FULL SCALE CALCIUM BROMIDE INJECTION WITH SUBSEQUENT MERCURY OXIDATION AND REMOVAL WITHIN WET FLUE GAS DESULPHURIZATION SYSTEM: EXPERIENCE AT A 700 MW COAL-FIRED POWER FACILITY by MARK SIMPSON BERRY BHARAT K. SONI, COMMITTEE CHAIR RAMSAY CHANG MELINDA M. LALOR LARRY S. MONROE PETER M. WALSH A DISSERTATION Submitted to the graduate faculty of The University of Alabama at Birmingham, in partial fulfillment of the requirements for the degree of Doctor of Philosophy BIRMINGHAM, ALABAMA 2012 Copyright by Mark Simpson Berry 2012 ii FULL SCALE CALCIUM BROMIDE INJECTION WITH SUBSEQUENT MERCURY OXIDATION AND REMOVAL WITHIN WET FLUE GAS DESULPHURIZATION SYSTEM: EXPERIENCE AT A 700 MW COAL-FIRED POWER FACILITY MARK SIMPSON BERRY INTERDISCIPLINARY ENGINEERING ABSTRACT The Environmental Protection Agency promulgated the Mercury and Air Toxics Standards rule, which requires that existing power plants reduce mercury emissions to meet an emission rate of 1.2 lb/TBtu on a 30-day rolling average and that new plants meet a 0.0002 lb/GWHr emission rate. This translates to mercury removals greater than 90% for existing units and greater than 99% for new units. Current state-of-the-art technology for the control of mercury emissions uses activated carbon injected upstream of a fabric filter, a costly proposition. For example, a fabric filter, if not already available, would require a $200M capital investment for a 700 MW size unit. A lower-cost option involves the injection of activated carbon into an existing cold-side electrostatic precipitator. Both options would incur the cost of activated carbon, upwards of $3M per year. The combination of selective catalytic reduction (SCR) reactors and wet flue gas desulphurization (wet FGD) systems have demonstrated the ability to substantially reduce mercury emissions, especially at units that burn coals containing sufficient halogens. Halogens are necessary for transforming elemental mercury to oxidized mercury, which is water-soluble. Plants burning halogen-deficient coals such as Power River Basin (PRB) coals currently have no alternative but to install activated carbon-based approaches to control mercury emissions. This research consisted of investigating calcium bromide addition onto PRB coal as a method of increasing flue gas halogen concentration. The treated coal was combusted in a 700 MW boiler and the subsequent treated flue gas was introduced into a wet FGD. Short-term parametric and an 83-day longer-term tests were completed to determine the ability of calcium bromine to oxidize mercury and to study the removal of iii the mercury in a wet FGD. The research goal was to show that calcium bromine addition to PRB coal was a viable approach for meeting the Mercury and Air Toxics Standards rule for existing boilers. The use of calcium bromide injection as an alternative to activated carbon approaches could save millions of dollars. The technology application described herein has the potential to reduce compliance cost by $200M for a 700 MW facility burning PRB coal. Keywords: mercury emissions, mercury oxidation, calcium bromide injection, mercury removal, mercury reemission, Powder River Basin coal iv DEDICATION I dedicate this body of work to my loving family. Particularly, I recognize my wife, Crystal Y. Berry, who sacrificed greatly to make this work possible. This dissertation would not have been possible without the inspiration of my father, Dr. Simpson Berry, Jr., and my brother, Edward J. Berry, Esquire. My father and brother have both inspired me by setting and achieving extremely high goals. Also, I thank my mother, Gwendolyn Nell Berry, whose never-ending support made me feel that anything was possible. I hope that the accomplishment of completing this dissertation might inspire my children, Brandiece N. Berry, Simpson Berry III, Mark Christian Berry, and James Stephen Berry, to reach and even exceed their own potential. v ACKNOWLEDGMENTS I thank Dr. Peter Walsh for his never-ending patience with me during this very long process and for his guidance. I also thank the members of my dissertation committee: Dr. Ramsay Chang, with the Electric Power Research Institute; Dr. Larry Monroe; Dr. Melinda Lalor; and Dr. Bharat Soni. I thank Dr. Bernhard Vosteen for his mentorship and guidance in the demonstration of bromine injection technology. Our professional relationship has developed into a friendship for which I am very grateful. I thank the team at URS Corporation that worked over a four-year time period collecting the information reflected in this dissertation. More specifically, I thank Katherine Dombrowski, PE, who served as the project manager from URS. I also thank Gary Blythe, Tom Machalek, Jenny Paradis, and Mandi Richardson of the URS Team. I thank Dr. Larry Monroe and Nick Irvin, PE of Southern Company Services for their contribution to this research. Last, I thank many people at Southern Company Services who encouraged me to finish my degree, Mr. Steve Wilson, PE, Dr. Charles Goodman (retired), Mr. Chris Hobson, and Mr. Paul Bowers. I recognize Alabama Power Company, Southern Company Services, and the Electric Power Research Institute (EPRI) for providing the financial support for this work. Also, I thank the Electric Power Research Institute for allowing me to share these results with the broader scientific community. vi TABLE OF CONTENTS Page ABSTRACT ....................................................................................................................... iii DEDICATION .................................................................................................................... v ACKNOWLEDGMENTS ................................................................................................. vi LIST OF TABLES ............................................................................................................. xi LIST OF FIGURES ......................................................................................................... xiv LIST OF ABBREVIATIONS ........................................................................................ xviii CHAPTER 1. INTRODUCTION AND RATIONALE ................................................................. 1 1.1 1.2 1.3 1.4 1.5 1.6 1.7 Regulatory Background ................................................................................. 1 Problem Statement ......................................................................................... 6 Purpose of the Study ...................................................................................... 7 Significance of the Study ............................................................................... 8 Overview of Methodology ............................................................................. 9 Research Hypotheses ..................................................................................... 9 Research Limitations ................................................................................... 10 2. LITERATURE REVIEW AND BACKGROUND INFORMATION ................. 12 2.1 2.2 2.3 2.4 Introduction .................................................................................................. 12 Hg Oxidation ................................................................................................ 13 2.2.1 Homogeneous Oxidation ................................................................. 14 2.2.2 Heterogeneous Oxidation................................................................. 22 Hg Capture in wet FGD ............................................................................... 42 2.3.1 Wet FGD Hg Removal Performance Data....................................... 43 2.3.2 Solubility .......................................................................................... 44 2.3.3 Role of Hg Reemission .................................................................... 46 2.3.4 Partitioning of Hg Within the wet FGD ........................................... 49 Literature Review Synopsis ......................................................................... 51 vii TABLE OF CONTENTS (continued) Page 2. LITERATURE REVIEW AND BACKGROUND INFORMATION 2.5 Critical Analysis........................................................................................... 54 2.5.1 Strengths of the Literature ............................................................... 54 2.5.2 Weaknesses of the Literature ........................................................... 55 2.5.3 Importance of the Current Work ...................................................... 56 2.5.4 Issues Not Addressed by the Current Work ..................................... 57 3. METHODS .......................................................................................................... 58 3.1 3.2 3.3 3.4 Introduction .................................................................................................. 58 Research Design........................................................................................... 62 3.2.1 James H. Miller Steam Plant ............................................................ 62 3.2.2 CaBr2 Feed Rates and Coal Br Concentration ................................. 70 3.2.3 Description of the Test Phases ......................................................... 71 Measurement Techniques ............................................................................ 78 3.3.1 Flue Gas Measurement Techniques ................................................. 78 3.3.2 Liquid and Solid Measurement Techniques .................................... 86 Statistical Methods ....................................................................................... 90 3.4.1 Description of the Data .................................................................... 90 3.4.2 Descriptive Statistics ........................................................................ 93 3.4.3 Statistical Tests Used to Evaluate Population Means ...................... 93 4. RESULTS .......................................................................................................... 97 4.1 4.2 4.3 4.4 Introduction .................................................................................................. 97 Hypothesis 1................................................................................................. 98 4.2.1 Baseline Hg Oxidation Analysis ...................................................... 98 4.2.2 Equipment Configuration Impacts on Baseline Hg Oxidation .............................................................. 105 4.2.3 Effect of SO2 Concentration .......................................................... 108 4.2.4 Effect of Flue Gas HBr and HCl Concentration ............................ 109 4.2.5 Operational Impacts on Hg Oxidation ........................................... 