Straw Cutting Process Improvement Industrial Engineering Designer: Matthew Estock (Project Manager) Mechanical Engineering Designers: Ian Balbresky, Tyler Banta, Mark Vaughn Client Coordinator: Wayne Geith Supervising Professor: Dr. Matthew Marshall Rochester Institute of Technology 76 Lomb Memorial Drive Rochester, NY 14623 INTRODUCTION The primary goal of the ArcWorks Straw Cutting Device project was to design, build, and deliver a functional straw cutting device to ArcWorks which will be able to cut multiple polypropylene copolymer (PPCO) straws to desired lengths with minimal deformation and burring. The device will have to follow ISO 9001 guidelines, along with complying with OSHA standards and being accessible to employees with a wide range of developmental disabilities. These straws are used within an assembly process at the ArcWorks facility which provides wash bottle assemblies for customers like Thermo Fisher and Nalgene. The current process at ArcWorks utilizes one automated machine along with a manual process to cut the raw material straws to the appropriate lengths. With the addition of our automated machine an increase in overall productivity at ArcWorks within their wash bottle assembly process will be seen; the increased productivity will benefit workers who are paid by the piece, and will also allow ArcWorks to reduce inventory levels. SUMMARY OF IMPACT The current device (shown in Figure 17) is able to safely cut 12 straws at a time, and is capable of cutting 1400 straws/hr, compared with the existing device’s 700 straws/hr capability, meaning that employees can increase their production and ArcWorks can reduce their safety stock. Unfortunately, the quality level of the cuts is not up to the standards set by ArcWorks. Figure 17. Straw cutter design. Clockwise from top right: blade carriage, trap door/height adjustment, vacuum attachment, and cutting plate. 4”, 2-column TECHNICAL DESCRIPTION The new device is a pneumatically-driven machine that cuts 12 straws at a time, safely and with minimal physical exertion, and removes the debris from the cutting area. The straw cut is completed using a single blade with a double bevel that is angled at 45 to the direction of motion (as shown in Figure 17). The straw pattern was laid out to maximize blade utilization and to ensure that only one new cut is initiated at a time. The blade is mounted on a blade carriage system that is driven by a 300 lb cylinder with a 3 in stroke. The cylinder operates on a 100 psi compressed air supply, already available in the ArcWorks facility. The cylinder is triggered with a two hand anti-tie down switch, and a mechanical switch only allows actuation when the lid is closed. The pneumatic system design is shown in Figure 18. The cut quality does not currently meet ArcWorks’s requirements, possibly due to the double bevel on the new cutting blade. The blade cuts through approximately half of the straw satisfactorily, but beyond that point, the straw bends and the remainder of the cut has the appearance of a tear, rather than a clean cut (Figure 19). The team has developed recommendations, including applying slight pressure to hold the straw in place and prevent bending, and using a different blade type; these will be investigated before delivering the machine to ArcWorks. Figure 18. Pneumatic system schematic 2.4” final height, 1-column Figure 19. High-speed images of straw cut. 1.7”, 2-column The device was required to be capable of cutting 9 different straw lengths, so an adjustable trap door mechanism was designed to support the straws during cutting. The height of the trap door can be changed to any of the 9 required length settings, and after a cut is complete a 12 lb pneumatic cylinder, with 1 in stroke, opens the door and allows the cut straws to fall down for removal. The trap door does not currently function as designed, so a backup block (Figure 20) was created to support the straws until further work on the device can be completed. The block does not allow the 9-length adjustability, but does allow the machine to function. Figure 20. Straw support block. 2” final height, 1-column The total cost of the project was $1541.63 More information is available at https://edge.rit.edu/content/P11008/public/Home Leak Test Station Process Improvement Industrial Engineering Designer: Andrew Lawlor Mechanical Engineering Designers: Adam Janicki, Christopher Somers, and John Zeffer Client Coordinator: Dennis Hezner Supervising Professor: Dr. Matthew Marshall Rochester Institute of Technology 76 Lomb Memorial Drive Rochester, NY 14623 INTRODUCTION The goal of this project was to design and build a pressure test device for use by employees at ARCWorks, a light manufacturing facility employing individuals with developmental disabilities. The existing test fixture relied on water to pressure-test, so it was messy, subjective, and it slowed down the assembly line. The current process involves an employee taking a cap, screwing it onto a bottle, plunging the bottle under water, and looking for air bubbles that may be escaping, which would indicate a leak. Employees are generally paid on a per-piece basis, so it is important to make the process as clear, safe, and efficient as possible. SUMMARY OF IMPACT The team took a two-pronged approach to the problem. First, they designed a new test fixture for employees on this line to use. The fixture is still under development, and is expected to be completed over the summer. It will allow a worker to run two tests simultaneously, and provides a very simple, objective indication system: A green LED indicates a good part, a red LED indicates a bad part, and a yellow LED indicates that a test is in progress. The second aspect of the project was to improve the manufacturing process. The team implemented a 5S (Sort, Set, Shine, Standardize, and Sustain) system in two phases, which gave the operators a sense of ownership and pride in their accomplishments. Figure 10. Pressure test fixture. TECHNICAL DESCRIPTION The design team chose a vacuum pressure approach, because it would be the simplest for the operators to use. The pressure test fixture the team designed and built is shown in Figure 11. The cap sits upon a soft rubber to create a seal. The two red buttons seen at the front left and right of the base plate are for the operator to initiate the test. The use of two buttons ensures that the worker will not run the risk of injuring their hands or interfering with the test. Shown behind the cap, at the top of the back plate, are the red and green light indicators. These indicators show the results of the test: red for a bad part and green for a good part. The yellow light is illuminated when the test is in progress. Below and behind the fixture (not shown) is a differential pressure sensor to measure the speed of pressure drop and a vacuum pump to pressurize the fixture. Operation of the machine is simple and intuitive for the operator to use. The operator will take a cap from their “incoming” lane. The operator will then place the cap onto the test fixture. Next the operator will press the two-hand start button. This will allow the machine to run unaffected by the operator. The vacuum will then run and determine if there is a good seal on the cap. If the seal is bad, a red light will indicate to the operator that the part is bad, and if the part is good a green light will appear. The vacuum will then release its pressure, allowing the operator to remove the cap and place in its respective bin. This process can be run simultaneously on both of the stations on the machine. Examples of good and bad part pressure curves are shown in Figure 12. To allow the system to function autonomously from a PC interface, the team used a Programmable Logic Controller (PLC) to control the system. The PLC will turn on the vacuum pump, read the pressure sensor, and control the indicator lights according to the pressure readings (pass, fail, or in-progress). The PLC also reads in a user-set switch position that indicates the particular configuration of cap being tested. The final system testing indicated that the vacuum test fixture resulted in more rejected parts than the water test system, partly because workers did not formerly hold the caps under water for a specific amount of time, and some leaks only become apparent over time. However, the new system did allow two parts to pass that actually failed the water test. Final work on this device is being done during the Summer of 2010. Figure 11. Actual pressure test system built. Figure 12. Examples of good and bad vacuum test data. The total cost of the project was $2106. More information is available at https://edge.rit.edu/content/P10008/public/Home
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