Journal of Scientific & Industrial Research Vol. 74, April 2015, pp. 236-244 Controlling Barium Sulphate scale deposition problems in an Unbleached Kraft Paper Mill B Sithole1*, M Doucette2 and R Fiolet3 *1 Forestry and Forest Products Research Centre, Discipline of Chemical Engineering, University of KwaZulu-Natal, CSIR, Durban, South Africa 2 Tolko Manitoba Kraft Papers, The Pas, Manitoba, R9A 1L4, Canada 3 Ashland Hercules Water Technologies, The Pas, Manitoba, R9A 1L4, Canada Received 27 July 2012; revised 19 November 2013; accepted 30 December 2014 Troubleshooting of scale deposits and defects in paper samples showed that the problem was caused by barium sulphate and calcium sulphate scales. However, it was ascertained that barium sulphate was more of a concern than calcium sulphate as it is more tenacious than the calcium sulphate scale. A study of the inputs of the scale components found that the major inputs of barium into the mill system were the wood chips and bark contamination. The major inputs of the sulphate component of the scale were sulphuric acid used for pH control and alum used for rosin sizing.Evaluation of several options for mitigating the scale deposition problem showed that bark removal and continuous application of a scale inhibitor comprised of phosphates/phosphonates and polyacrylates were effective in reducing and controlling the scale deposit problems. Institution of these measures led to a cleaner paper machine that required far fewer boil outs than before. In addition, productivity improved and the fisheye defects disappeared.A rapid method was developed for on-site estimation of barium levels in mill process samples. The data were used to adjust the dosage of the scale inhibitor to ensure optimum effectiveness of the programme. Keywords: Scale, barium sulphate, deposition, alum, pH control, scale inhibitors Introduction The formation of sulphate scale deposits is a huge problem in pulp and papermaking operations. The deposits cause a number of problems such as deposition on mill equipment that can grow to cause process upset and blockages of pipes1-3. A particularly problematic issue if the breakage of scale deposits to small particles that appear as fish eyes in the final pulp and paper product. Several approaches can be used to avoid or reduce scale deposition4,5, but barium sulphate forms tenacious deposits that are very difficult to remove and control6,7.Several years ago we worked with a sack kraft mill to help in its conversion from rosin to alkyl ketene dimer (AKD) sizing in order to improve runnability. AKD is normally used in alkaline paper and board grades, but not in sack kraft grades. The conversion was a success and the mill was the first sack kraft mill in North America to achieve this. However, about two years later the mill reverted back to rosin sizing due to the much higher cost of AKD versus rosin size. A few months after the —————— *Author for correspondence E-mail:[email protected] switch the mill experienced serious deposits that accrued on the Uhle box strips, headbox, LEXAN® sheets, header, and slice. To cope with these problems, the mill washed the headbox with caustic and chelant every month, and even more frequently at times, in contrast to a competitor mill where the headbox required only two washes per year. With time, the boil outs were ineffective in removing the deposits. In addition, a substantial portion of the paper produced was off-grade and plagued with fisheye defects.The deposits were very expensive for the mill and, at the time, cost upwards of $0.5 million per annum for boil outs, downtime for cleaning, replacement of LEXAN sheets, reduced efficiency due to poor machine and winder runnability, and off-grade and/or rejected paper products.A team was set-up and called in to troubleshoot the deposition problem and help recommend methods to eliminate or control the problem. We found that the deposit was an inorganic scale comprised largely of barium sulphate and some calcium sulphate. The inputs of the principal scale components were determined and used to develop methods to reduce or control the scale deposits. SITHOLE et al: CONTROLLING BaSO4 SCALE DEPOSITION PROBLEMS The options that were investigated included pre-acidification of pulp before washing and use of scale control additives. Advantages of preacidification include: improved pH control in the wet end – a stable wet end pH requires less acid and makes correction at the silo easier; less “shock” at the alum addition point resulting in reduced deposition, i.e., reduced formation of aluminum hydroxide and barium sulphate; soluble “anionic trash” is partially neutralized by pH reduction – leads to lower cationic demand; greater alum/size efficiency also results in reduced sulphate and barium from wood other benefits - reduced size demand, improved refining and strength Observations at the mill A quick review of mill operations showed the use of fresher chips than prior to the deposition problems and visible bark in the chip supply. The chip supply had changed from a well known furnish from the nearby saw mill to unknown furnish