111 4.2.6 Summary ........................................................................................ 117 Hypothesis 2............................................................................................... 120 4.3.1 CaBr2 Addition Rate Strategy ........................................................ 120 4.3.2 Heterogeneous versus Homogeneous Oxidation ........................... 125 4.3.3 Summary ........................................................................................ 131 Hypothesis 3............................................................................................... 132 4.4.1 Wet FGD Hg Removal Efficiency ................................................. 132 4.4.2 Evaluation of Hg Reemission ........................................................ 135 4.4.3 Insights Into the Occurrence of Reemission .................................. 139 viii TABLE OF CONTENTS (continued) Page 4. RESULTS 4.5 4.6 4.7 4.4.4 An Evaluation of Br/Hg Ratio ....................................................... 146 4.4.5 Summary ........................................................................................ 147 Hypothesis 4 .............................................................................................. 148 4.5.1 Analysis of Phase III Hg Emissions............................................... 148 4.5.2 Impact of Coal Characteristics ....................................................... 154 4.5.3 Impact of Load ............................................................................... 158 4.5.4 Impact of Calcium Bromide Addition ........................................... 166 4.5.5 Comparison of Hg Emissions from Unit 3 and Unit 4............................................................................ 167 4.5.6 Br/Hg Ratio Impact on Hg Removal Performance ........................ 167 4.5.7 Summary ........................................................................................ 168 Hypothesis 5............................................................................................... 169 4.6.1 Overview ........................................................................................ 169 4.6.2 Unit 4 Hourly Average Hg Emission Rate Analysis ..................... 170 4.6.3 Unit 3 and Unit 4 30-Day Hg Emission Rate Analysis ................. 172 4.6.4 Seven-day CaBr2 Addition System Outage Simulation ................. 174 4.6.5 Summary ........................................................................................ 176 Hypothesis 6............................................................................................... 176 4.7.1 Economic Analysis of CaBr2 Addition .......................................... 176 4.7.2 Economic Analysis of Activated Carbon Injection (ACI) into a Cold-side ESP ............................................ 177 4.7.3 Comparison Cost of 90% Hg Control ............................................ 178 4.7.4 Summary ........................................................................................ 180 5. INTERPRETATIONS AND RECOMMENDATIONS ..................................... 182 6. IMPLICATIONS FOR FURTHER RESEARCH .............................................. 185 LIST OF REFRENCES .................................................................................................. 188 APPENDIX ..................................................................................................................... 199 A. PHASES I, IIA, IIB, AND III BASELINE MERCURY OXIDATION INFORMATION ................................................................ 199 ix TABLE OF CONTENTS (continued) Page APPENDIX B. PHASES I, IIA, IIB, AND III COAL MERCURY CONCENTRATION.................................................................................. 202 C. NORMALITY ANALYSIS ....................................................................... 204 D. STATISTICAL TEST RESULTS ............................................................. 229 x LIST OF TABLES Table Page 1.1 Summary of the Mercury and Air Toxic Standards (MATS) Rule for Coal-Fired Power Stations ........................................................................ 3 1.2 Relative Cost of Mercury Control Technologies .................................................... 5 2.1 SCR Key Design Parameters ................................................................................ 26 2.2 Solubility of Various Hg Compounds in Water .................................................... 45 3.1 Coal Analysis Plan ................................................................................................ 65 3.2 Information Used to Calculate Coal Bromine Concentration ............................... 71 3.3 Phase I Test Conditions ........................................................................................ 73 3.4 Phase IIA Test Conditions .................................................................................... 75 3.5 Phase IIB Test Conditions .................................................................................... 76 3.6 Phase III Test Conditions ...................................................................................... 78 3.7 Wet FGD Slurry Analytical Methods ................................................................... 87 3.8 Coal Analytical Methods ...................................................................................... 88 3.9 Gypsum Analytical Methods ................................................................................ 