Proceedings: 2003 DEER Conference U.S. Department of Energy 9th Diesel Engine Emissions Reduction Conference Newport, Rhode Island, August 24 to 28, 2003 SELECTIVE CATALYTIC REDUCTION OF DIESEL ENGINE NOX EMISSIONS USING ETHANOL AS A REDUCTANT Michael D. Kass, John F. Thomas, Samuel A. Lewis, Sr., John M. Storey, Norberto Domingo, and Ron L. Graves Oak Ridge National Laboratory ABSTRACT NOx emissions from a heavy-duty diesel engine were reduced by more than 90% and 80% utilizing a full-scale ethanol-SCR system for space velocities of 21000/h and 57000/h respectively. These results were achieved for catalyst temperatures between 360 and 400oC and for C1:NOx ratios of 4-6. The SCR process appears to rapidly convert ethanol to acetaldehyde, which subsequently slipped past the catalyst at appreciable levels at a space velocity of 57000/h. Ammonia and N2O were produced during conversion; the concentrations of each were higher for the low space velocity condition. However, the concentration of N2O did not exceed 10 ppm. In contrast to other catalyst technologies, NOx reduction appeared to be enhanced by initial catalyst aging, with the presumed mechanism being sulfate accumulation within the catalyst. A concept for utilizing ethanol (distilled from an E-diesel fuel) as the SCR reductant was demonstrated. INTRODUCTION The use of hydrocarbons to reduce diesel exhaust NOx emissions via selective catalytic reduction (SCR) has not been studied as extensively as urea-based SCR systems. Benchscale evaluations of hydrocarbon-SCR (HC-SCR) have typically not demonstrated high efficiencies (greater than 80 percent NOx reduction) for realistic space velocities (1). On the other hand urea-SCR was developed in the 1970s for stationary applications (including stationary diesel engines) and has consistently demonstrated NOx reduction efficiencies greater than 90 percent when the SCR system operates in a favorable temperature window (2). In fact, urea-SCR is one of a few catalyst technologies capable of reducing diesel NOx emissions to the 2007 NOx limit of 0.2 g/bhp-hr (2). There are also concerns with applying urea-based SCR to on-road vehicles, including 1) the need for a separate onboard tank for urea, 2) the infrastructure to supply urea, 3) residue buildup during inadvertent over-injection or injection at low temperatures, 4) corrosivity associated with urea, 5) high freeze point, and 9) the performance is best at optimum NO/NO2 ratios which, in turn, require a pre-oxidation catalyst to maintain optimum NO/NO2 ratios which can only be partially controlled using a pre-oxidation catalyst. Because of these concerns, there is a need for more convenient SCR systems, preferably those that use diesel fuel or a fuel-borne additive as the Alexander Panov Caterpillar, Inc. reducing agent. As a result, investigators have been pursuing new methods of HC-SCR. HYDROCARBON SCR Although the development of hydrocarbon-based SCR has not progressed as far as urea-based systems, catalysts utilizing hydrocarbon reductants have been developed and evaluated since the 1980s. The NOx reduction efficiencies for HC-SCR have tended to be lower than for ammonia-based SCR systems (1, 3-7). Of the HC-SCR systems studied, the alumina supported (highly-loaded) silver catalysts have been identified as one of the more promising NOx control technologies for light-duty diesel emissions (1). Successful reducing agents include paraffins, alcohols, and aldehydes. In some cases, the conversion levels can be greater than 80% for the temperature range of 350 to 500oC and these systems have demonstrated good resistance to both water and SO2 inhibition. Although the effects of SO2 are not well known, recent investigations have suggested that the formation of sulfate on the silver surfaces actually improves the NOx conversion of these catalysts (8-9). It is believed that the accumulation of sulfate on the silver sites increases the selectivity toward NOx reduction, which correspondingly increases HC slip and reduces N2O formation (9). ETHANOL AS A REDUCTANT Ethanol has been demonstrated to be a successful reducing agent for silver-doped alumina catalyst systems (1, 5, 8, 9). In the mid 1980s Caterpillar developed and marketed an ethanol-SCR system for use with stationary diesel engines; NOx conversion efficiencies were around 75% (10). More recent studies have