of variable quality from places distant from the mill. In addition, brownstock washing at the mill was much poorer than at a competitor mill. Additives used at the mill were wet-strength resin, biocide, oil-based defoamer, cationic wet-end and surface starches, calcium carbonate, rosin size, alum, retention and drainage aids. Experimental Approach Analysis of deposits The approach developed was to conduct thorough analyses of the deposits to determine their composition and to trace the source or cause(s) of the deposition. Initially, deposit samples from the headbox and LEXAN sheets were collected and analysed for comparison with the deposits on the paper samples. Later, samples of deposits as well as pulps were collected at several unit operations across the mill to profile the levels of major components suspected to be the cause of the deposits.The samples were freeze-dried and portions were analysed for ash content. The samples and ashes were then characterized by Fourier transform infra-red spectroscopy (FTIR) to obtain information about the functional groups present and by energy dispersive spectroscopy (EDS) to obtain information about the inorganic elements present. Portions of the dried deposits were extracted sequentially with acetone and 237 chloroform and the extracts were dried and characterized by FTIR and gas chromatography to determine the organic components extracted from the deposits. The metals present were determined by inductively coupled plasma - optical emission spectrometry (Perkin Elmer, USA). The analytical techniques used have been described before8. Profile of scale components along the fibre line This study was conducted to ascertain which unit operations were more prone to deposition than others. Time-sequenced samples were collected along the fibre line and analysed for ash, barium, calcium and sulphur content. The sampling points were weak black liquor tank (WBL), raw stock chest (RSC), decker stock (DS), before the twin roll press (BTRP), after the twin roll press (ATRP), after the high consistency refiner (AHCR), machine chest outlet (MCO), white water silo (WWS), and headbox (HB). The samples were collected over 2 weeks except for the headbox sample where the samples were collected over three weeks. Pre-acidification of stock before washing Laboratory experiments were conducted to assess the best conditions for pre-acidification of pulp stock with acid to remove metal ions from the pulp. The pre-acidification studies were conducted as follows: Pulp stock was vacuum filtered. The pH of the filtrates was measured and the filtrates were then analysed for metals. Distilled water (same volume as the filtrate) was added to the filtered pad, and the pH was adjusted from an initial value of 9.5 to lower values using nitric acid. The mixture was shaken for 5 minutes and filtered as before. The process was repeated down to pH 3. All the filtrates were analysed for metal content.A control study was done by washing with distilled water with no pH adjustment. Pulp stock was vacuum filtered. The volume of the filtrate was measured and the filtrate was analysed for metals. Distilled water (same volume as filtrate) was added to pad with no pH adjustment. The sample was processed as described before. The washing was repeated twice with fresh water volumes. All the filtrates were analysed for metal content.The pulps used in these studies were Raw Stock, Brown Stock, and Machine Chest Outlet. Spot test for measuring barium levels in process samples Normally, the concentration of barium ions in process samples can be determined with accuracy by spectrometric methods. However, the methods are not 238 J SCI IND RES VOL 74 APRIL 2015 rapid enough to yield data that could be used to make important mill decisions. Consequently, a spot test for rapid “ball park” estimation of barium levels was developed and instituted at the mill. The method was based on formation of barium sulphate precipitates by mixing barium laden samples with a copper sulphate solution. Since copper sulphate is soluble in water, it can react with barium ion to produce a thick white precipitate of barium sulfate: Ba2+(aq) + CuSO4 → BaSO4(s) + Cu2+(aq) A 1,000 ppm stock solution of BaCl2 was prepared in distilled water and then diluted to make solutions that contained 0.5 to 10 ppm of barium. 5 mL of each solution were mixed with 1 mL of a 50,000 ppm aqueous copper sulphate solution in clear conical polypropylene centrifuge tubes. The samples were mixed well, allowed to sit for 5 minutes, and then centrifuged on a portable microcentrifuge for 1 minute. The tubes were placed on a rack to be used as standards for estimating the concentrations of precipitated barium in process samples. To measure barium levels in process samples, 100 g of pulp stock were acidified to pH 3 with nitric acid and then centrifuged to collect the aqueous fraction. 