89 3.10 Fly Ash Analytical Methods ................................................................................. 90 3.11 Independent and Dependent Variables Used to Test for Statistical Significance of the Effect of CaBr2 Injection on Hg Emissions from Wet FGD .......................................................................... 92 xi LIST OF TABLES (continued) Table Page 3.12 Time Periods During Which Independent and Dependent Data Were Collected for Statistical Significance Analysis................................... 93 3.13 Statistical Tests Performed in Evaluating Hypothesis 4 and Hypothesis 5 ................................................................................................... 96 4.1 Coal Characteristics Summary ............................................................................ 101 4.2 Important Equipment Design and Operating Data Values that Affect Hg Oxidation .................................................................................... 107 4.3 Flue Gas HCl, HBr, Cl2 and Br2 Concentrations during Baseline Conditions ............................................................................................ 110 4.4 Qualitative Summary of Miller Unit 4 Ability to Support Hg Oxidation ....................................................................................................... 119 4.5 Summary of Hg Oxidation Ratios as a Function of Br/Hg Ratio ....................... 122 4.6 Guidance on Br/Hg Ratio to Achieve Oxidation Ratios Greater Than 0.9 While Firing PRB Coal as a Function of SCR Status .......................... 124 4.7 Hg Oxidation and Removal Information Collected During Phases IIA and IIB. ............................................................................................. 134 4.8 Reemission Parameter Qualitative Ranking System........................................... 143 4.9 Summary Operational Information Describing the Potential for Hg Reemission Events to Occur Within the 2 MW Pilot Wet FGD During Phases IIA and IIB Testing. ................................................... 145 4.10 Wet FGD Hg Removal Ratio and Reemission Parameter as a Function of Br/Hg Ratio and SCR Condition .............................................. 146 4.11 Unit 3 Hourly Average Hg Emissions Descriptive Statistics During CaBr2 Addition Period on Unit 4 and Not During CaBr2 Addition Period on Unit 4 ........................................................................ 155 xii LIST OF TABLES (continued) Table Page 4.12 Unit 4 Hourly Average Emissions Descriptive Statistics During September 2010 and January 2011 ......................................................... 157 4.13 Unit 3 Hourly Average Hg Emissions Descriptive Statistics of Various Load Conditions From September 1, 2010, Through January 31, 2011. ................................................................................. 159 4.14 Unit 4 Hourly Average Hg Emissions Descriptive Statistics of Various Load Conditions From September 1-30, 2010, and From January 1-30, 2011 ............................................................................. 161 4.15 Unit 4 Average Hourly Hg Emissions Descriptive Statistics of Various Load Conditions From October 1 through December 19, 2010 ............................................................................................. 164 4.16 Unit 4 Average Hourly Hg Emissions Descriptive Statistics During Periods With and Without CaBr2 Addition ............................................ 166 4.17 Phase III Br/Hg Ratio Summary Based on Hg Content Measured in the Coal and Minimum Observed Daily Br Concentrations (wt ppm on the Dry Coal) .......................................................... 168 4.18 Financial and Miller Unit 4 Operation Assumptions Used to Calculate Yearly CaBr2 Chemical Costs............................................................. 177 4.19 Financial Assumptions Used to Calculate Activated Carbon Costs for One Year of Operation at Miller Unit 4 With a 90% Hg Capture Goal When the Unit Operated With a 90% Capacity Factor ........................................................................................ 178 4.20 Comparison of CaBr2 and Activated Carbon Injection Reagent Costs Associated With 90% Hg Removal From a Boiler Burning PRB Coal With an SCR/Cold-side ESP/Wet FGD or Cold-side ESP/Wet FGD .................................................................................... 180 xiii LIST OF FIGURES Figure Page 2.1 Schematic diagram of the changes in flue gas composition in an SCR ......................................................................................... 39 2.2 Schematic diagram of Hg reemission reaction pathways ..................................... 48 3.1 Electric utility technology development curve ..................................................... 59 3.2 Diagram of 2 MW slipstream pilot-scale wet FGD installed for testing at Plant Miller Unit 4 ........................................................................... 70 4.1 Hg oxidation at baseline conditions (i.e., no CaBr2 addition to the coal) as a function of the location of Hg concentration measurement and of SCR operating condition ..................................................... 99 4.2 Phase I summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), SCR inlet and outlet NOx concentrations (ppmv), and stack SO2 concentration (ppmv) used to illustrate consistency or variability of operating conditions when SCR is in service and with NH3 injection ................................................. 