soils, but was not extended deep enough to evaluate the total thickness of overburden soils which had sloughed into the trench. TH-19 at Station 40+75 confirmed that the overburden soils which had sloughed into the trench in this area extend below the top of bedrock a distance of approximately one foot and are underlain by approximately two feet of sediment. TH-15 and TH-16 each encountered a minimal amount of sloughed soils and sediment and also encountered bedrock above the depth to which the trench was completed. This may be attributed to the possibility of the test hole being located at the edge of the slurry wall instead of at the center. Gradation tests were performed on samples collected from test holes TH-15, TH-17, TH-18, and TH-19 to determine the percent of fines (materials passing the #200 sieve) content by weight. The sloughed overburden materials collected from TH-17, TH-18, and TH-19 contained fines materials ranging from 42 to 67 percent by weight. The sediments collected from TH-15 and TH-19 contained 27 and 25 percent fines materials by weight, respectively. The design parameters for the S-B backfill require a fines content of 25 to 40 percent. The results of the gradation testing indicate that the fines content of the sloughed overburden and sediments which have filled the bedrock key meet the minimum fines content requirements for the S-B backfill material. Based on these test results, RMC has recommended that no remedial actions take place at this time to remove the sloughed overburden and sediments from the areas investigated. CONCLUSION AND RECOMMENDATIONS In general, construction of the Stegner Farms Pit slurry wall was performed in conformance with the specified quality control standards. Corrective field actions were quickly implemented when necessary due to visual observations or results of quality control testing. When sand content and filtrate test results did not meet the specifications, fresh slurry was introduced into the trench. 6 When results of slump testing for the S-B backfill did not meet specifications, corrective actions included addition/reduction of slurry added to backfill material and adjustments to the mixing operations. As a final quality control measure, periodic inspections during mining are recommended to check for localized seep zones. Table 3 outlines areas along the slurry wall where either sloughing or excessive sedimentation are suspected to have occurred based on visual observations, trench depth measurements, and/or the results of the drilling investigation. The potential for seepage through the slurry wall in these areas may be greater than the areas of the wall which did not experience sloughing and where desanding operations were effective. If seepage is observed as mining progresses, remedial activities may need to be implemented such as the construction of a low permeability embankment slope liner. 7 TABLE 1 Materials Quality Control Program Soil/Bentonite Slurry Trench Cut-Off Wall SUBJECT Material STANDARD MINIMUM FREQUENCY SPECIFIED VALUES Water ---- -pH -Total Hardness Per water source or as changes occur As required to properly hydrate bentonite with approved additives Additives ---- Manufacturers certificate of compliance with stated characteristics One time As approved by Engineer Bentonite API Std 13A Manufacturers certificate of compliance One time Premium grade sodium cation montomorillonite Selected soils obtained from a borrow area approved by the Engineer Per borrow source or as changes occur -65 to 100% passing 3/8" -40 to 85% passing #20 -25 to 40% passing #200 Roll to 1/8" thread Backfill Soils Prepared for Placement into the trench ---- API Std 13B -Unit Weight -Viscosity -Filtrate Loss 1 set per shift or per batch (pond) -pH Slurry Backfill Mix TYPE OF TEST Unit weight ≥1.03 gm/cc V ≥ 40 sec-March @ 68° Loss ≤ 30 cc in 30 min. @ 100 psi pH ≥ 8 In Trench API Std 13B 1 -Unit Weight -Sand Content 1 set per shift at point of trenching -Unit weight = 1.03 - 1.40 gm/cc -Sand content = 20% by volume At Trench ASTM C 143 -Slump -Gradation 1 set per 100 cu/yds. 1 set per 300 cu/yds. -Slump 2 to 6 inches -65 to 100% passing 3/8" sieve -40 to 85% passing #20 sieve -25 to 40% passing #200 sieve Table 2 Stegner Farms Pit Slurry Wall Test Summary Slurry Mixture Test Location (sta.) Water Pond Slurry Pond Slurry Pond 1+00 Slurry Pond 1+75 Slurry Pond 2+75 3+00 Slurry Pond Slurry Pond 3+80 5+25 Slurry Pipe 7+00 Slurry Pipe 7+70 Slurry Pipe 8+45 Slurry Pipe 9+10 Slurry Pipe 10+25 Slurry Pipe Date 4/10 4/12 4/12 4/12 4/13 4/13 4/24 4/24 4/24 4/24 4/25 4/25 4/26 4/28 4/28 4/29 4/29 4/29 4/29 5/1 5/1 5/1 5/1 5/2 Marsh Funnel Viscosity (sec) Unit Weight Filtrate Loss (gm/cc) (ml) 35 44 1.12 1.07 54 1.09 30 1.05 32 29 Soil-Bentonite Backfill Mix Sand Content (vol %) 22.8 Cake Thickness (in) 0.0625 8.25 27.6 11 0.125 27.0 10 0.125 23.6 22.8 7 7 0.125 0.125 28.6 6 0.1875 1.06 1.03 39 44 1.19 1.06 36 1.06 26.6 10 0.1875 27.6 12 0.1875 36 36 37 30.2 40 44 35 1.07 1.15 pH 7.10 11 Test Location (sta.) Date 0+00 0+50 1+50 1+50 4/25 4/25 4/26 4/26 0.50 5.50 7.50 5.50 2+75 3+50 4+00 4+00 4+25 5+00 6+00 6+50 7+50 4/27 4/27 4/29 4/29 4/29 5/1 5/1 5/1 5/2 5.25 5.25 7.50 5.00 4.00 5.00 6.00 4.00 5.00 8+50 5/2 9+20 10+00 10+60 5/2 5/3 5/3 Slump (in) 3/8" (%) #20 (%) #200 (%) Moisture Content (%) 98 80 85 66 49 34 26 20 93 77 48 28 85 95 69 78 42 48 27 29 96 80 50 26 3.50 94 82 55 26 4.00 6.00 3.75 97 72 42 28 0.125 Signature of Technician Page 1 of 5 Table 2 Stegner Farms Pit Slurry Wall Test Summary Slurry Mixture Test Location (sta.) 11+05 11+75 Slurry Pond Slurry Pipe Slurry Pond 13+50 Slurry Pipe 16+45 Slurry Pipe 17+50 Slurry Pipe Slurry Pond 19+80 Slurry Pond 21+50 Slurry Pond 23+00 Slurry Pond 24+00 Slurry Pond Slurry Pond 25+80 Slurry Pipe 28+50 Date 5/2 5/2 5/3 5/3 5/3 5/3 5/3 5/5 5/5 5/5 5/6 5/9 5/9 5/10 5/10 5/11 5/11 5/12 5/12 5/13 5/13 5/13 5/15 5/18 Marsh Funnel Viscosity (sec) 39 45 44 52 45 47 49 Sand Content (vol %) Cake Thickness (in) 20 0.1875 30.8 16 0.1875 18.8 10 0.125 18.4 16 0.125 20.2 18 0.125 Unit Weight Filtrate Loss (gm/cc) (ml) 1.17 37.6 1.06 1.07 43 1.07 1.19 1.07 1.17 1.06 1.07 1.26 1.06 96 1.08 34 1.03 1.23 37 48 Soil-Bentonite Backfill Mix 17.4 34 41 53 43 1.06 1.39 1.07 1.26 27.2 0.125 14 0.125 20+ 22.6 20 0.125 pH Test Location (sta.) 11+00 11+50 Date 5/3 5/4 Slump (in) 5.50 6.25 3/8" (%) #20 (%) #200 (%) Moisture Content (%) 93 81 48 27 14+00 15+50 16+00 17+00 17+50 18+00 18+50 20+00 21+00 21+50 5/5 5/9 5/9 5/9 5/10 5/10 5/10 5/12 5/13 5/13 3.50 3.00 2.50 4.00 5.50 5.00 5.00 5.00 6.50 4.50 76 84 64 69 38 42 22 24 97 79 50 27 91 89 86 94 68 73 70 75 41 45 40 40 26 26 24 23 23+00 23+50 24+00 24+75 25+50 26+00 26+75 27+50 5/15 5/15 5/15 5/18 5/19 5/19 5/19 5/20 2.50 3.00 3.50 5.00 5.00 4.00 6.00 5.50 94 75 40 23 76 57 27 26 87 72 37 27 Signature of Technician Page 2 of 5 Table 2 Stegner Farms Pit Slurry Wall Test Summary Slurry Mixture Test Location (sta.) Slurry Pond 31+40 33+90 Slurry Pond Desander 36+00 Slurry Pond Slurry Pond Date 5/19 Marsh Funnel Viscosity (sec) 46 5/19 5/22 5/23 5/23 5/23 5/24 5/25 41+30 Slurry Pond Slurry Pond 42+50 5/30 5/31 5/31 5/31 45+00 Slurry Pond 6/1 6/2 47+45 6/3 Unit Weight Filtrate Loss (gm/cc) (ml) 1.06 1.35 51 50 41 48 41 42 44 Soil-Bentonite Backfill Mix 1.36 1.05 1.35 1.39 29.0 Sand Content (vol %) 20+ Cake Thickness (in) 0.1875 39.8 20+ 0.1875 30.5 29.1 20 20+ 0.125 0.1875 1.05 1.34 1.06 33.1 1.24 25.8 1.34 1.06 1.24 20 15 0.125 0.125 20 21.9 13 0.125 pH Test Location (sta.) 28+00 29+00 29+50 30+50 31+50 32+50 33+75 34+50 35+50 36+50 37+00 37+50 38+00 38+50 39+50 40+00 41+00 42+50 43+50 44+50 45+00 45+50 46+00 46+50 Date 5/20 5/22 5/22 5/22 5/23 5/23 5/24 5/24 5/25 5/26 5/26 5/30 5/30 5/30 5/31 5/31 6/1 6/1 6/2 6/3 6/3 6/5 6/5 6/5 Slump (in) 5.50 6.00 4.50 4.50 5.00 4.50 3.50 4.00 4.50 6.00 5.50 5.50 5.00 5.00 4.50 5.00 5.50 5.50 5.00 5.00 4.00 5.50 5.00 5.00 3/8" (%) 92 #20 (%) 76 #200 (%) 39 Moisture Content (%) 27 91 74 38 25 80 62 39 21 81 63 29 21 81 85 61 69 29 35 21 25 89 69 38 25 90 79 49 26 97 77 83 62 55 38 27 24 89 67 41 25 94 82 51 25 Signature of Technician Page 3 of 5 Table 2 Stegner Farms Pit Slurry Wall Test Summary Slurry Mixture Test Location (sta.) Slurry Pond Date 6/6 49+50 Slurry Pond 6/6 6/7 51+00 Slurry Pond 6/7 6/8 53+00 6/8 56+00 Slurry Pond Slurry Pond Slurry Pond 58+00 Slurry Pond 60+50 6/9 6/9 6/9 6/10 6/10 6/12 6/12 63+00 6/13 Slurry Pond 6/14 Marsh Funnel Viscosity (sec) 38 Soil-Bentonite Backfill Mix Unit Weight Filtrate Loss (gm/cc) (ml) 1.05 Sand Content (vol %) Cake Thickness (in) 11 47 1.02 12 44 1.22 1.06 1.19 7 38 45 40 44 1.24 1.06 1.06 1.26 1.08 1.26 47 1.06 9 19.4 11 0.125 14.0 7 0.1875 13 pH Test Location (sta.) 47+50 48+00 49+00 50+00 50+50 51+00 52+00 52+50 54+00 54+50 55+00 56+00 57+00 57+50 58+00 59+00 59+50 60+25 61+50 62+00 62+50 63+00 63+50 64+00 Date 6/7 6/7 6/7 6/8 6/8 6/9 6/9 6/9 6/10 6/10 6/10 6/12 6/13 6/13 6/13 6/13 6/13 6/14 6/15 6/15 6/16 6/16 6/16 6/16 Slump (in) 2.50 7.00 6.00 4.00 2.00 3.00 5.00 5.00 3.50 4.50 5.00 4.50 4.00 4.50 6.00 3.00 6.00 1.00 4.50 4.50 6.50 3.50 5.50 3.50 3/8" (%) 93 #20 (%) 75 #200 (%) 47 Moisture Content (%) 28 92 71 41 26 77 60 32 20 86 69 37 24 93 76 43 23 93 97 75 83 38 39 25 29 93 74 41 27 96 90 78 76 42 43 28 26 28 92 75 38 25 Signature of Technician Page 4 of 5 Table 2 Stegner Farms Pit Slurry Wall Test Summary Slurry Mixture Marsh Funnel Viscosity (sec) Soil-Bentonite Backfill Mix Test Location (sta.) 6470 Slurry Pond Slurry Pond 6660 Date 6/14 6/15 6/16 6/16 Slurry Pond 6885 6/19 6/19 46 Slurry Pond 6/20 43 1.05 