5 mL of the liquid were reacted with copper sulphate as previously described in the preparation of barium sulphate precipitate standards. The concentration of barium in the precipitates was estimated by visual comparison of the amount of precipitates with the known barium sulphate precipitates in the calibration standards. mills that use rosin size are plagued with aluminium and/or calcium rosinate deposits9-11, but this was not the case in this mill. Analysis of the extracts by gas chromatography showed the presence of wood resin but no rosin size or oils. These results indicated that the deposition problem, and consequently, the fisheye defects in the paper, were not attributable to wood pitch or improperly retained rosin size. Indeed, the extractives content of one problem paper, grade A, were lower than those of the good paper. Ash content and characterization of the ash The ash contents were very high (58 -88%) in the headbox and LEXAN sheet deposit samples but low (less than 1%) in the final paper samples. Analysis of the ash by energy dispersive spectroscopy (EDS) showed that the major elements present in the headbox and LEXAN sheet deposit samples were aluminum, barium, calcium and sulphur, whereas the fisheye defects showed the presence of mainly barium and sulphur. The presence of aluminium is not unexpected since alum was used for rosin sizing at the mill, but the presence of barium, calcium and sulphur were of concern. Further analysis of the ash samples by FTIR showed that they contained large amounts of barium sulphate and calcium sulphate. Calcium sulphate was dominant in the whitewater silo ash whereas barium sulphate was more dominant in the LEXAN sheet and headbox deposit. Typical FTIR spectra are shown in Figure 1. From these results it Results and Discussions The headbox deposit samples were brown flaky material, whereas the deposits in the paper products were in the form of fisheye defects. The deposits on mill equipment were tenacious and not easily removed by scraping with a metal blade. However, deposits in the whitewater silo were easier to scrape off than the ones in the headbox. Solvent extracts Acetone extractives provide quantitative data on the presence of wood resin, hydrocarbon oils, defoamer oils or rosin size whereas chloroform extractives are used to quantify the concentrations of multivalent metal soaps of wood resin and/or rosin size. The values of the acetone solvent extracts were low and were within the normal range for unbleached kraft papers. The chloroform extracts were negligible indicating that there was no deposition of metal soaps. At times, Fig. 1—FTIR spectrum of headbox ash samples showed a good match with barium sulphate. SITHOLE et al: CONTROLLING BaSO4 SCALE DEPOSITION PROBLEMS 239 was deduced that the fisheye defects in the final products were caused by contamination from barium sulphate deposited on the LEXAN sheets. The high levels of ash (barium sulphate) in the headbox samples resulted in deposition of barium sulphate on the LEXAN sheets. the northeast USA where barium is present in water and soil13. Later reports show that the problem was endemic in the kraft bleach plant, especially since the advent of chlorine dioxide bleaching. The information from the literature is further summarized in the sections that follow. Profile of scale components along the fibre line Barium sulphate is a recalcitrant scale The results for the profiles of scale components along the fibre line are showed that large amounts of ash, and therefore by inference, scale deposition, occurred in the whitewater silo and on the headbox. Indeed, the data for barium and sulphate concentrations confirm this, as cab ne seen in Figure 2. The trend observed here agrees with literature reports of barium profiles across a kraft mill4.Although the scale deposits contained barium sulphate and calcium sulphate, it was deduced that it was worthwhile to focus more on barium sulphate scale than on calcium sulphate scale since the barium sulphate scale is more tenacious and difficult to control and remove than the calcium sulphate scale. Finding a solution or solutions to the scale deposition problem required an understanding of barium sulphate scale precipitation: its mechanism, inputs of scale components, and scale removal strategies. Review of barium sulphate scaling A review of the literature on barium sulphate scaling in pulp and papermaking reveals that the problem can be widespread12. A paper from the 70s states that the deposition problem was not isolated to any particular geographic region, since it had been observed in groundwood mills, fine paper machines and unbleached kraft machines in all parts of the USA4. However, a paper from the 90s states that the problems occurred in the southeast and some parts of Fig. 2—Profile of barium content along the fibre line (values magnified x100). Of the three mineral scales encountered in pulp and papermaking, (barium sulphate, calcium oxalate, and calcium carbonate), barium sulphate is the most difficult to remove and the most difficult to prevent2,14. Barium sulphate scale is difficult to remove because sulphate is a strong acid and the dianion sulphate persists to a pH below 2. It requires a strong acid to remove and the acid used cannot be sulphuric acid. Preventing barium sulphate scales is difficult because the sulphate ion