shown that when using ethanol as a reductant over alumina supported silver catalysts, NOx conversion efficiencies greater than 90% were observed for a C1:NOx ratio of 4 and a space velocity (SV) of 50000/h (10). In addition it appears that the NOx conversion efficiency is independent of the NO/NO2 ratio (8-9). These investigations; however, were performed under controlled laboratory settings and actual performance data from engine tests are lacking. Ethanol is also of interest because it can be easily incorporated into diesel fuel using an emulsifying agent. Ethanol has been evaluated as an additive to diesel fuel over 1 the past 20 years to 1) lessen the demand for imported oil, 2) promote the use of a domestic renewable resource to power diesel engines, and 3) to lower particulate matter (PM) emissions. Previous efforts have shown that ethanol-diesel mixtures (commonly known as E-diesel) containing up to 15% ethanol are relatively stable and do not adversely affect engine operation (12). The ethanol, ECD-1 fuel, and GE Betz additive (Blending Agent DMX10011) were splash-blended by Growmark Inc. at their manufacturing facility to form a stable micro-emulsion containing 15 % by volume ethanol. REDUCTANTS Fuel-borne reductant separation RATIONALE OF CURRENT WORK The primary rationale guiding this effort was to investigate the NOx reduction potential for ethanol-SCR using a heavy-duty diesel engine. This included performing a convincing proof-ofconcept for use of a fuel-borne reductant. Specifically, we wanted to show that the ethanol (contained within E-diesel) has the potential to reduce NOx emissions via HC-SCR after being separated (by mild distillation) from the fuel blend and used as an injected reductant preceding an alumina supported silver catalyst. An on-board processing system (not part of this work) can be envisioned to strip ethanol from the base fuel and inject it into the exhaust as a reductant for NOx conversion. . NOMENCLATURE C1 DOE ECM E-diesel EGR FG FTIR GC-MS HC HC-SCR NOx NTRC ORNL PM SCR SV A means for expressing hydrocarbon concentration. It is obtained by multiplying the number of carbon atoms per molecule by the concentration in ppm. Department of Energy Electronic Control Module A ethanol and diesel fuel mixture, usually containing a blending agent and mixed as a microemulsion Exhaust Gas Recirculation Fuel Grade Fourier Transform Infrared Gas Chromatigraph-Mass Spectrometer Hydrocarbon Hydrocarbon – Selective Catalytic Reduction Oxides of Nitrogen National Transportation Research Center Oak Ridge National Laboratory Particulate Matter Selective Catalytic Reduction Space Velocity MATERIALS AND EQUIPMENT TEST FUELS The test fuels investigated in this study included BP/ARCO ECD-1 and an E-diesel blend originally containing 15 vol.% ethanol, 1.5 vol.% blending agent, and 83.5 vol.% ECD-1. ECD-1 is a low sulfur diesel fuel (less than 15 ppmv) developed to reduce the levels of regulated emissions. The ethanol used in this study was fuel-grade (supplied by Williams-Pekin, Inc.) and is a corn-derived product denatured using gasoline and containing a corrosion inhibitor; pertinent specifications are listed in Table 1. Table 1. Specifications for fuel-grade ethanol supplied by Williams-Pekin, Inc. Ethanol content, vol.% 92.1 min Methanol content, vol.% 0.5 max Denaturant content, vol.% 2 min, 5 max Water content, mass% ~0.5 Approximately 1 liter of ethanol was stripped from 7 liters of the E-diesel blend through the application of moderate heat and vacuum using a laboratory distillation device (Buchi RE-121 Rotovapor). Visual inspection showed that the distillate was of single phase. This suggests that the distillate was primarily ethanol since diesel fuel, including the light aromatic constituents, is immiscible with ethanol, even at low concentrations. This relatively simple test demonstrates the feasibility of using an on-vehicle device to remove lesser portions of ethanol from E-diesel. The remaining ~6 liters of stripped E-diesel fuel (mostly depleted of ethanol) was added back to the original blend which subsequently lowered the ethanol content to ~13 vol.