7210 Slurry Pond 6/21 6/21 19.7 43 1.31 1.05 7470 6/22 1.35 23.1 62 44 Unit Weight Filtrate Loss (gm/cc) (ml) 20.8 1.06 1.06 1.23 15.6 1.06 1.32 20.8 Sand Content (vol %) 20 11 20 18 20+ Cake Thickness (in) 0.125 0.125 0.125 0.125 0.1875 pH Test Location (sta.) 6500 6575 6650 6700 6800 6875 6950 7050 7100 7150 7200 7300 7400 7450 Date 6/19 6/19 6/19 6/19 6/20 6/21 6/21 6/22 6/22 6/22 6/22 6/22 6/23 6/23 Slump (in) 5.50 6.50 5.50 5.00 6.00 5.50 4.50 4.50 3.50 3.00 3.50 4.50 5.50 5.00 3/8" (%) 87 #20 (%) 71 #200 (%) 35 Moisture Content (%) 24 76 60 33 24 90 73 41 28 86 70 37 25 92 81 38 24 90 71 34 24 Signature of Technician Page 5 of 5 Table 3 Stegner Farms Pit Slurry Wall Areas of Concern Station 5+75 to 6+50 6+90 to 7+10 17+00 to 18+50 Reason for Concern Other Notes Visually observed localized sloughing of overburden soils; approximately 3 to 4.5 feet of material in 5-foot key based on use of weighted measuring line; material is likely a combination Good results from filter press test on slurry from this area of of sediment overlain by the sloughed soils; could not return to area trenching. Sand content 10 percent. Good results from filter press test on slurry from this area of Bedrock key full or nearly full of sediment based on depth measurements. trenching. Sand content 10 percent. Sediment approximately 2 to 3 feet deep in 4-foot key based on depth measurements; could Good results from filter press test on slurry from this area of not return to area with track hoe to clean out bedrock key. trenching. Sand content 10 percent. Visually observed localized sloughing of overburden soils; bedrock key full of material based on depth measurements; material is likely a combination of sediment overlain by sloughed Poor results from filter press test on slurry from this area of soils; could not return to area with track hoe to clean out bedrock key trenching. Sand content 20+ percent. 24+00 to 26+00 28+50 to 30+00; 32+00 to 33+00; 34+75 to 35+25; 35+75 to 36+25; Bedrock key full or nearly full of sediment based on depth measurements; could not return to 36+75 to 37+75 area with track hoe to clean out bedrock key. 40+25 to 41+00 Sloughing of overburden soils suspected based on visual appearance of trench banks upon returning from weekend; 2 to 8 feet of material in 3-foot bedrock key based on depth measurements; presence of sediment and sloughed overburden soils confirmed by te 63+75 to 64+25 Bedrock key full or nearly full of sediment based on depth measurements. Poor results from filter press test on slurry from this area of trenching. Sand content 20+ percent. Desander in operation but pump could not be lowered to bottom of trench. Poor results from filter press test on slurry from this area of trenching. Sand content 20 percent. Desander in operation but pump could not be lowered to bottom of trench. Good results from filter press test on slurry from this area of trenching. Sand content 13 to 20 percent. Desander in operation with pump being set at bottom of trench. Table 4 Stegner Farms Pit Slurry Wall Results of Slurry Wall As-Built Geotechnical Investigation As-Trenched As-Built Investigation Top of Sand (ft) Bedrock Encountered (ft) Sampled Interval (ft) Dry Weight Passing #200 (%) 18.5 18.0 19.6 17 - 19 27 16.5 / 21.0 NE 17.0 17.3 ----- ----- 2575 16.5 / 20.5 NE 16.0 20.0 18 - 20 42 TH-18 4050 15.0 / 18.0 10.0 NE NE 12 - 14 67 TH-19 4075 15.0 / 18.0 13.0 17.0 19.0 15 - 17 17 - 19 50 25 Test Hole ID Top of Bedrock Top of / Total Depth Sloughed Soils (ft/ft) (ft) Station TH-15 710 19.0 / 23.0 TH-16 905 TH-17 R:\0636_059\CoverSheet.dwg, 11/13/2008 1:31:26 PM R:\0636_059\PlanView.dwg, 11/13/2008 1:44:48 PM R:\0636_059\Testholes.dwg, 11/13/2008 11:43:14 AM R:\0636_059\Testholes.dwg, 11/13/2008 11:45:28 AM R:\0636_059\Photos Figure.dwg, 11/13/2008 12:03:30 PM APPENDIX A DAILY CONSTRUCTION LOGS Stegner Farms Pit Slurry Wall Daily Construction Logs-4/10/00 to 5/6/00 4/10/00 and 4/11/00 - Site preparation was started on approximately April 4. Platform preparation has begun with backfill berms being placed on the inside of the slurry wall with bentonite _ A soils testing lab has been set up on site for quality control of construction materials. _ A plastic lined slurry pond was built near Station 20+00 for the purpose of mixing trench slurry. _ Construction equipment arrived at varying times after April 4. _ A water pond was dug next to the slurry pond to enable the use of groundwater for mixing of trench slurry. The pH of the water source was 7.10 on the first day of production. _ Construction of a pair of backfill berms on the inside of the slurry wall has begun and will be ongoing during the first few days of construction. Bentonite is being mixed into the berm closest to the slurry wall for inclusion in the backfill mix. 4/12/00 - First day of digging trench. Trenched 0+00 to 1+25. _ Bedrock encountered at 16.5 to 17.0 feet. Initial bedrock key is 3 feet. Bedrock is layered and somewhat crumbly with water apparent in the layering. May need to dig deeper to find more competent bedrock. _ Dug water pond bigger to keep from running out before each slurry bentonite truck is offloaded. 