is ubiquitous in a pulp mill and in the bleach plant. A solubility product plot of barium sulphate shows that at any realistic sulphate level, the solubility product of barium sulphate is exceeded in the presence of very small amounts of barium ions4. Barium sulphate deposition correlates with pulp lignin content. On two parallel lines, the deposition is more likely on lower kappa number pulp4. This is probably because higher kappa pulps have more lignin content that acts as a dispersant15 or inhibitor for the barium sulphate scale. Decreasing of the pH of the stock towards the headbox further favours barium sulphate deposition, and the loss of the lignin (a natural dispersant) due to precipitation of dissolved lignins may be a contributing factor. Location and description Barium sulphate scale builds up on headboxes, flow spreaders, or organ tubes of the paper machine6. It is also found on table-roll deflectors, in stock lines, rectifier rolls, vacuum boxes, etc. The scale varies in colour and consistency, being very thin, bright, and rough in the headboxes and greyish-to-brown, hard and pasty in other areas. Two types of barium sulphate crystals occur that differ in size and shape: rhombic and dendritic. It has been observed that scaling is most severe at points of cascades and pressure drops, but both forms of crystals have been found in whitewater systems of kraft paper machines16. Barium sulphate has been blamed for corrosion problems, since under-deposit corrosion can result from the presence of sulphate-reducing bacteria which exist in the anaerobic space beneath the 240 J SCI IND RES VOL 74 APRIL 2015 deposit13. The by-products of theses microbes can be highly corrosive to even stainless steel, causing pitting of the metal and a roughened surface that will be more prone to deposition after cleaning. Mechanism Scaling tendency (also called the saturation level or ratio) is a measure of a system’s level of saturation with respect to a solid phase chemical species, in this case BaSO4. The scaling tendency indicates the magnitude of the driving force for the dissolved species to precipitate. The value is thermodynamically based on the ratio of the ion activity product to the equilibrium constant of the precipitation reaction or the solubility product17-18. 2- [Ba 2 ][SO 4 ] Saturation index log 10 K sp BaSO 4 where [Ba2+] is the concentration of free barium ions, [SO42-] is the concentration of free sulphate ions, and KspBaSO4 is the solubility product for the precipitation reaction. Remember that the activity of the solid species, the product in the chemical reaction equation, is equal to one. All of the quantities on the right side of the above equation are adjusted for pH, temperature and ionic strength. Calculation and use of the saturation index, and generation of the data from which it is derived, are best done by computational programmes such as WaterCycle, ScaleChem; Avista Advisor19. When the scaling tendency = 0, barium sulphate is in equilibrium with the solution. When it is < 0, the mineral is undersaturated, and when it is > 0, the mineral is oversaturated. Therefore, when the solubility product is exceeded, the scaling tendency is high as the reaction is in a supersaturation state. Consequently, deposition of BaSO4 occurs. The Ksp for barium sulphate is 1.0810-10 at 20°C and 1.9810-10 at 25°C. To put this solubility product into perspective, barium sulphate scale is 25 times less soluble than calcium carbonate and 35 times less soluble than calcium oxalate7.Deposition can also occur via nucleation, whereby clusters of barium and sulfate reach “critical nucleus size” and crystals begin to form and build. This mechanism is initiated by BaSO4 seed crystals, shocks to the system (pH, thermal, shear), or over time (induction time).The deposition can also occur via crystal growth: after nucleation, BaSO4 crystals build with new molecules being added to the crystal surface or face of the initial crystals. Inputs of barium and sulphate ions Inputs of barium and sulphate into the pulp and papermaking process in an unbleached kraft paper mill include: acidification of pulp with sulphuric acid, carryover from Na2S in white liquor that has been oxidised to sulphate, use of alum for rosin sizing, and naturally occurring barium in wood and/or water. Softwoods contain 8-15 ppm barium whereas hardwoods contain 5 times more barium20-21. The barium levels are higher in bark than in wood. It has been reported that 50% of the barium in wood input into the digester remains bound to carboxylic acids on the pulp5. The amount of barium on pulp is little affected by brownstock washing. The sulphate anion is the net product of bound sulphur on brown stock pulp, sulphur carryover from brownstock washing, sulphuric acid used for pH adjustment, and alum used for rosin sizing. Formation of barium sulphate scale Very minute amounts of barium can eventually result in large quantities of deposit13. The surface of the deposit is very rough, and as a result traps fibres and other filler particles. Eventually the deposit grows large enough to plug consistency regulators