“Something for nothing” hits pay dirt! Joseph D. Gierlach Jr. ~ Vice President, Technical Training and Support TEGG Corporation ~ Pittsburgh, PA ABSTRACT: It has been said by wise men that, “the best things in life are free.” This statement can be very hard to accept in today’s competitive world, and it can be argued that there is nothing left in life that is free. Occasionally, though, we see glimpses of this that can lead to revelations which prevent catastrophe and forge relationships between contractor and customer that will last a lifetime. This paper covers a recent case study in which a simple service led to the discovery of a major deficiency that surely would have resulted in a failure in a large food processing facility. The irony of the story is that the component was not part of the original inventory of components, and the fault was identified simply by taking one extra step out of curiosity. The results are unmistakable, and reinforce the fact that going the extra mile and giving “something for nothing” can and does pay dividends. INTRODUCTION: With the demands on electrical systems and components in the 21st century, reliability, uptime, reduced operating costs, longevity, and consistency have become paramount considerations. One cannot afford to have an interruption in supply power, let alone the failure or destruction of a component in a system that provides the life blood of any given facility. Interestingly, though, a paradox had developed with respect to maintenance by depending on system performance and reducing allocations in budgets. There is nothing that will last forever without some attention focused on prevention to foster that reliability and performance desired. Insanity has been characterized as “doing the same things over again and expecting different results.” This is a fitting description of some maintenance philosophies where the mentality is that less attention will not contribute to equipment failures or “if it ain’t broke, don’t fix it.” Not all facilities have the resources or contingency plans in place for a “run to failure” operation; however, for those who fit this category, a well administered maintenance program aids in not only lowering operating costs, but increasing the MTBF of components. Doing more for less has become the most common theme throughout the industry, and managers are faced with the challenges of stretching their resources, including budgets and personnel. This can become taxing as the demands grow and possibly lead to shortfalls with unintended consequences. Manufacturing processes of any type, such as metals, plastics, or even food products, require continuous operation that cannot suffer disruption, as this could cause a chain reaction event that could render an entire run or batch useless or scrap. This is not a good scenario for the bottom line of any company if the goal is to maximize profit margins. CASE STUDY: Recently, one such event took place at a bacon processing plant in northeast Ohio. A major processor of food products implemented a maintenance agreement with Advanced Electrical Testing and Preventative Maintenance, located in Canton, Ohio. Work commenced at the facility in June of 2008 and was performed by Jeff Hinton and Jerry Bennett, lead technicians who have been performing TEGG services for about a year. The inventory on this particular site consisted of 222 components, so there was enough service to keep the technicians on site for a couple of weeks, and time would be of the essence. Jeff Hinton Jerry Bennett Throughout the application of the service, a number of deficiencies were identified and documented. A summary of the classes included 19 infrared, 42 electrical, and 1 ultrasonic problem. Interestingly, the one ultrasonic class problem just happened to be located within a 12,470 VAC safety disconnect switch (similar to Figure #1 below) feeding a primary side of a main service, oil-filled transformer with a 480 VAC secondary, and this was one of two major components that did not make the inventory list. Additionally, this was a parallel service that had two identical switches and transformers side by side. Figure #1 As is typical with higher voltage classes of equipment, there is an inherent danger with opening the equipment while energized, so this is not a common practice. Manufacturers will include electrical and/or mechanical interlocks to prevent this from taking place; a prudent measure given the risks. It is difficult, if not impossible, to perform maintenance on equipment such as this without gaining access to the interior section. A more acceptable course of action would be to secure a shutdown of the equipment, administer several industry standard tests, install properly sized and placed infrared windows, return to service, and then use thermography to ascertain operating health. Through discussions with the customer contact, Jeff and Jerry were able to get some background on the two identical disconnects. The one switch had been rebuilt in 2006, with new hardware and terminations. Anyone who works on this type of equipment knows that it is an art to properly terminate high voltage cables. Improper installations can and have resulted in failures, which is never a pretty sight, is costly, and generally has collateral damage of other components. Being the conscientious technicians that Jeff and Jerry are by nature, they decided to listen to the switches with the ultrasonic probe using both the airborne scanning module and the contact attachment. Up on the mezzanine servicing the Main Distribution Panel, there were the two switches, one fed by the 12,470 VAC coming in from the utility, and the other tapped from the line side of switch number one. The vented bottoms of the enclosures made the use of the airborne scanning module elementary. The first switch appeared normal as one would expect - very quiet with only ambient and competing ultrasound present. The second switch “surprised” the technicians with respect to tonal quality and also intensity. The emission from this device was a very familiar audible sound that Jeff and Jerry have heard many times through their training and work in the field. It appeared to them to be tracking of some sort, or possibly a mechanical vibration. A thorough visual inspection of the enclosure soon ruled out any loose tags, nameplates, hinges or propagating emissions from the transformer that was close by. It did not take long to confirm that what they were dealing with was in fact an electrical anomaly originating from the interior of the second disconnect