4/13/00 - Trenched 1+25 to 2+00. _ Some sediment in bedrock key from 0+00 to 1+25. Delayed to discuss depth of bedrock key to look for better bedrock and to accommodate sediment while maintaining 3-foot key. We will try to get a 4- to 5-foot key into bedrock. 4/14/00 - Cleaned out 0+00 to 0+25 and recovered mainly sand from the bottom of the trench. _ Shutdown until all parties can agree on a depth of key based on bedrock conditions as well as a solution for sediment build-up in the trench. 4/19/00 - RMC, Hall-Irwin, and Camas have agreed to get a desander for the site to removed sediment buildup in the trench. Until the desander is operational, the length of trench dug each day will be cleaned again the following morning to remove sediment. Until the desander is operation, the bedrock key will extend a minimum of four feet into bedrock. Once the desander is operational, the bedrock key will extend a minimum of three feet into bedrock. 4/24/00 - Work resumed with bedrock key a minimum of four feet. _ Trenched 2+00 to 3+15. _ Trench slurry is a thin at 32 seconds through the Marsh funnel. Hall-Irwin crew having troubles with some of the equipment at the bentonite mixing pond. _ 0+00 to 2+00 should be re-keyed as the wall is completed to remove sediment from key. F:\0636_059\CONSTRUCTION\CONSTRUCTION LOG 4-10 TO 5-6.DOC 4/25/00 - Trenched 3+15 to 4+55 with 4-foot key. _ Trench slurry still thin. Mixing hopper is not working right. Bentonite and water are not mixing properly out of the hopper. It needs to have some veins welded to the inside of the discharge pipe to create turbulence in the mixture. _ Backfilled 0+00 to 1+25. First couple of batches were too dry but have improved significantly. 4/26/00 - Trenched 4+55 to 5+25. _ Backfilled 1+25 to 2+50 _ Cleaned trench back to 3+50 (approximate location of toe of slope for backfill) _ No bentonite slurry added to trench today. 4/27/00 - Still having trouble at bentonite mixing pond. Hall-Irwin now has a trailer on site to hold the bentonite powder until mixing it so that delivery trucks don’t have to stay at site while backfill mixes straight from their trucks. The trailer is not working right and slurry is thin again. _ Trenched 5+25 to 5+50 _ Backfilled 2+50 to 3+50 4/28/00 - Trenched 5+50 to 7+00 _ Backfilled 3+50 to 3+70 _ Slurry going into trench has improved to 44 seconds through the Marsh funnel. 4/29/00 - Trenched 7+00 to 8+95 _ Backfilled 3+70 to 4+75 _ Possible leaky area in wall between 5+50 and 6+50, particularly near 5+90 to 6+00. Banks of trench have sloughed off and there is no way for the excavating hoe to get back to the area now that we have turned the corner and are heading west. 5/1/00 - Trenched 8+95 to 10+95 _ Backfilled 4+75 to 7+00 _ The corner (approximately 6+90 to 7+10) appears to have a significant amount of sediment and material in the key. It tagged at 19 feet and bedrock tagged at approximately 19 feet. Spoke with Hall-Irwin about cleaning it out but due to the configuration of the corner (the backhoe would need to sit to the side of the trench to clean it) we would cause more problems if we tried to clean it. 5/2/00 - Trenched 10+95 to 12+85 _ Backfilled 7+00 to 9+50 _ Cleaned trench 9+15 to 10+95 _ Slurry still mixing thin. 5/3/00 F:\0636_059\CONSTRUCTION\CONSTRUCTION LOG 4-10 TO 5-6.DOC _ _ _ _ _ Trenched 12+85 to 15+10 Backfilled 9+50 to 11+30 Cleaned trench 11+00 to 12+85 Bentonite slurry has improved significantly to 45 seconds through Marsh funnel. Desander is almost ready for operation and has been placed next to trench at 14+80. Possible leaky area at 12+50 to 12+75. This is the area of the trench that we cleaned to in the morning. Sloughing of the trench walls at 12+95 has prevented us from getting back to the area to clean it again. 5/4/00 - Trenched 15+10 to 16+35 _ Backfilled 11+30 to 13+50 _ Desander operated for approximately three hours before the submersible pump burned up. _ Down for approximately four hours to repair mixing backhoe. 