112 4.3 Phase IIA summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), SCR outlet NOx concentration (ppmv), and stack SO2 concentration (ppmv) used to illustrate consistency or variability of operating conditions during periods when SCR is bypassed and when SCR is in service without NH3 injection ......................................................................................... 113 4.4 Phase IIB summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), and SCR inlet and outlet NOx concentrations (ppmv) used to illustrate consistency or variability of operating conditions during a period when SCR was in service with NH3 injection ....................................................................... 115 xiv LIST OF FIGURES (continued) Figure Page 4.5 Phase III summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), SCR inlet and outlet NOx concentrations (ppmv), wet FGD inlet SO2, and outlet SO2 concentrations (ppmv) used to illustrate consistency or variability of operating conditions during a period when SCR was in service with NH3 injection ....................................................................... 116 4.6 Hg oxidation ratio versus Br/Hg ratio (lb/lb) with and without the SCR in service. Figure was developed with the use of data from Phases I, IIA, and IIB ................................................................................. 124 4.7 Hg oxidation ratio versus Br concentration (wt ppm on the dry coal) with SCR in service with NH3 injection to control NOx ..................................... 126 4.8 Hg oxidation ratio versus Br concentration (wt ppm in the dry coal) at the wet FGD inlet as a function of SCR operational status ............................ 128 4.9 Illustration of NH3 consumption and its effect on Hg oxidation behavior in an SCR ............................................................................. 130 4.10 Total Hg removal across a 2 MW pilot-scale wet FGD as a function of Br concentration (wt ppm on the dry coal) and SCR operational condition ........................................................................... 133 4.11 Wet FGD Hg removal versus Hg oxidation ratio for differing SCR reactor operational conditions during Phase IIA and Phase IIB. A marker below the 45-degree line represents lower-than-expected Hg removal, and a marker above the 45-degree line represents betterthan-expected Hg removal. A marker to the right of the vertical line represents 90% oxidation. A marker above the horizontal line represents 90% removal in the wet FGD. A marker within the green box represents at least 90% Hg oxidation and 90% Hg removal .......................................................................................... 138 4.12 Wet FGD Hg Reemission Probability Diagram. Diagram demonstrates visually that the probability of reemitting Hg from a wet FGD sump is a function of slurry bromine and chlorine concentration, sulfite concentration, oxidation reduction potential, Hg concentration in solution, and Hg concentration in the total suspended solids ......................................................................................... 141 xv LIST OF FIGURES (continued) Figure Page 4.13 Hourly average Hg emissions concentration (µg/m3) from Miller Unit 3 and Unit 4 from September 1, 2010, through January 30, 2011, which includes the bromine addition test period from October 1 through December 19. Hg emissions data were not available from December 20 through December 31. A = calcium bromide addition begins. B = Unit 4 outage. No bromide was injected during start-up. C = Missing data from dataset ................................... 149 4.14 Hourly average Hg emissions concentration (µg/m3); Br concentration (wt ppm on the dry coal); and load (MW) from Miller Unit 4 from September 1, 2010 through January 30, 2011, which includes the CaBr2 addition test period from October 1 through December 19. Hg emissions data were not available from December 20 through December 31 .......................................................... 151 4.15 Hourly average Hg emissions concentration (µg/m3) and Br concentration (wt ppm on the dry coal) from Miller Unit 4 from October 1 through December 19, 2010. Includes a Unit 4 outage from December 6 through 9, 2010. CaBr2 was not added during start-up after the outage. CaBr2 was returned to service at a lower addition rate after the unit reached full load. ..................... 152 4.16 Hourly average Hg emissions concentration (µg/m3) and Br concentration (wt ppm on the dry coal) on Miller Unit 4 from December 4 through December 19, 2010, which includes short boiler outage............................................................................................... 153 4.17 Hourly average Unit 3 Hg emissions as a function of unit load (1, Load > 600 MW; 2, 500 MW < Load < 600 MW; 3, Load < 500 MW); the figure includes data from September 1, 2010, through January 30, 2011 .................................................................................... 160 4.18 Unit 4 hourly average Hg emissions as a function of unit load (1, Load > 600 MW; 2, 500 MW < Load < 600 MW; 3, Load < 500 MW); the figure includes Unit 3 Hg wet FGD stack emissions data from September 1-30, 2010, and from January 1-30, 2011 .............................................................................. 