%. This partially stripped E-diesel was also evaluated as a test fuel. Evaluated reductants The two reductants evaluated in this study were fuel-grade ethanol in the as-received condition (untreated) and the ethanol portion that had been stripped (distilled) from the E-diesel blend. Both the untreated and stripped ethanol batches were evaluated as reducing agents while running the engine on ECD-1. Following these tests, the engine was operated using the 13 vol.% E-diesel blend while using the stripped ethanol as the reductant. A single test was performed using reagent-grade (high purity) ethanol. SCR SYSTEM IMPLEMENTATION The ethanol delivery system consisted of a cooled Buick gasoline injector, a fuel injection pump (Mallory Series 60FI), and a return style regulator, which was used to maintain pressure near 400 kPa. The injector was located in a bend in the exhaust 64 cm from the turbo outlet. Caterpillar, Inc. provided two seven liter catalysts to ORNL. The catalysts had a cell density of 31 cells/cm2 (200 cells/in2) and measured 24.1cm (9.5 in) in diameter by 15.2 cm (6 in) long. They were installed in the exhaust at a distance of ~1.5 meters from the engine turbo outlet. During the initial test runs, the second brick was installed directly behind the first catalyst. During this investigation the exhaust was unfiltered (no particulate traps were used). EXPERIMENTAL FACILITY The evaluation was conducted at the National Transportation Research Center (NTRC) by ORNL staff. A Cummins 5.9 liter ISB turbo-charged, direct injection, diesel engine (1999 model, 24 valve, in-line 6 cylinder) was used as the test engine. This engine was altered from the commercially available version due to the addition of a Cummins supplied exhaust gas recirculation system and a non-standard ECM, fuel pump, fuel injectors, and turbine. The engine was rated for 175 HP and 2.5 g/HP-h of NOx over the heavy-duty STP. The EGR valve could be controlled either via the ECM map or by manual override. The engine was coupled to a General Electric direct current motoring 2 dynamometer capable of absorbing 224 kW (300 hp) and motoring 213 kW (285 hp). The ethanol-SCR system layout and sample locations are shown schematically in Fig. 1. Gaseous emissions were sampled from the raw exhaust stream and directed to a standard emissions bench and a Fourier Transform Infrared (FTIR) spectrometer. The standard bench (composed of Horiba Ltd. and California Analytical Instruments analyzers) provided measurements of NOx, THC, CO, CO2, and O2. The FTIR spectrometer (Nicolet Instrument Corp. Magna-IR 560) provided speciation of ammonia, N2O, and acetaldehyde. using fuel-grade ethanol by injecting into a graduated cylinder for measured time periods. EXPERIMENTS INITIAL SHAKEDOWN AND CATALYST DEGREENING Both catalysts were initially mounted in the exhaust. Initial shakedown evaluations were performed to evaluate the operation and performance of the ethanol delivery system, bench analyzers, and data acquisition system. The engine was run at several different operating modes for about 2 to 3 hours with reductant injection to briefly examine the performance of the catalysts in the green state. Following this, the catalysts were aged for approximately 10 hours while maintaining the engine exhaust temperature near 400oC. REDUCTANT INJECTION The general method for testing at a given condition (set engine speed and load, fuel type, reductant type, catalyst) was to begin with a relatively low reductant injection rate. After achieving steady-state conditions and recording data, the injection rate was increased. In this manner we would sweep across a reasonable range stoichiometry and stop when relatively high HC slip was observed. SPACE VELOCITY COMPARISON Fig. 1. Schematic diagram showing layout of ethanol-SCR components and sampling locations. A stream of exhaust was sent to a micro-dilution tunnel for additional speciation via GC-MS and for measurement of N2O and ethanol slip. Bag samples were drawn from the microdiluter for hydrocarbon speciation via GC-MS. In addition a photoacoustic spectrometer (from Innova AirTech Instruments model 1312) was used to measure both ethanol slip and tailpipe N2O emissions. This instrument has been used successfully to quantify ethanol emissions from vehicles operating on ethanol/gasoline blends (6). Fuel consumption was measured using a Max Machinery Inc. fuel flow measurement system. Intake airflow was measured using a Marion laminar flow element. The space velocity of the gas flux was calculated and reported for standard conditions. A custom