5/5/00 - Trenched 16+35 to 17+60 _ Backfilled 13+50 to 14+75 _ Cleaned trench 15+75 to 16+35 _ Mixing backhoe and dozer broke down after lunch. Backhoe has a broken hydraulic hose. Dozer has a bad hydraulic pump. 5/6/00 - Mixing backhoe and dozer still down. _ Could not clean trench to sloughing of walls at 17+70 _ Trenched 17+60 to 18+25 _ No backfilling Conclusions: The first two weeks of production have gone somewhat slowly due to equipment problems. The bedrock has been consistently around 17 feet deep and locally up to 19 feet deep. The bedrock generally consists of a one-foot weathered orange-brown claystone zone that is slightly moist. Below the weathered zone, the claystone becomes shaley with layering more apparent at increasing depths. The initial layering is disorganized and slightly moist. The layering in the deeper bedrock becomes thicker and slightly moist to wet between layers. The bedrock also becomes harder with the thicker layering. Below the weathered zone the bedrock becomes gray with occasional orange-brown areas. The backfill has been generally within the specifications on all tests beyond Station 0+50. The fines content (-200 material by weight) has been in the 45 to 50 percent range which is slightly higher than called for in the specifications but should not pose a problem as long as the backfill mixture remains workable. The desanding operations are expected to resume on Wednesday, May 10. F:\0636_059\CONSTRUCTION\CONSTRUCTION LOG 4-10 TO 5-6.DOC Stegner Farms Pit Slurry Wall Daily Construction Logs-5/8/00 to 5/20/00 5/8/00 - Trenched 18+25 to 19+40. _ Backfilled 14+75 to 15+25. 5/9/00 - Trenched 19+40 to 20+40. _ Backfilled 15+25 to 17+25. _ Could not clean trenching from previous day due to sloughing of overburden along trench sides. _ Potential problem area from 17+50 to 18+50 where bedrock key was tagged at less than 3 feet. _ Desander not running yet. 5/10/00 - Trenched 20+40 to 22+20. _ Backfilled 17+25 to 19+30. - Could not clean trenching from previous day due to sloughing of overburden along trench sides. - Potential problem areas at 19+75 and 20+50 where bedrock key was tagged at less than 3 feet. _ Desander not running yet. 5/11/00 - Trenched 22+20 to 23+30. _ No backfilling. - Could not clean trenching from previous day due to sloughing of overburden along trench sides. - Potential problem areas at 20+50, 21+00, 21+25 and 21+75 where bedrock key was tagged at less than 3 feet. _ Desander not running yet. 5/12/00 - Trenched 23+30 to 24+25. _ Backfilled 19+30 to 20+50. - Could not clean trenching from previous day due to sloughing of overburden along trench sides. - Desander not running yet. 5/13/00 - Trenched 24+25 to 26+30. _ Backfilled 20+50 to 22+75. - Could not clean trenching from previous day due to sloughing of overburden along trench sides. - Sloughing continues to worsen due to thinning overburden. Trying to control it by removing areas of cracking before finishing each set. Some sloughing has occurred after completion of sets in areas that can no longer be reached by the backhoe. 5/15/00 - Trenched 26+30 to 27+50. _ Backfilled 22+75 to 24+45. - Could not clean trenching from previous day due to sloughing of overburden along trench sides. _ Extensive sloughing during trenching has resulted in trench widths of 7 to 10 feet at surface. This makes it very difficult to accurately check trench depths. - Potential problem areas from 24+00 to 26+00 where bedrock key was tagged at less than 3 feet. 5/16/00 - No work completed due to equipment problems. 5/17/00 - Trenched 27+50 to 27+70 _ No backfilling _ Work day shortened by equipment problems and heavy rains. 5/18/00 - Trenched 27+70 to 30+00. _ Backfilled 24+45 to 25+40. - Desander in operation. 5/19/00 - Trenched 30+00 to 31+70. _ Backfilled 25+40 to 26+75. - Sloughing continues during trenching but we have been able to significantly reduce the occurrence of sloughing after each trenching set is completed. Width of trench still makes it difficult to accurately check trench depths. _ Potential problem areas from 28+50 to 30+00 where bedrock key was tagged at less than 3 feet. _ Desander in operation. 5/20/00 - Trenched 31+70 to 33+00. _ Backfilled 26+75 to 28+75. - Potential problem area from 32+50 to 32+60 where sloughing occurred beyond the reach of the trenching backhoe. _ Desander in operation. Conclusions: Construction progress has improved. However, due to thinning of the overburden along the south side of the project, the overburden has been sloughing during and after completion of trenching in some areas. We are trying to control the amount of sloughing material that falls into the trench by removing any unstable areas of overburden before the completion of each trenching set. Several areas of the bedrock key along the south side have tagged at less than 3 feet. This may be due to sediment accumulation or sloughing of overburden. It may also be due to the difficulty in accurately checking the trench depth due to the increase in width of the trench at the surface due to the sloughing. Desanding operations began on May 18 and have continued. Stegner Farms Pit Slurry Wall Daily Construction Logs-5/22/00 to 6/3/00 5/22/00 - Trenched 