162 xvi LIST OF FIGURES (continued) Figure Page 4.19 Unit 4 hourly average Hg emissions as a function of unit load (1, Load > 600 MW; 2, 500 MW < Load < 600 MW; 3, Load < 500 MW); the figure includes Unit 4 wet FGD outlet Hg emissions data from October 1 through December 19, 2010 ............................................................................................. 165 4.20 Chronological plot of Phase III Unit 4 hourly average Hg emissions rate (lb/TBtu) and Br concentration (wt ppm on dry coal) during the 83-day CaBr2 injection test. ............................................................... 171 4.21 Chronological plot of Phase III Unit 4 and Unit 3 daily and 30-day rolling Hg emissions rate (lb/TBtu). ....................................................... 173 4.22 Seven-day simulation of CaBr2 injection system outage combining Phase III Unit 4 30-day rolling Hg emissions rate data with Unit 4 daily Hg emissions rate data during September 1-7, 2010. The resulting plot represents the impact of higher emissions on MATS rule compliance. ................................................................................. 174 xvii LIST OF ABREVIATIONS acfm actual cubic feet per minute ACI activated carbon injection ads adsorbed Br bromine Br2 bromine (gas) Coxidized concentration of oxidized mercury at the wet flue gas desulphurization inlet Ctotal concentration of total mercury at the wet flue gas desulphurization inlet CaBr2 calcium bromide Cl2 chlorine (gas) CAIR Clean Air Interstate Rule CAMR Clean Air Mercury Rule CMM continuous mercury monitoring system DOE NETL Department of Energy, National Energy Technology Laboratory EPA Environmental Protection Agency ESP electrostatic precipitator FAMS flue gas adsorbent mercury speciation FF fabric filter FGD flue gas desulphurization g gas HBr hydrogen bromide xviii LIST OF ABREVIATIONS (continued) HCl hydrogen chloride Hg mercury Hg0 elemental mercury Hgel elemental mercury ICR information collection request JB Jarque-Bera statistic l liquid LSFO limestone forced oxidation scrubber Macf million actual cubic feet MATS Mercury and Air Toxics Standards Rule MBtu one million British thermal units NH3 ammonia ORP oxidation reduction potential PM particulate matter ppmv part per million by volume ppm part per million RP reemission parameter s solid SCEM semi-continuous emissions monitor SCR selective catalytic reduction SO2 sulfur dioxide SO3 sulfur trioxide TBtu one trillion British thermal units UBC unburned carbon xix LIST OF ABREVIATIONS (continued) wet FGD wet flue gas desulphurization wt % percent by weight wt ppb part per billion by weight wt ppm part per million by weight xx CHAPTER 1 INTRODUCTION AND RATIONALE 1.1 Regulatory Background In December 2000, Carol Browner, the Administrator of the Environmental Protection Agency (EPA), declared under authority granted by Section 112 of the Clean Air Act, that it was prudent and necessary to regulate mercury (Hg) emissions from coalfired power plants. On March 15, 2005, the EPA issued the Clean Air Mercury Rule (CAMR), designed to reduce and permanently cap Hg emissions from coal-fired power plants. The EPA designed the CAMR to work in conjunction with the Clean Air Interstate Rule (CAIR); this rule required that certain power plants install selective catalytic reduction (SCR) systems to reduce NOx emissions and wet flue gas desulphurization (wet FGD) systems to reduce SO2 emissions. EPA was aware that the combination of SCR systems and wet FGD systems had demonstrated the ability to substantially reduce Hg emissions. Both CAMR and CAIR were based on a cap-andtrade mechanism designed to give utilities flexibility in meeting the required emission reductions. EPA asserted that the utility sector constituted the largest emitter of Hg. The goal of the combined rule structure was to reduce Hg emissions from 48 tons, the estimated coal-fired power plant emissions of Hg in 2005, in two phases, at the lowest cost. The first-phase cap was 38 tons, a reduction of 21%. In the second phase, due in 1 2018, utilities reduce emissions to 15 tons, a reduction of 69%. On February 8, 2008, the Circuit Court of Appeals for the District of Columbia vacated the CAMR rule and ordered the EPA to develop a new rule to reduce hazardous air pollutants, including Hg emissions. On Feb 16, 2012, EPA in response to the Court’s directive, published the Mercury and Air Toxics Standards (MATS) Rule, (Hazardous Air Pollutants, 2012) which will require the reduction of Hg emissions from existing and new coal-fired power plants. The MATS rule became effective immediately and requires utilities to meet emissions limits for various pollutants in three years, included provisions that allow utilities to request a one-year compliance extension from their state environmental agencies, as well as a process by which utilities can request an additional one-year extension from the EPA. The MATS rule set limits on emissions of inorganic acids, Hg, and other metals. The rule used hydrochloric acid as a surrogate for inorganic-acid emissions, employed filterable particulate matter as a surrogate for heavy-metals emissions, and set direct limits on the emissions of Hg. The EPA set differing limits for plants burning low-rank coals (lignite) and those burning higher rank coals (i.e., subbituminous and bituminous). The MATS rule also established limits for Integrated Gasification Combined Cycle units utilizing all types of coals. The limits required for non-low-rank coal-fired units are listed in Table 1.1, which excludes values for low-rank coals and Integrated Gasification Combined Cycle units because this dissertation focuses only on subbituminous coals. 