PC-based system was used to control reductant injection. Injector duty cycle (% of time in open position) was adjusted to control the flow rate of ethanol into the exhaust. Other system parameters were held constant, such as the injector pulsing frequency (10 Hz) and the ethanol injection line pressure (~400 kPa) and ethanol temperature (30-40oC). The injection system was calibrated for a relevant duty cycle range During the initial test results after aging we suspected that the first catalyst brick was providing the bulk of the SCR capability and that the second catalyst brick was relatively ineffective. For this reason, and also to achieve SV values in a realistic range, the downstream (or second) catalyst brick was removed. For most tests the ethanol-SCR system performance was evaluated for a relatively low SV of ~21000/h and a higher SV near 57000/h, while attempting to maintain the same narrow catalyst temperature range for both conditions. The engine operating modes corresponding to these two conditions are detailed below in Table 2. (SV is reported for STP.) Table 2. Key engine operating parameters for space velocity evaluation Space velocity (1/h) ~21000 ~57000 Engine Speed (rpm) 1115 2225 Engine torque (ft-lbs) 230 180 Catalyst temperature (oC) 350 to 380 350 to 380 NOx flux (g/min) 1.5 2.1 During normal operation the NOx flux for the low-speed condition was significantly higher than the high-speed condition. The EGR valve was controlled to be partially open for the low speed (21000/h) condition in order to reduce the NOx emissions. (During both operating modes the EGR valve is normally closed.) As revealed in the table, the NOx flux ended up being higher for the high-speed condition. TEMPERATURE EVALUATION In addition to measuring the conversion efficiency of the catalyst between 350 to 400oC, data was also taken to evaluate o performance between 250 and 350 C. The torque applied to 3 the low-speed condition was reduced to obtain lower catalyst core temperatures. The conversion efficiency was evaluated for two C1(2X ethanol):NOx ratios. EVALUATION OF REDUCTANT AND FUEL TYPE The performance of the SCR catalysts was determined as a function of the reductant type (untreated or distilled ethanol) for both the low and high-speed conditions while operating the engine using ECD-1 fuel. In addition the performance was also evaluated (for both conditions) using distilled ethanol as the reductant while operating the engine using the E-diesel blend (which was the source of the distilled ethanol). In order to gain insight into reductant impurity contributions, an additional experiment was performed utilizing high-purity reagent-grade ethanol with the engine operating on ECD-1 fuel. The NOx flux and catalyst temperature did not change appreciably when running the engine on ECD-1 or E-diesel at the above two conditions. Bag samples for the GC-MS analysis were taken for several of the test sequences. Generally bag samples were taken for a perceived high and low slip condition (low and high reductant injection rates). installation are also included in the diagram, since this data represents the initial state of the catalysts following the degreening period. (Note that because two catalyst bricks were used for this condition, the SV is one-half the value of the other presented data.) During the runs taken on October 8, 9, and 17 untreated fuel-grade (FG) ethanol was used as the reductant and the engine was operated using ECD-1 fuel. The engine was run using ECD-1 for the days of October 10 and 15, but distilled FG ethanol was used as the reducing agent for these evaluations. The Oct. 16 data was taken while running the engine on E-diesel and utilizing distilled FG ethanol as the reductant. This data set represents a simulation of a fuel-borne reductant, where the fuel used to run the engine was also used to supply the reducing agent for the catalyst. An additional data set taken on Oct. 17 using high purity reagent-grade ethanol is shown in Fig. 2. Table 3. condition Test RESULTS AND DISCUSSION DESCRIPTION OF TEST CONDITIONS The test conditions depicted in Table 3 show the key operating parameters associated with each test condition, including the day each particular study was performed. Operating parameters associated for each test Space Velocity date shakedown tests Fuel ECD-1 10 hrs, catalyst aging