33+00 to 34+95. _ Backfilled 28+75 to 31+40. _ Sloughing of overburden has improved significantly. _ Slurry sand content very high. Need to get fresh slurry introduced into trench. _ Desander in operation but pump cannot be lowered to bottom of trench with overloading. _ Potential problem area from 32+00 to 33+00 where bedrock key was tagged at less than 3 feet. 5/23/00 - Trenched 34+95 to 37+05. _ Backfilled 31+40 to 33+60. _ Slurry sand content remains high (20+%). - Desander in operation but pump cannot be lowered to bottom of trench with overloading. - Potential problem areas at 35+00 and 36+00 where bedrock key was tagged at less than 3 feet. 5/24/00 - Trenched 37+05 to 38+60. _ Backfilled 33+60 to 35+20. _ Desander in operation but pump cannot be lowered to bottom of trench with overloading. _ Potential problem area from 36+00 to 37+50 where bedrock key was tagged at less than 3 feet. 5/25/00 - Trenched 38+60 to 39+81. _ Backfilled 35+20 to 36+25. _ Trying to improve sand content in slurry by removing high sand-content slurry at point of trenching and at backfill while pumping fresh slurry into trench near desander. _ Desander in operation but pump cannot be lowered to bottom of trench with overloading. _ Potential problem area from 37+50 to 38+50 where bedrock key was tagged at less than 3 feet. 5/26/00 - Trenched 39+81 to 41+25. _ Backfilled 36+25 to 37+00. _ Potential problem area from 39+00 to 40+50 where bedrock key was tagged at less than 3 feet. _ Replacement desander arrived on-site. Old desander pulled away from trench at 8:40am. New desander not set up yet. 5/30/00 - Trenched 41+25 to 42+15. _ _ _ _ Backfilled 37+00 to 39+00. Replacement desander began operation at 1:40pm. Localized minor sloughing of overburden evident throughout open trench. Potential problem area from 40+25 to 41+00 where significant sloughing occurred and trench tagged very shallow. 531/00 - Trenched 42+15 to 43+40. _ Backfilled 39+00 to 40+50. _ A new impeller has been put on the desander pump. It is now being set at the bottom of the trench key. _ Slurry sand content has improved (15%). 6/1/00 - Trenched 43+40 to 45+39. _ Backfilled 40+50 to 42+70. _ Desander in operation with pump set at bottom of trench key. 6/2/00 - Trenched 45+39 to 46+45. _ Backfilled 42+70 to 43+50. 6/3/00 - Trenched 46+45 to 47+67. _ Backfilled 43+50 to 45+00. Conclusions: Sloughing has improved with one problem area between 40+25 and 41+00. Several areas of the bedrock key along the west side have tagged at less than 3 feet. This may be due to sediment accumulation or sloughing of overburden. A new desander was put into operation on 5/30/00. The desander pump was retrofitted with a smaller impeller on 5/31/00 which allows the pump to now be set at the bottom of the trench key. Stegner Farms Pit Slurry Wall Daily Construction Logs-6/5/00 to 6/23/00 6/5/00 - Trenched 47+67 to 48+72. - Backfilled 45+00 to 46+70. - Minor sloughing of overburden visible near backfill. Should not impact bedrock key. 6/6/00 - Trenched 48+72 to 50+12. - Backfilled 46+70 to 46+90. - No areas of overburden sloughing visible. 6/7/00 - Trenched 50+12 to 51+50. - Backfilled 46+90 to 49+50. - No areas of overburden sloughing visible. Minimal amounts of material have settled into bedrock key. 6/8/00 - Trenched 51+50 to 53+60. - Backfilled 49+50 to 50+50. - Three to six inches of material settled into bedrock key. 6/9/00 - Trenched 53+60 to 56+10. - Backfilled 50+50 to 54+00. - No areas of overburden sloughing visible. Minimal amounts of material have settled into bedrock key. 6/10/00 - Trenched 56+10 to 58+20. - Backfilled 54+00 to 55+50. - No areas of overburden sloughing visible. Minimal amounts of material have settled into bedrock key. 6/12/00 - Trenched 58+20 to 61+15. - Backfilled 55+50 to 56+50. - No areas of overburden sloughing visible from weekend. 6/13/00 - Trenched 61+15 to 63+57. - Backfilled 56+50 to 59+50. 6/14/00 - Trenched 63+57 to 65+18. - Backfilled 59+50 to 61+00. - No areas of overburden sloughing visible. 6/15/00 - Trenched 65+18 to 66+00. - Backfilled 61+00 to 62+25. - No areas of overburden sloughing visible. Six to 12 inches of material has collected in bedrock key. Station 64+00 tagged as if bedrock key was full of sediment. 6/16/00 - Trenched 66+00 to 67+60. - Backfilled 62+25 to 64+50. 6/17/00 - No work completed due to heavy rain. 6/19/00 - Trenched 67+60 to 69+60. - Backfilled 64+50 to 67+20. 