and cause flow control problems, such as consistency and basis weight variations. With more time, the deposits will grow large enough and become unstable, and pieces will break off and cause sheet spots, breaks and press end crushing. Precipitation or agglomeration of BaSO4 into small or large particles dictates how they will partition between fibres and filtrates. This is dependent on the type of washing equipment used. For example, in drum filters, barium sulphate particles that are less than 50 µm are retained in the pulp, whereas particles that are <1 µm exit with the filtrate5. pH is a critical parameter in BaSO4 scale formation. Deposition occurs most at points of pH shock, such as white water dilution and acid/alum addition points. In general, the pH of pulp stock decreases from 10 at the brownstock washers to 5 at the paper machine headbox. The pH directly affects the distribution in solution of the various ions and complexes in the system. Solutions to barium sulphate scale In general, solutions to barium scale deposition can be divided into four groups: Reduce the input of scale materials Where possible, switching from hardwoods to softwoods will help greatly in minimizing barium 241 SITHOLE et al: CONTROLLING BaSO4 SCALE DEPOSITION PROBLEMS scale deposition. Good debarking is a good way to reduce input of barium into the system because trace metals are at significantly higher concentrations in the bark than they are in clean wood. Good brownstock washing will reduce inputs of barium. Inputs of sulphate can be reduced by good white liquor clarification and avoiding the use of sulphuric acid for acidification of pulp. Reid et al.5 concluded that mills using wood species with high levels of barium (>25 ppm on pulp) can only minimize BaSO4 scaling, whereas it is possible to avoid BaSO4 scaling in mills that have pulps with lower barium concentrations. Remove built-up scale This is usually accomplished by mechanical means, viz, hydroblasting and/or by chemical means that can be boil-outs with chelants or acid washes. Hydroblasting entails fracturing and removing deposits with intense, high-pressure, water washing. It is “akin to trying to demolish a concrete highway with a pressure washer”2. Prevent scale build-up Equipment made of stainless steel and Teflon equipment is less prone to scale deposition. Process changes, such as the addition of dispersants and crystal modifiers to prevent crystal growth, can also be used to prevent the build-up of barium sulphate scale. Replace alum with polyaluminium chloride (PAC) No sulphate ions are introduced by PAC but the kraft (sulphate) pulping process introduces such a high sulphate ion concentration, that the sulfate reduction from replacing alum may have a negligible effect on BaSO4 deposition. In addition, PAC introduces chloride ion into the white water system that may be of some concern in chlorine stress corrosion cracking. However, the chloride ion concentration introduced with PAC would probably be too low to cause a problem. Solutions implemented at the mill The solutions listed in the previous section were explored to ascertain which ones could best be implemented at the mill. The first obvious one was bark content in the chips. The mill improved their chip screening procedures and emphasized the importance of minimal bark content in the chips in discussions with their chip suppliers.An initial profile was conducted to ascertain which mill unit operations were most prone to the accumulation of barium sulphate scale. This was done by determining the ash content of pulps from 3 unit operations, viz., the stock tower, the machine chest and the headbox. Four samples were collected over four days and analysed for ash content as an indicator of barium scale content. The results demonstrated that the ash content increased along the fibre line to the paper machine and was highest at the headbox where the ash content was 7-10 times higher than at the stock tower and machine chest unit operations. Quantitative measurements of the actual concentrations of barium and sulphate in a thick stock sample, white water silo sample, and a headbox sample and their calculated scaling tendencies clearly indicated that the scaling tendency was very high, as illustrated in Table 1. At the time of investigation, the mill was practicing Option 2 in the form of caustic washes of the headbox every month (sooner in some instances). However, this was an expensive option; in a competitor’s mill, such washes were necessary only twice a year. The barium sulphate scale had been increasing steadily over the previous six months. To make matters worse, the last boil-out had not been 100% effective in removing the barium sulphate scale. These results indicated that a solution to the scale problem required institution of measures to reduce the inputs of barium sulphate scale components to the headbox in order to reduce the frequency of boil-out episodes, or methods to facilitate and improve the efficiency of the boil-outs.Option 4, replacement of alum with PAC, was examined. Some facts to consider about PAC are: its basicity is important; higher