ECD-1 1 Oct. 7, 8 10,500 ECD-1 2 Oct. 8 28,500 ECD-1 3 21,000 ECD-1 57,000 ECD-1 21,000 ECD-1 As shown in Table 3, we evaluated 8 conditions as part of this investigation. The test conditions labeled as 1, 3, 4, and 5 were repeated on later days. Key parameters included space velocity, fuel type, and reductant type. 4 5 Oct. 8-10, 17 Oct. 8, 15, 17 Oct. 10, 15 ENGINE OPERATION AND EMISSIONS 6 Oct. 16 21,000 E-diesel 7 Oct. 16 57,000 E-diesel 8 Oct. 17 21,000 ECD-1 Analysis of the engine-out emissions for both engine operating conditions is shown in Table 4. Both the chemiluminescent bench detectors and the FTIR spectrometer showed that the NOx in the exhaust was primarily NO. The engine-out NOx emission levels were similar for both fuel types. However, the E-diesel fuel did produce a small increase in the emissions of HC and CO, which was consistent with earlier results when running the engine on this fuel type. There was also a drop in engine performance associated with E-diesel usage. This is expected since the energy density of the 13% ethanol fuel is about 6% lower than the straight ECD-1 fuel. In addition, the combustion characteristics for the two fuels are not identical. NOx CONVERSION RESULTS The NOx conversion efficiencies associated with the ethanolSCR system were measured over a 2-week period in October 2002. The initial runs incorporated both catalyst bricks. However the back brick was removed since it lowered the SV to unrealistically low levels and made interpretation of the data more difficult. As shown in Figs 2 and 3 the NOx conversion efficiency increased with increasing C1:NOx ratio for both the low SV condition (Fig. 2) and the high SV condition (Fig. 3). The conversion efficiencies associated with the double brick EtOH Reductant Fuel-grade, as received none Fuel-grade, as received Fuel-grade, as received Fuel-grade, as received Fuel-grade, as received Distilled from Ediesel Distilled from Ediesel Distilled from Ediesel Reagent grade Table 4. Bench analyzer results for engine operating conditions and fuel type Bench Results 1115 rpm/230 ft-lbs (21000/h) ECD-1 E-Diesel 2225 rpm/180 ft-lbs (57000/h) ECD-1 E-Diesel NOx, ppm 280-315 306-309 150-164 159-164 CO2, % 10.1 10.1 7.4-7.7 7.1-7.3 HC, ppm 12-23 24-29 18-27 39-46 CO, ppm 253-320 213-216 107-135 170-172 Therm. Eff., % BMEP, psig 38.1 36.0 31.6 29.7 95.5-97.5 97.4 73-76 75.5 The data presented in Figs. 2 and 3 show that NOx conversion increased with increasing ethanol delivery (C1:NOx ratio) for all 4 Because the catalyst performance improved with the sequence of experimentation, we had difficulty making detailed assessments of SCR performance with fuel type or reductant grade. However, the Oct. 17 data presented in Fig. 2 shows no observable difference in NOx conversion performance when using either fuel-grade (untreated) or reagent-grade ethanol as the reducing species. Likewise, the Oct. 16 and 17 results shown in Fig. 3 indicate that NOx conversion was not greatly affected when running the engine on E-diesel and using distilled ethanol as the reducing species. The Oct. 16 results clearly demonstrate the utility of using ethanol as a fuel-borne reductant to reduce NOx emissions. The NOx conversion was over 90% for a C1:NOx ratio of ~5 at 21000/h and near 85% for a C1:NOx ratio of 7 at 57000/h. 100 90 NOx Conversion (%) 80 70 FUEL PENALTY For the experiments represented in Figs. 3 and 4, the C1:NOx ratio can also be expressed as a fuel penalty. Figure 4 gives calculated fuel penalty on an energy basis as a function of the C1:NOx ratio for the two engine conditions (Table 2.). It was assumed the ethanol reductant that is distilled from the fuel contains 63% of the energy on a weight basis compared to ECD1 fuel. 100 90 NOx Conversion (%) 80 70 60 50 40 Oct. 8: ECD1 fuel, Reductant = FG ethanol (untreated)* 30 Oct. 8: ECD1 fuel, Reductant = FG ethanol (untreated) 20 Oct. 15: ECD1 fuel, Reductant = FG ethanol (untreated) 10 Oct. 16: E-diesel fuel, Reductant = FG ethanol (distilled) Oct. 17: ECD1 fuel, Reductant = FG ethanol (untreated) 0 0 2 4 6 8 10 12 14 16 C1(2X ethanol):NOx Ratio Fig 3. NOx conversion as a function of C1:NOx ratio for the high speed engine operating condition (2225 RPM, 182 ft-lb, ~57000/h space velocity. *Note, for this condition SV 26500/h. 3.5 3.0 Fuel Penalty, Energy Basis (%) operating conditions. These figures