safety switch. Jerry quickly made several recordings of each switch, as comparisons of similar components are crucial to making sound judgment calls. Seeking a second opinion, he also reached out to me through a phone call and we discussed his observations. The recordings were sent for analysis, and in Figure #2 below are the frequency spectrums of the two switches. Figure #2 The red trace illustrates the first switch in which there were no ultrasonic emissions present. The white trace is the recording of the second that clearly has an anomaly. The frequency content in between each 60 Hz peak is clearly more evident, the amplitude of the frequency peaks are much higher in intensity, and the 60 Hz peaks begin to “disappear” on the outer part of the spectrum, suggesting not corona only, but destructive corona with tracking. Nuisance corona in this type of equipment would not be uncommon, however, when the 60 Hz peaks start to disappear on the outer portion of the spectrum, this indicates that “electrical discharges” are now taking place, better known as tracking. The time domain is even more telling in this example, as it truly illustrates why comparison recordings have so much value in identifying problem items. Everyone knows that as we have intermittent discharges relative to tracking, there are more inconsistencies in the time domain. One would expect that the characteristic “band” of white noise would be present; however, the amplitude and spacing (more specifically, timing) should be uniform in this tool and recording. As evidenced by Figure #3 below, this is clearly not the case. Figure #3 Although we can see that there is an abundance of white noise throughout the recording, the “excursions” that take place suggest no uniformity in spacing at all, which is our tell-tale sign of electrical discharges due to the timing of the events. On the non-deficient switch, this becomes even more transparent and is illustrated in Figure #4 below. Figure #4 This is the more atypical time domain spectrum of a properly functioning electrical component of this type. There is minimal content throughout the recording period, with the minor exceptions of two excursions that represent an adjustment of the instrument’s contact module for positioning purposes. The above represents what one expects to “hear” when applying the ultrasonic instrument in the electrical arena, notwithstanding the obvious items such as transformers, contactors, and variable speed drives, to mention a few. By comparing these two recordings, it became even more evident that something was taking place in the second switch that could be nothing short of imminent failure. Action had to be taken as soon as possible with this discovery. After consulting the customer contact and presenting the exculpatory evidence and findings, the recommendation was made that a shutdown should be scheduled to open the switch to investigate the suspicions related to the destructive corona. The customer agreed, and a plan was devised to secure this outage on July 4, 2008. As this was a holiday weekend, everything came at a premium, so our analysis had to prove correct. Jerry and Jeff made preparations over the next week by securing all the parts for this particular switch that might be needed - tools, temporary grounding clusters, lock-out / tag-out items, and a coordinated plan with plant personnel and the utility supply to ensure a smooth and safe transition to the de-energized service. Finally the day arrived and work began early that morning. After working with plant staff to secure the removal of source power, verify the absence of power, and lock out all the applicable components, it was now time to open the suspect switch. All were curious as to what would be revealed, as this remained a hypothesis based solely on the recording and spectral analysis until now. In a matter of moments, it was crystal clear that our diagnosis was right on target. The visual inspection quickly uncovered two major deficiencies that could have never been identified while in operation and undoubtedly would have failed at some point. First, the A and B phase knife contacts on the line side of the switch were only seated into the clip approximately ¼”, barely making contact for the size of the service. This contributes to high resistance connections which produces additive levels of thermal energy; however, one could not see this without opening the door (not a recommended protocol due to the voltage potential) or the benefit of infrared windows (not installed at this site). Absent this observation, the switch would have more than likely remained in service, continued to deteriorate, and ultimately experienced a failure due to this. Line side knife contacts are seen in Figure #5 below. Figure #5 Full Switch View Close Up of A & B Phase You can see by the close-up view above that the left (A Phase) contact is not seated properly compared to the right (B Phase) contact knife. Comparative ductor measurements indicated a deviation that was simply not within the acceptable limits, so the technicians exercised the switch blades four (4) times before the knives would seat properly, assuring good, low resistance connections. Cleaning, burnishing, lubrication, and a retest of the contacts verified that the repair actions were successful, with all values now within tolerances. This was not, however, the source of the ultrasonic emissions identified and recorded two short weeks ago which predicated the outage and maintenance efforts. The source was close by, though, and did not take long to deduce the course of action. The conductors in this switch were cotton jacketed SRML type insulation which connected the load side of the switch to the pin bushings of the service transformers. The conductors were all routed through a dielectric, mica board to allow for securing the wires and provide separation of magnetic fields. The white, powdery residue that is typical of the nitric acid formed when destructive corona releases nitrates into the oxygen was clearly present on these conductors and mica board. Nitric acid both degrades and destroys electrical insulation and insulators, allowing discharges along the insulator path that ultimately seek a path to ground and cause a flashover. This can be seen below in Figure #6. Nitric Acid Residue Figure #6 This left no doubt that insulation breakdown had occurred and the integrity was compromised, setting the stage for an explosion to eventually manifest. A failure of these conductors surely would not be contained to this area and would initiate a