basicity translates to a more stable and less corrosive additive; PAC consists of cationic aluminum polymers, which cause coagulation, but it is important not to overfeed. The performance of PAC is affected by system temperature, pH, alkalinity, system charge demand, feed point (mixing energy and time), and dilution water. It is important to not pre-dilute prior to addition and the dilution should be at the injection point only. The pros for using PAC include: Has a higher charge and can be more effective than alum Table 1—Concentrations of barium and sulphate moieties in pulp samples and their effect on scaling tendency (temperature corrected to 50oC). Sample Thick stock Headbox Whitewater silo Barium, ppm Sulphate, ppm Scaling tendency 0.82 0.52 0.32 380.2 650.2 470.1 149.3 x saturation 162.3 x saturation 58.8 x saturation 242 J SCI IND RES VOL 74 APRIL 2015 Retains higher charge density at higher pH Does not depress pH as much as alum Does not cationize anionic fibers as much as alum Forms cationic micelles in the water phase of a stock system which combines with pitch particles and anionic trash - micelles deposit on the anionic fibers and are carried out with the sheet PAC treated stock slurry contains less anionic trash and free fines that will improve drainage (more pronounced in low shear systems) The cons include: Can cause deposits Is more expensive than alum Is more corrosive than alum Behaves differently (in terms of charge and reaction time) under different dilution scenarios From this review, it was decided that the disadvantages of using PAC far-outweighed the benefits and so other options for mitigating the scale deposition problem were explored.Option 1 was then examined. Among the choices in this option were chemistry changes such as: pre-acidification of stock, higher pH at the headbox, and reduced alum, or PAC substitution, for size development. The one considered feasible was good brownstock washing of pulp via pre-acidification of stock as studies have demonstrated that barium that is bound to fiber (via carboxylic acid groups) and is released under acid environments22. For example, the barium content of pulp varies from 6 ppm under alkaline conditions to less than 0.1 ppm under acid conditions; the corresponding values for calcium ions are 900 and less than 10 ppm, respectively. Results for pre-acidification studies The results for pulp washing studies, conducted in the laboratory indicated that washing with tap water is not effective in removing metal ions from the pulp. The effect of washing with pH adjusted water, however, is very dramatic as illustrated in Figure 3. Washing with alkaline water was not effective in removing metal ions from the pulp but washing under acid conditions was effective. From this, it can be surmised that countercurrent washing operations will not be effective in removing metal ions from brownstock pulps: as long as the return wash waters are alkaline, insignificant metal ions will be removed from the washed pulps. The results demonstrate that pre-acidification of pulps will be beneficial in removing significant inputs of barium into Fig. 3—Effect of pH on wash removal of metal ions from brownstock pulp (actual concentration of barium has been scaled up x100). the headbox system.The results show that pre-acidification washing of machine chest (MC) outlet stock was more advantageous than pre-acidification washing of raw stock pulp, i.e., more metal ions were removed in the washing of MC pulp than in the washing of raw stock pulp. However, for practical reasons, it makes sense to apply the procedure to raw stock pulp and not the machine chest outlet pulp. Using pre-acidification before pulp washing can help to lower scale deposition on mill equipment. A proviso is that the wash effluents need to be sewered so as to avoid recirculation of the removed metal ions.A mill trial of the pre-acidification strategy was conducted over four days. Samples were collected at three points and analysed for ash content. The results indicated that the ash content in the headbox decreased to about 25% (versus >30% before pre-acidification). The improvement was not impressive and not as great as expected. This is most probably because sulphuric acid was used for pre-acidification and, also, the acid filtrates were not sewered as the mill had no facilities to do this. Non-sulphate containing acids were not considered due to budget restrictions. Consequently, the improvement was not good enough to warrant full scale application. Scale inhibitor trial The next option studied was use of additives to control and manage the scale deposits. A barium inhibitor program was trialed: this was a continuous treatment program using chemicals that operated on all three mechanisms of scale inhibition: threshold (nucleation) inhibition, dispersion (inhibition of crystal growth Inhibition), and crystal modification. Information about the inhibitor, as provided by the supplier, included: SITHOLE et al: CONTROLLING BaSO4 SCALE DEPOSITION PROBLEMS The inhibitor has been shown to be effective for scale control The additives in the product