also show that the level of NOx conversion increased with the progression of experimentation up to Oct 16 for both operating conditions. This effect did not appear to be influenced by either fuel or reductant type. For the low-speed condition (Fig. 2) the maximum level of NOx conversion (associated with a C1:NOx ratio of ~4) increased from ~70% (Oct. 7-8) to approximately 95% for the runs on Oct. 16 and 17. The higher SV condition presented in Fig 3 shows that the optimum C1:NOx ratio increased to ~7.5 and the conversion efficiency increased from 74% (on Oct. 8) to around 85% for the Oct. 16 runs. This behavior is a strong indication that the catalysts had not been fully aged prior to evaluation. But, closeness of the data on Oct 16 and 17 suggests that catalyst aging was nearing completion on Oct. 16. The cumulative engine running time put on the catalyst prior to the Oct 16 runs was estimated to be around 32 hours. The degreening period that was used was based on input from catalyst chemists experienced with these catalyst systems. However, the exceptionally low fuel sulfur level of the ECD-1 fuel (<15 ppm) likely necessitated a longer aging period to ensure complete sulfate accumulation on the silver catalyst sites. SV ~ 21,000/h 2.5 2.0 SV ~ 57,000/h 1.5 1.0 0.5 60 50 0.0 Oct. 7-8: ECD1 fuel, Reductant = FG ethanol (untreated)* Oct. 8-9: ECD1 fuel, Reductant = FG ethanol (untreated) Oct. 10: ECD1 fuel, Reductant = FG ethanol (untreated) Oct. 10: ECD1 fuel, Reductant = FG ethanol (distilled) Oct. 15: ECD1 fuel, Reductant = FG ethanol (distilled) Oct. 16: E-diesel fuel, Reductant = FG ethanol (distilled) Oct. 17: ECD1 fuel, Reductant = FG ethanol (untreated) Oct. 17: ECD1 fuel, Reductant = reagent grade ethanol 40 30 20 10 0 0 2 4 6 8 10 0.0 2.0 4.0 6.0 C1/NOx Ratio 8.0 10.0 12.0 Fig 4. Fuel penalty versus C1:NOx ratio for the two main engine conditions. HYDROCARBON SLIP MEASUREMENTS 12 C1(2X ethanol):NOx Ratio Fig 2. NOx conversion as a function of C1:NOx ratio for the low speed engine operating condition (1115 RPM, 230 ft-lb, ~21000/h space velocity. *Note, for this condition SV 10500/h. As shown in Table 2 the engine-out hydrocarbon emissions were low (< 50 ppm) for both operating conditions though there was a slight increase associated with using E-diesel as the fuel. These levels decreased further through the catalyst (when no reductant was added), thus indicating that some oxidation was taking place. However, the hydrocarbon emissions downstream of the catalyst increased with the addition of ethanol into the exhaust as depicted in Figs 5 and 6. (Note that the test conditions presented in Figs 5 and 6 correspond to those in Figs 2 and 3 respectively.) 5 800 800 As with the data presented in Figs 2 and 5, the increase in slip associated with succession of experimentation prevents detailed assessment of HC slip. However, on Oct. 17 the HC slip was exceptionally low for the runs utilizing high purity reagent-grade ethanol as the reductant. This suggests that the impurities present in the fuel-grade ethanol may contribute substantially to HC slip (even if they do not influence NOx conversion). 600 600 TEMPERATURE EVALUATION 400 400 200 200 1200 1200 1000 C1(2X ethanol):NOx ~6.3 1000 HC Slip (ppm) C1(2X ethanol):NOx ~2.8 0 200 0 400 350 300 250 The conversion efficiency of this particular ethanol-SCR system is thought to be near optimum for catalyst temperatures near 400oC. However, during actual engine operation, the exhaust temperatures can be much lower, particularly during idling and low-load operation. Therefore we felt some measure of the low temperature performance of ethanol-SCR was needed. The results of this evaluation are shown in Fig. 7. Catalyst Core Temperature (oC) 100 Fig 5. HC slip as a function of C1:NOx ratio for SV ~ 21000/h. C1(2X ethanol):NOx ~6.3 250 Oct. 7-8: ECD1 fuel, Reductant = FG ethanol (untreated)* Oct. 8-9: ECD1 fuel, Reductant = FG ethanol (untreated) Oct. 10: ECD1 fuel, Reductant = FG ethanol (untreated) Oct. 10: ECD1 fuel, Reductant = FG ethanol (distilled) Oct. 15: ECD1 fuel, Reductant = FG ethanol (distilled) Oct. 16: E-diesel fuel, Reductant = FG ethanol (distilled) Oct. 17: ECD1 fuel, Reductant = FG ethanol (untreated) Oct. 17: ECD1 fuel, Reductant = reagent grade ethanol 200 HC Slip (ppm) NOx Conversion (%) 80 150 C1(2X ethanol):NOx ~2.8 60 40 20 0 200 100 250 300 350 Catalyst Core Temperature (oC) 400 Fig 7. NOx conversion as a function of temperature. 