chain reaction that would impact not only the conductors, but the switch itself, the service transformer, and possibly the downstream components supplied by this transformer due to their close proximity. Repair work continued, and the load side conductors were removed to measure the length of the replacement runs. Further evidence of the discovery and heating effects (suggesting current flow to ground…) can be seen below in Figure #7. Insulation Breakdown Figure #7 The conductors were extremely difficult to remove from the mica board due to swelling of the insulation and effects of the nitrates and heat! Evidence of thermal heating was apparent on the conductors; however, this would have NEVER been identified with even the best of the infrared cameras on the market, as there were no IR windows installed on this equipment. Indirect measurements of temperature and thermal energy can be very misleading, as the source energy can be hundreds or even thousands of degrees higher than what a camera would detect on the outside of equipment such as this. The new conductors were cut to length, mica board cleaned of all residue that could contribute to a path for current flow to ground, all connections were tightened and torqued to specifications, and the entire service completed on a July 4th holiday with the customer close by to witness the efforts. Once the repair and replacement of the conductors was completed, the final checks with a ductor were performed to ensure that good, solid electrical connections were present to minimize the heating effects of the passive points. Figures #8, #9, and #10 show the end result as a marked difference from what was found. Figure #8 Figure #9 Figure #10 Upon completion of this final task, the procedure to restore the utility supply was initiated. Plant personnel worked with Jerry and Jeff to return the two switches and transformers to service and get the normal loads back online. Once this became a reality, one final task remained, which was to verify the repairs under normal loads with the ultraprobe. With guarded anticipation, the rescan of the units was conducted and the results were as one would expect. Jerry characterized what he determined by saying, “it is quiet as a church mouse.” This is the ultimate validation of both the repairs that were performed, as well as the initial diagnosis with the ultraprobe. Although the units were not part of the preliminary inventory, the discovery of the ultrasonic emission and subsequent analysis with the spectralyzer software indicated a major problem that needed attention. When presented to the customer, the evidence had to be convincing, as it was on a “sight unseen” basis. The proof became the final product. SUMMARY: Maximizing both uptime and equipment longevity have become more important than ever, and facilities need to have a multi-pronged approach to maintaining components. To accomplish this requires not just a good plan and execution of that plan, but taking advantage of every single tool available to aid in good, solid, and precise identification of problem areas. One must also have competent, forward-thinking personnel applying service and maintenance with the propensity to not only think outside the proverbial box, but take extra steps along the way that sometimes uncover hidden time bombs. That was certainly the case in this example. Jerry and Jeff could have easily performed their duties on just the components contained in the inventory and gone home. In between tasks, the conscientious nature of the technicians shone through by their taking a listen to nearby items. The ultrasound is a routine service in many cases, and “going through the motions” with complacency setting in can be common. It was anything but routine in this example. When one is expecting to hear NOTHING and something different transpires, it raises your ears very quickly. You cannot take for granted that equipment that should be silent will always be that way. Anything can take place, and today’s stresses on systems foster an atmosphere conducive to deficiencies, particularly on equipment that typically lacks maintenance. Budget dollars should be spent wisely in all cases to maximize return and service. Escalating costs of products, services, and commodities have impacted organizations from coast to coast, causing shifts in planning strategies that typically result in cuts of maintenance budgets. This looks good on the balance sheet, but the ramifications of such decisions are seldom taken into consideration. What is the cost of reduced maintenance frequency or total inaction? Reducing operating costs and retaining capital is a must for any business to redeem margins, realize planning goals and remain solvent. The short-term savings can be literally wiped out with the failure of one major component in the electrical system, leading to expenditures of hundreds or thousands of times more than was initially saved. The adage of “you never have enough money to do it right the first time, but always have enough to do it again” certainly comes to mind when a malfunction or failure occurs. Planning should include the most critical items that service any facility. This includes not only contingency plans if something does in fact fail, but a proactive mindset to maintain these items in the most cost-effective manner and achieve the desired results of equipment service for many years. Using all the available tools, technology, and test equipment is the first step in assuring this outcome. Utilizing service organizations that routinely go the extra mile while servicing items does not hurt the cause either. In closing, expect the unexpected with electrical equipment. You never know what will be uncovered even with the most mundane of tasks, and the “pay dirt” realized comes in the form of a lasting relationship for years to come as customers get “something for nothing.” ACKNOWLEDGEMENTS The author wishes to thank UE Systems, Inc. and Advanced Electrical Testing and Preventative Maintenance for contributions to this article. We also thank our TEGG customers for giving us the chance to perform inspections during scheduled maintenance agreements with the intent of gathering information for this paper. Contributors Jeff Hinton Jerry Bennett Mark Goodman Alan Bandes Doug Waetjen Lead Technician - Advanced Electrical Testing and Preventative Maintenance, Canton, OH Technician - Advanced Electrical Testing and Preventative Maintenance, Canton, OH UE Systems, Inc. UE Systems, Inc. UE Systems, Inc.
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