were a blend of polyphosphates, organic phosphonates and polyacrylate dispersants The dispersant components use charge and molecular structure to interfere with the combination of BaSO4 molecules The polyphosphates and organic phosphonates function as nucleation inhibitors The components in the inhibitor degrade slowly in paper machine environments But they can be affected by pH and are more effective at relatively higher pH (above 4.5 to 5.0) The ingredients interfere with the barium sulphate reaction (nucleation) and increase the apparent solubility product of the scale However, they degrade (become ineffective) with time and with exposure to higher temperatures in the system The inhibitor is used at sub-stoichiometric levels and minimum concentrations are, thus, required The dosages used vary with scaling tendency The inhibitor is prone to interference from aluminum ions. Another benefit of using this additive chemistry is that phosphonates and polyacrylates are also effective in controlling calcium sulphate scale23-24. The scale inhibitor was to be fed continuously, neat in an area of good mixing after the alum and rosin size dosage points and close to the headbox. Parameters for success for the trial were a reduction of barium sulphate scale deposition, improved runnability/machine efficiency, improved basis weight and moisture profiles, reduced down time for cleaning mill equipment, fewer and more effective boil outs (the additive was supposed to soften the scale deposits thus making them easier to clean from metal surfaces), and improved reliability and operation of metering and regulating devices. A chelant boil out was performed before the trial to ensure minimum barium sulphate buildup Fig. 4. 243 Results for spot tests for barium levels in process samples Results for barium levels showed measurable levels of barium at the beginning of the trial on samples collected after the addition point of the scale inhibitor in the headbox. However, after 3 days no barium precipitates were evident in samples collected at this point. Samples collected (before the scale inhibitor Fig. 4—Effect of acid washing on the removal of metal ions (actual concentration of barium has been scaled up x100). addition point) at the twin roll press showed consistent levels of barium precipitates that corresponded to about 3 ppm free barium. These results demonstrated that the inhibitor was effective in removing barium from the system. Results for on-line deposition coupon tests Deposition on test coupons was negligible throughout the trial period and varied from 0.02 to 0.6 g for regular one month exposure tests. The low measurements contrasted with values that exceeded 5 g in pre-trial tests. This confirmed the effectiveness of the scale inhibitor programme in preventing the deposition of scale on mill equipment. Results of scale inhibitor trial The 3 week trial appeared to be a success in that visual inspection of the headbox, foils, LEXAN sheets, Uhle boxes showed that they were clean. There were no fisheye defects in the paper produced during the trial. Prior to the trial, these points would be encrusted with significant amounts of scale deposits after running for 3 weeks. Almost all of the criteria for success were achieved and the costs associated with use of the inhibitor were deemed to be cost-effective. Calculations indicated that the costs would be recouped in less than a year. The mill was satisfied with the results and the scale inhibitor programme was implemented on a full time basis. In addition to this, the mill improved chip screening operations to reduce the amount of residual bark in the chips. Conclusions Troubleshooting of scale deposits and defects in paper samples showed that the problem was caused 244 J SCI IND RES VOL 74 APRIL 2015 by barium sulphate and calcium sulphate scales. However, it was ascertained that barium sulphate was more of a concern than calcium sulphate as it is more tenacious than the calcium sulphate scale. A study of the inputs of the scale components found that the major inputs of barium into the mill system were the wood chips and bark contamination. The major inputs of the sulphate component of the scale were sulphuric acid used for pH control and alum used for rosin sizing.Evaluation of several options for mitigating the scale deposition problem showed that bark removal and continuous application of a scale inhibitor comprised of phosphates/phosphonates and polyacrylates were effective in reducing and controlling the scale deposit problems. Institution of these measures led to a cleaner paper machine that required far fewer boil outs than before. In addition, productivity improved and the fisheye defects disappeared.A rapid method was developed for onsite estimation of barium levels in mill process samples. The data were used to adjust the dosage of the scale inhibitor to ensure optimum effectiveness of the programme. 8 9 10 11 12 13 14 15 16 17 References 1 2 3 4 5 6 7 Back E L & Allen L H (Editors), Pitch Control, Wood Resin and Deresination, TAPPI PRESS, Atlanta (2000). 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