50 0 0 2 4 6 8 10 12 C1(2X ethanol):NOx Ratio Fig 6. HC slip as a function of C1:NOx ratio for SV ~57000/h. These figures also show that HC slip increased with succeeding experiments up to the runs on Oct 16. This further supports the assessment that the catalysts were insufficiently aged at the end of the de-greening period. These catalyst systems are believed to behave more like an oxidation catalyst in the green state; i.e. they oxidize HC species present in the exhaust. However, recent studies have indicated that as the silver sites become sulfated, these catalysts become more selective to NOx conversion, and hence their ability to oxidize hydrocarbons is reduced as the sulfate level increases (9). During each test condition the HC emissions increase in an approximate linear manner with the flow rate of ethanol. As expected the slip was higher for the high-speed condition than the low-speed condition since the residence time is much lower. Assuming straight-line behavior, then for a C1:NOx ratio of 6, the HC slip is ~170 ppm for the high-speed condition versus ~150 ppm for the low-speed condition. Throughout this test, the engine was run at a fixed speed of 1115 RPM. The load was initially set to 230 ft-lbs to achieve a catalyst temperature between 350 and 400oC. Next, the load was gradually reduced to achieve temperatures approximating 350, 300, and 250oC. (Note that the SV dropped from 21000/h to 17000/h as the catalyst core approached 250oC.) The C1:NOx ratio was maintained near 6.3 and 2.8 for each temperature setting. The NOx conversion associated with these temperatures for both C1:NOx ratios is shown in Fig. 6. The NOx conversion was observed to drop sharply with decreasing catalyst temperature for the two C1:NOx ratios studied. However, the two curves appear to converge near a value of ~25% as the catalyst temperature approaches 250oC. Without additional measurements it is unclear whether this value represents a lower bound. The hydrocarbon slip corresponding with the conditions presented in Fig. 7 are shown in Fig. 8. In this figure, the HC slip increases with decreasing catalyst temperature for both conditions. However the rise is much more dramatic for C1:NOx ratio of 6.3 versus 2.8. In fact the HC slip for the low C1:NOx ratio only begins to rise sharply when the catalyst core temperature is lowered to ~250oC. This suggests that the additional ethanol slips past the catalyst. 6 C1:NOx ~6.3 300 1000 250 800 200 6 NOx @ 21000/h NOx @ 57000/h 600 400 400 200 200 350 300 4 150 3 100 250 2 50 1 0 0 200 0 0 0 2 4 6 8 C1(2X ethanol):NOx Ratio Catalyst Core Temperature (oC) Fig 8. Hydrocarbon slip as a function of temperature. 5 N2O @ 57000/h 10 12 Fig 10. N2O emissions as a function of space velocity and C1:NOx ratio. FTIR RESULTS AND BAG ANALYSIS FTIR Results A Nicolet Magna-IR 560 FTIR spectrometer equipped with a REGA 700S sampling system was used to speciate NOx, N2O, ammonia, and acetaldehyde emissions from the catalyst exit as a function of SV and C1:NOx ratio. The results for ammonia, N2O, and acetaldehyde and their corresponding NOx emissions are shown in Figs. 9, 10, and 11 respectively. The N2O emissions were also observed to increase with increasing C1:NOx ratio (see Fig. 10); the concentrations of N2O, however, are quite low (<10 ppm). This represents an important finding since early HC-SCR catalyst formulations emitted large concentrations of N2O during NOx conversion. Like the ammonia results, the N2O emissions were higher for the low-speed condition indicating that residence time is critical for N2O formation. The kinetics of N2O formation and its role in NOx reduction are not well understood. 300 250 NOx Level (ppm) 70 NOx @ 21000/h NOx @ 57000/h NH3 @ 21000/h NH3 @ 57000/h 60 50 200 40 150 30 100 20 50 10 0 0 0 2 4 6 8 10 NOx @ 21000/h NOx @ 57000/h Acet @ 21000/h Acet @ 57000/h 200 50 40 150 30 100 20 50 10 0 Ammonia Level (ppm) 300 60 250 NOx Level (ppm) As shown in Fig. 9, ammonia was detected by the FTIR spectrometer and was observed to increase with increasing C1:NOx ratio. Interestingly, the ammonia emissions were significantly higher for the low-speed condition than for the highspeed condition. This is an important finding since ammonia formation and its subsequent use to further aid in NOx reduction is one of the pathways that is believed to occur for NOx reduction by silver-loaded alumina catalysts (3). The lower residence time allows more ammonia to be formed, which subsequently may be important for the conversion of NOx to N2. 