6/20/00 - Trenched 69+60 to 71+25. - Backfilled 67+20 to 68+40. - Drilled five test holes in completed slurry wall to evaluate condition of bedrock key. - Sloughing has begun again but crew has been able to keep sides sloped so that material does not fall into trench after completion of trenching sets. 6/21/00 - Trenched 71+25 to 73+25. - Backfilled 68+40 to 71+10. - Sloughing continues at point of trenching but no areas of sloughing are visible after completing and leaving each set. - Zero to 12 inches of material has collected in the bedrock key. 6/22/00 - Trenched 73+25 to 75+03 (also 0+00). - Backfilled 71+10 to 73+50. - Sloughing continues at point of trenching but no areas of sloughing are visible after completing and leaving each set. 6/23/00 - Re-trenched 0+00 to 1+20. - Backfilled 73+50 to 75+03 (also 0+00) to 1+20. - Slurry wall has been completed. Crew will begin site cleanup on June 26. Conclusions: The desander was fully operational throughout this period. Sloughing began again near 70+00 but crew was able to remove loose material during each trenching set so that material did not fall into bedrock key after completion of each set. Trench depths indicated that approximately six to twelve inches of sediment was collecting along the bedrock key with localized areas of deeper sediment. Locally, the bedrock was too hard for the key to be extended a full three feet into bedrock. In these areas, the minimum key was two feet into bedrock. The slurry wall construction was complete on June 23 after re-trenching and backfilling the 0+00 to 1+20 interval. APPENDIX B SAND CONTENT AND FILTRATE ANALYSIS STEGNER FARMS PIT SLURRY WALL SAND CONTENT AND FILTRATE ANALYSIS SAMPLE I.D. Slurry Pond 100 175 275 300 380 700 770 910 4/12 4/12 4/13 4/24 4/24 4/25 4/28 4/29 5/1 TEST PRESSURE 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 1175 5/2 100 psi 240 310 37.6 0.1875 1350 5/3 100 psi 301 331 30.8 0.1875 1750 5/5 100 psi 355 425 18.8 0.125 1980 2150 2300 2400 5/9 5/10 5/11 5/12 100 psi 100 psi 100 psi 100 psi 202 249 312 146 232 319 342 216 0.125 0.125 0.125 0.125 2580 5/13 100 psi 239 259 18.4 20.2 17.4 27.2 28.8 / 20 min ; filter press leaking CO2 2850 3140 3390 34+00 (Desander) 3600 4130 4250 4500 4745 4950 5100 5300 5600 5800 6050 6300 DATE TIME API - 30 MIN. FILTER CAKE START END FILTRATE LOSS (ML) THICKNESS (IN) 1253 318 331 1106 246 1237 257 126 153 103 328 341 1136 316 107 327 156 223 7.6 / 10 min 9.2 / 10 min 9.0 / 10 min 23.6 22.8 28.6 26.6 27.6 30.2 0.0625 0.125 0.125 0.125 0.125 0.1875 0.1875 0.1875 0.125 100 psi 100 psi 100 psi 1238 1207 206 108 1237 236 22.6 29.0 39.8 0.125 0.1875 0.1875 5/23 5/23 5/30 100 psi 100 psi 100 psi 1046 916 132 1116 946 202 30.5 29.1 33.1 0.125 0.1875 0.125 6/3 6/6 6/7 6/8 6/9 6/10 6/12 6/13 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 100 psi 152 1142 725 204 1235 145 250 130 125 227 222 25.8 0.125 More troubles with filter press leaking CO2 755 234 1240 ----200 253 235 21.9 20.0; Valve leaked CO2 Valve leaked CO2 Valve leaked CO2 Valve leaked CO2 19.4 14.0 Valve leaked CO2 Slightly Sandy Moderately Sandy Moderately Sandy Moderately Sandy Moderately Sandy Very Sandy Very Sandy Very Sandy % BY VOLUME 11 10 7 7 6 10 12 11 20 16 10 16 18 14 20+ 5/18 5/19 5/22 5/31 6/1 SAND CONTENT COMMENT 0.125 0.1875 0.125 0.1875 6470 6/14 100 psi 727 757 20.8 0.125 6660 6/16 100 psi 838 908 15.6 0.125 6885 6/19 100 psi 226 256 20.8 0.125 7210 6/21 100 psi 119 149 19.7 0.125 7470 6/22 100 psi 854 924 23.1 0.1875 Moderately Sandy Very Sandy Very Sandy Moderately Sandy Very Sandy Moderately Sandy; Good Cohesive Cake Slightly Sandy; Good Cohesive Cake Cohesive Cake Slightly Sandy Moderately Sandy; Good Cohesive Cake Moderately Sandy; Good Cohesive Cake Moderately Sandy; Good Cohesive Cake Moderately Sandy; Good Cohesive Cake Slightly Sandy; Good Cohesive Cake 20 20+ 20+ 20 20+ 20 15 20 13 11 12 7 9 11 7 13 20 11 20 18 20+ APPENDIX C S-B BACKFILL GRADATION STEGNER FARMS PIT SLURRY WALL S-B BACKFILL GRADATION SAMPLE I.D. 0 50 400 500 600 750 850 1000 1150 1400 1550 1700 1850 2000 2150 2300 2475 2675 2800 2950 3150 3375 3550 3650 3800 3950 4100 4250 4450 4600 4750 4900 5050 5200 5400 5500 5610 5800 5950 6025 6150 6300 6500 6650 6800 6950 7100 7300 DATE TARE WEIGHT SAMPLE WEIGHT (-TARE) DRY WEIGHT (-TARE) MOISTURE CONTENT 4/25 4/25 4/29 5/1 5/1 5/2 5/2 5/3 5/4 5/5 5/9 5/9 5/10 5/12 5/13 5/15 5/18 5/19 5/20 5/22 5/23 5/24 5/25 5/26 5/30 5/31 6/1 6/1 6/3 6/5 6/7 6/7 6/8 6/9 6/10 6/10 6/12 6/13 6/13 6/14 6/15 6/16 6/19 1/0 6/20 6/21 6/22 6/22 (gm) 250 245 320 320 335 315 315 335 330 315 320 335 335 335 335 320 335 335 315 315 335 335 335 320 315 325 335 335 335 320 335 335 335 335 15 335 340 325 315 330 325 335 335 320 315 335 325 335 (gm) 1015 1000 690 1030 1060 1230 1350 1285 1355 1120 1375 1265 1585 1450 1370 1245 1445 1275 1650 1345 1420 1555 1640 1415 1385 1465 1630 1520 1625 1440 1365 1365 1325 1200 1230 1350 1420 1310 1460 1725 1350 1820 1740 1985 1640 1765 1130 1595 (gm) 750 800 500 750 755 905 1000 920 990 870 1045 925 1170 1075 1035 955 1070 935 1210 1010 1120 1235 1290 1065 1035 1080 1190 1150 1220 1080 980 1015 1065 915 940 1010 1005 955 