Ideas and innovations Seeding Modification separates seed and fertiliser K ondinin Group member Murray Dodd has modified his new Alfarm A550 air seeder to separate seed and fertiliser when sowing crops on his property at Kalannie, Western Australia. Murray and his wife Therese crop about 2000 hectares of Eradu noodle wheat, 1000ha of lupins and 300ha barley on their sandy loam property. In early 1995 Murray decided to buy an Alfarm A550 air seeder (see Machinery Evaluation, Farming Ahead No 52, page 23) and matching 13.7 metre, 75 tine A 5 3 0 cultivator to meet his cropping commitments. Although the seeder had a simple belt conveyer, micrometer type metering system and non pressurised seed and fertiliser bins, the unit was not fitted with a double shoot system. Murray immediately set about modifying the unit to separate seed and fertiliser. Modification He fixed a divider plate in the mixing chamber and venturi to keep the seed and fertiliser separated after they left the flat belt conveyer. A second long divider plate was fitted to the primary distribution duct to separate seed and fertiliser as the material is carried to the primary head. Murray ordered his air seeder with a 17 outlet primary head but he has added an eight outlet plate to the existing nine hole plate on the cultivator drawbar. He has also replaced the original Alfarm secondary heads with 17 plastic John Shearer secondary heads. The modification of the venturi and primary Murray Dodd has fitted a dividing plate to the primary distribution duct on his Alfarm A550 air seeder. duct allowed grain to be delivered from the seed compartment through the mixing c h a m b e r, primary duct, primary head, transition piece hoses and through eight metal tubes to eight secondary heads. Fertiliser was separately delivered from the fertiliser compartment through nine steel tubes to the nine secondary heads. The Shearer secondary heads allowed Murray to close off outlets where required and distribute seed and fertiliser independently and evenly across the width of the bar. The modifications cost Murray about $2500 which included replacement hoses and 15 hours of work. Gas burner The original diesel motor driven fan was also replaced with a higher speed Harmon fan, driven by a hydra motor. Murray said the new fan and drive has cost about $2500 but he is expecting a significant increase in air volume. The original venturi inspection cover was removed and replaced with two perspex covers, retained by simple release spring clips. These made it easier to visually check the venture and mixing chamber for blockages. Although the perspex can become covered in dust and lose its transparency, Murray said it is has allowed faster access to the mixing chamber. - Alan Montgomery Murray mounted a gas burner beside the fan air intake to eliminate moisture in the fertiliser hoses but the hoses failed after only 1200ha of work. Murray believes the heat from the burner may have contributed to the failure of the original non-reinforced hoses. He has replaced them with reinforced rubber hoses which have been interwoven to reduce bending when the rig is turned. Tubes and hoses on the right carry grain and those on the left carry fertiliser. FARMING AHEAD No. 53 -May 1996 Easy to operate clips hold perspex inspection covers over the mixing chamber and venturi. The transition piece has two nine hole connecting plates with interwoven reinforced rubber hoses. 15
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