12 C1(2X ethanol):NOx Ratio Fig 9. Ammonia emissions as a function of space velocity and C1:NOx ratio. Acetaldehyde Level (ppm) HC Slip (ppm) 600 400 7 N2O @ 21000/h C1:NOx ~2.8 800 NOx Level (ppm) 1000 1200 N2O Level (ppm) 1200 0 0 2 4 6 8 10 12 C1(2X ethanol):NOx Ratio Fig 11. Acetaldehyde emissions as a function of space velocity and C1:NOx ratio. The emissions of acetaldehyde (shown in Fig. 11) were observed to increase with increasing C1:NOx ratio and reached appreciable levels for the high-speed setting at moderate C1:NOx ratios. Acetaldehyde emissions are formed directly from the oxidation of ethanol (via catalysis) and therefore would be expected to increase proportionally with ethanol concentration. The much higher acetaldehyde emissions associated with the high-speed condition suggests that 1) most if not all the ethanol is converted into acetaldehyde over the catalyst, and 2) the subsequent reactions utilizing acetaldehyde to reduce NOx proceed less rapidly than does acetaldehyde formation. These results agree with the bench studies performed by Noto et al. (5) which showed that most of the ethanol is converted to acetaldehyde for these catalyst types. 7 Bag Analysis The bag samples were collected using the miro-diluter highlighted in the Fig. 1 schematic. CG-MS analysis revealed that detectable levels of nitrophenol were formed during the ethanol-SCR process. Although we were not able to accurately quantify nitrophenol emissions, we are able to note that its concentration increased with ethanol delivery and space velocity. CONCLUSIONS A full-scale ethanol-SCR system demonstrated excellent reduction of NOx emissions from a heavy-duty diesel engine for exhaust and catalyst temperatures of 350-400oC. The NOx conversion reached 95% to 85% for space velocities of 21000/h and 57000/h respectively. In addition, the C1:NOx ratios used to achieve these efficiencies were considered to be reasonable; approaching a value of 4 for 21000/h condition and around 7 for the 57000 condition. This represents energy based fuel penalties of approximately 1.5 and 1.8 % respectively. The NOx conversion efficiency, however, depended greatly upon the catalyst core temperature. When the core temperature was lowered from ~360oC to ~250oC, the conversion efficiencies fell to near 25% for both speed conditions. Because the catalysts were not thoroughly aged prior to testing, the NOx conversion improved with progression of experimentation and thus interfered with data interpretation. The results suggest that the de-greening period needed to be extended to over 35 hours when using ECD-1 (and probably any low sulfur fuel) as the fuel type. The increase in NOx conversion with succeeding experimentation was accompanied by an increase in HC slip which further supports the belief that the accumulation of sulfate on the silver catalyst sites actually enhances the NOx conversion for these particular SCR systems. This investigation also showed that the ethanol was rapidly converted to acetaldehyde by the silver-loaded alumina catalyst, which subsequently slipped past the catalyst at appreciable levels when the space velocity was increased to 57000/h. Ammonia and N2O were also detected in the exhaust. The concentrations for both these compounds were observed to be higher for the low space velocity condition. However, the concentration of N2O did not exceed 10 ppm, which is considered to be exceptionally low. ACKNOWLEDGMENTS This work was supported by the Department of Energy Office of Freedom CAR & Vehicle Technologies. Cummins Engine Company, Inc. provided both the test engine and auxiliary components. The authors would also like to acknowledge Dave Loos and Norm Marek of the Illinois Department of Commerce and Community Affairs for their efforts to coordinate the delivery of the splash-blended E-diesel and other fuel components. Finally we would like to thank Glenn Kenreck of GE Betz for performing a blending agent compatibility study and Jeff Chambers (of ORNL) for assistance with engine setup. REFERENCES 1. 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