1050 1270 975 1365 1315 1515 1185 1330 855 1220 (%) 26.1 20.0 27.5 27.2 28.8 26.4 25.9 28.4 26.9 22.3 24.0 26.9 26.2 25.9 24.5 23.3 26.0 26.7 26.7 24.9 21.1 20.6 21.3 24.7 25.3 26.3 27.0 24.3 24.9 25.0 28.2 25.6 19.6 23.8 23.6 25.2 29.2 27.1 28.1 26.4 27.8 25.0 24.4 23.7 27.7 24.6 24.3 23.5 DRY WEIGHT PASSING 3/8' #20 (%) 98 80 93 85 95 96 94 97 93 76 84 97 91 89 86 94 76 87 92 91 80 81 81 85 89 90 97 77 89 94 93 92 77 86 93 93 97 93 96 90 93 92 87 76 90 86 92 90 (%) 85 66 77 69 78 80 82 72 81 64 69 79 68 73 70 75 57 72 76 74 62 63 61 69 69 79 83 62 67 82 75 71 60 69 76 75 83 74 78 76 77 75 71 60 73 70 81 71 #200 (%) 49 34 48 42 48 50 55 42 48 38 42 50 41 45 40 40 27 37 39 38 29 29 29 35 38 49 55 38 41 51 47 41 32 37 43 38 39 41 42 43 42 38 35 33 41 37 38 34 APPENDIX D TRENCH DEPTH WORKSHEETS Stegner Farms Pit Slurry Wall Trench Depth Worksheet (Work Completed May 8 through May 20, 2000) Station 15+50 16+00 16+50 17+00 17+50 Depth to Bedrock 17.0 18.0 18.0 19.0 17.0 Depth of Trench 21.0 22.5 22.5 23.0 21.0 Depth Tagged Between Trenching and Backfill 8-May 9-May 10-May 11-May 12-May 18+00 17.0 21.0 19.0 18+50 18.0 22.5 20.5 19+00 18.0 22.5 22.5 19+50 19.0 23.0 18.0 7.0 20+00 17.0 21.0 20.0 19.0 20+50 16.0 20.0 18.5 18.0 21+00 16.0 20.0 19.5 18.0 21+50 17.0 21.0 20.0 22+00 16.5 20.5 20.0 22+50 16.5 20.5 20.5 23+00 18.5 22.5 7.5 23+50 22.0 25.0 16.5 24+00 17.0 21.0 24+50 19.0 23.0 22.0 17.0 25+00 16.0 20.0 19.0 16.0 25+50 19.0 23.0 12.0 26+00 16.5 20.5 12.5 26+50 18.0 22.0 27+00 18.5 22.5 27+50 21.0 24.0 11.0 28+00 19.0 22.0 18.5 28+50 17.0 20.0 16.0 29+00 17.0 20.0 16.5 29+50 16.5 19.5 17.0 30+00 16.0 19.0 17.0 30+50 16.0 19.0 19.0 31+00 17.0 20.0 31+50 15.5 18.5 32+00 18.5 21.5 32+50 15.0 18.0 13-May 15-May 16-May 17-May 18-May 19-May BTS 13.5 19.0 BTS BTS 16.5 BTS = Backfilled To Surface Note: Due to the increasing width of trench at the ground surface (see Daily Construction Logs), trench depths checked on 5/15 and 5/19 may not be representative of actual trench depths. Can not reach out to centerline of trench so tag line may be getting caught along edge of trench. BTS 20-May Stegner Farms Pit Slurry Wall Trench Depth Worksheet (Work Completed May 22 through June 3, 2000) Station 29+50 30+00 30+50 31+00 31+50 Depth to Bedrock 16.5 16.0 16.0 17.0 15.5 Depth of Trench 19.5 19.0 19.0 20.0 18.5 Depth Tagged Between Trenching and Backfill 22-May 23-May 24-May 25-May 26-May 32+00 18.5 21.5 15.0 32+50 15.0 18.0 14.0 33+00 15.5 18.5 15.0 33+50 16.0 19.0 34+00 16.5 19.5 15.5 34+50 17.0 20.0 18.0 35+00 16.0 19.0 15.0 35+50 16.0 19.0 18.5 36+00 15.0 18.0 16.0 36+50 15.0 18.0 16.5 37+00 15.0 18.0 15.0 15.0 37+50 15.0 18.0 17.0 16.0 38+00 16.0 19.0 18.0 13.0 38+50 15.0 18.0 17.0 16.5 39+00 15.0 18.0 16.0 7.5 39+50 16.0 19.0 17.5 13.0 40+00 15.0 18.0 17.0 16.5 40+50 15.0 18.0 16.5 10.0 41+00 15.0 18.0 16.0 41+50 16.0 19.0 19.0 42+00 17.0 20.0 42+50 16.0 19.0 43+00 15.0 18.0 30-May 31-May 1-Jun 2-Jun 3-Jun BTS 11.0 16.0 16.0 BTS BTS BTS 16.5 12.5 BTS BTS BTS 43+50 15.0 18.0 11.0 44+00 15.0 18.0 16.0 44+50 16.0 19.0 16.0 45+00 14.0 18.0 14.0 BTS 45+50 15.0 18.0 15.0 46+00 15.5 18.5 17.5 46+50 14.0 17.0 BTS = Backfilled To Surface Stegner Farms Pit Slurry Wall Trench Depth Worksheet (Work Completed June 5 through June 14, 2000) Station 45+00 45+50 46+00 46+50 4700 Depth to Bedrock 14.0 15.0 15.5 14.0 14.5 Depth of Trench 18.0 18.0 18.5 17.0 17.5 4750 19.0 21.0 4800 17.5 20.0 4850 16.0 19.0 4900 16.0 19.0 4950 15.0 18.0 5000 17.0 20.0 5050 15.0 18.0 5100 15.0 18.0 5150 15.0 18.0 5200 14.0 17.0 5250 13.0 16.0 5300 13.5 17.0 5350 15.0 18.0 5400 15.0 18.0 5450 15.0 18.0 5500 17.0 20.0 5550 15.0 18.0 5600 15.0 18.0 5650 15.0 18.0 5700 14.0 17.0 5750 17.0 20.0 5800 16.0 19.0 5850 16.0 19.0 5900 16.0 19.0 5950 16.0 19.0 6000 15.0 19.0 6050 17.0 20.0 6100 18.0 21.0 6150 16.0 19.0 6200 16.0 19.0 BTS = Backfilled To Surface Depth Tagged Between Trenching and Backfill 5-Jun 6-Jun 7-Jun 8-Jun 9-Jun BTS 13.5 16.5 16.5 20.0 10-Jun 12-Jun 13-Jun 14-Jun Stegner Farms Pit Slurry Wall Trench Depth Worksheet (Work Completed June 15 through June 23, 2000) Station 6100 6150 6200 6250 6300 Depth to Bedrock 18.0 16.0 16.0 17.0 16.0 Depth of Trench 21.0 19.0 19.0 20.0 19.0 6350 15.0 18.0 18.0 6400 17.0 20.0 17.0 6450 16.0 19.0 18.0 6500 21.0 23.0 6550 17.0 20.0 6600 16.0 19.0 6650 15.0 18.0 6700 14.0 17.5 6750 15.0 17.5 6800 14.0 17.0 6850 14.0 17.0 6900 14.0 17.0 6950 14.0 17.0 7000 14.0 17.0 7050 14.0 17.0 15.0 7100 14.0 17.0 17.0 7150 16.0 19.0 7200 14.5 17.5 7250 13.0 16.0 7300 13.0 16.0 7350 15.0 18.0 7400 14.0 17.0 7450 14.0 17.0 7500 15.0 18.0 BTS = Backfilled To Surface Depth Tagged Between Trenching and Backfill 15-Jun 16-Jun 17-Jun 19-Jun 20-Jun BTS 21-Jun 10.0 17.5 17.5 BTS 22-Jun 23-Jun
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