2 Table 1.1 Summary of the Mercury and Air Toxic Standards (MATS) Rule for CoalFired Power Stations Subcategory Existing Unit: nonlow-rank coal New Unit: non-low rank-coal Filterable Particulate Matter Hydrogen Chloride Mercury 0.030 lb/MBtu 0.0020 lb/MBtu 1.2 lb/TBtu (0.30 lb/MWh) (0.020 lb/MWh) (0.020 lb/GWh) 0.0070 lb/MWh 0.40 lb/GWh 0.00020 lb/GWh Note: all limits here are based on a 30-day rolling average. lb/MBtu = pounds pollutant per million British thermal units. lb/TBtu = pounds of pollutant per trillion British thermal units. lb/MWh = pounds of pollutant per megawatt-hour electric output (gross). lb/GWh = pounds of pollutant per gigawatt-hour electric output (gross). Table adapted from “Hazardous Air Pollutants from Coal and Oil Fired Electric Utility Steam Generating Units”, Table 3 page 9367, 77 Federal Register (2012). In light of the EPA’s dissemination of the MATS rule, utilities must begin to make compliance decisions that could mean billions of dollars of investment to bring existing power stations into compliance by 2015. Alternatively utilities could choose to close facilities because additional investment in them would not be in the best interest of the company. For example, On March 22, 2012, American Electric Power announced that, in response to the MATS rule, it would retire 4,600 MW of coal-fired generation and likely install environmental controls on 13,000 MW of coal-fired generation (Hemlepp and Rozsa, 2012). Every utility in the United States is expected to engage in similar decision-making processes to determine which power stations to retire and which power stations to modify by installing controls. The decision-making process is complex. At a minimum, the analysis must include the type of control to install, the difficulty involved 3 in the installation, the cost of installation, the long-term variable operating and maintenance costs of the control technology, and the longevity of the facility after it is controlled. The longevity of a facility is often uncertain because the regulatory environment constantly changes. In a report describing the impacts of the MATS rule on society, EPA (2011) concluded that utilities had available a number of technologies with which to meet the Hg provisions of the rule, and those technologies included sorbent injection into a fabric filter (FF), the use of SCR and wet FGD, and halogen injection with sorbent injection or SCR and wet FGD. Estimates of the potential cost of compliance technology will vary EPA (2012). Table 1.2, adapted from Jozewicz (2010) is a summary of the relative costs of technologies that might be used for compliance with the Hg portion of MATS. It must be acknowledged that utilities cannot make compliance decisions for MATS without considering the potential impacts of those decisions on existing and impending regulations such as Regional Haze, 8-hour Ozone Standard, CAIR, Steam Effluent Guideline Revisions, and the Coal Combustion Residuals Rule. For example, using halogen injection for MATS compliance will raise the risk of increasing the Hg concentration in wet FGD system blowdown. The revision of steam effluent guidelines, scheduled to be disseminated by the EPA in November 2012 (EPA 2012), likely will impose stringent limits on Hg emissions from the liquid discharges of wet FGD systems. As a result, using halogen injection to meet the MATS rule could require the installation of additional technology to reduce the possibility of increasing Hg emissions from wet FGD blowdown. 4 Table 1.2 Relative Cost of Mercury Control Technologies Capital Cost Incremental Operations and Maintenance Cost Notes Coal Treatment: Pre Combustion High Moderate Not many options commercially available Coal Additives Low Low Halogen injection Co-benefit maximization wet FGD Low Low Hg reemission management Co-benefit maximization SCR Moderate Moderate Hg oxidation Co-benefit maximization SCR + wet FGD Moderate Moderate Optimize Hg oxidation and minimize Hg reemission Activated carbon injection Upstream of existing cold-side ESP Low Moderate to High Varies based on site conditions Fabric filter plus activated carbon injection High Moderate Sets benchmark for Hg removal performance Approach Note: From “Process Optimization Guidance for Reducing Mercury Emissions from Coal Combustion in Power Plants” by Division of Technology, Industry and Economics (DTIE) Chemicals Branch Geneva, Switzerland, p. 77. November 2010. Adapted with permission. Because of the potential high cost of compliance and because of the repercussions if compliance is not achieved (both financial and political), utilities are conservative when making technology investment decisions. Although the vendors supplying the various technologies to utilities are likely to provide performance guarantees, vendors’ financial responsibilities are typically limited (e.g., a percentage of the equipment price) 5 and cover only a very short timeframe (e.g., the period of testing during initial equipment commissioning, but may extend for 12 months of operating time). This limited guarantee customarily only translates into a vendor putting forth a best effort, but falling short of guaranteeing compliance. The utility must accept a measurable amount of operational and compliance risk with any environmental control technology decision. To minimize this risk, utilities typically desire that the technology chosen for compliance has been tested rigorously or generously used under varying conditions. 1.2 Problem Statement At some point, utilities must make technology decisions for complying with the MATS rule. In the absence of compliance certainty, utilities must draw upon all available information to support technology decisions that yield, the highest degree of compliance certainty at the lowest possible cost. This type of technology choice (i.e., low risk at low cost) is in the best interest of utility customers because they ultimately bear the cost of lowering emissions. Often, regulated utilities seek permission from their regulatory bodies to increase rates to pay for compliance costs associated with environmental regulations. Because of the pressures exerted upon public utility commissions by the electorate, it is in the best interest of all parties (utilities, public service commissions, and utility customers) to keep the cost of compliance at a minimum. For unregulated utilities, the ultimate financial risk to purchase and install compliance technology is borne entirely by the utility, which likely translates into tighter operating margins to maintain profitability. For regulated and unregulated utilities, the dollars invested in compliance technology must be kept to a minimum. 6 Due to their conservative nature, it is often difficult for a utility to justify accepting a higher risk of compliance failure in order to lower costs. As described in Table 1.2, halogen injection potentially provides a means of achieving MATS compliance at a cost lower than those of other approaches. This study involved providing the utility industry with sufficient information to support a decision to use calcium bromide (CaBr2) injection to meet the Hg provision of the MATS rule at units burning Powder River Basin (PRB) coal equipped with a SCR for NOx reduction and a wet FGD for SO2 control. The information gleaned during the study, in conjunction with other publicly available information, such as that found in scientific journals, will provide enough technical certainty to support a decision by a utility to employ CaBr2 injection as a compliance technology. Additionally, the study was designed to provide scientists and engineers with data concerning the performance of the approach. 1.3 Purpose of the Study This research was undertaken to provide sufficient information to support achieving compliance with the MATS rule by using CaBr2 on the coal (i.e., halogen injection technology), for a coal unit burning a low-sulfur, low halogen coal (i.e. PRB) at a site equipped with an SCR for NOx control, a cold-side ESP for particulate matter (PM) control, and a wet FGD for SO2 control. The program specifically evaluated the use of CaBr2 as a coal additive to aid in the oxidation of Hg so that it can be captured within a wet FGD. As shown in Table 1.2, if successful, a coal-additive approach, like CaBr2 addition, could provide a lower cost solution to compliance with the Hg portion of the MATS rule. The investigator developed a four-year, three-phase program to demonstrate 7 that CaBr2, when added to the coal, could successfully support Hg removals in excess of 90% , thereby lowering Hg emissions below 1.2 lb/TBtu. During the study, CaBr2 was added to the coal to promote Hg oxidation; once oxidized, the Hg was then removed in a wet FGD at high efficiencies (>90%). The program was designed to ensure that both Hg oxidation and Hg removal at the desired efficiencies were attainable in an actual situation. A 720 MW power station that burned PRB, which is low in sulfur and halogens, was selected for the study. Phase I included only flue gas measurements to evaluate the ability of CaBr2 to affect Hg speciation. Phase II, completed in two parts IIA and IIB, included the installation of a slipstream 2 MW pilot wet FGD. The Phase II tests were used to determine the ability of a wet FGD to remove the oxidized Hg. During Phase III, an 83-day injection of CaBr2 was conducted to evaluate longer term Hg removal in a full-scale wet FGD. The study was also designed to provide full-scale data to be used by more fundamental researchers to better understand the mechanisms controlling performance of the approach. The availability of such information is often key to scientific breakthroughs and a better understanding of a process. 1.4 Significance of the Study This study adds to the information available to utilities seeking to determine whether CaBr2 addition constitutes a viable technology for compliance with the Hg portion of the MATS rule. The study also provides performance results in an actual application setting and can be used by researchers and modelers to test theories for Hg 8 oxidation via CaBr2 injection. Findings from this research will fill in some of the gaps in current understanding of the performance of the technology. 1.5 Overview of Methodology This work was completed over a four-year time span in three separate phases. The phased approach was used to reduce cost and simplify the evaluation of the technology. Because the program involved using a 720 MW boiler, a professional testing company was contracted to make all of the required measurements, including all flue gas, liquids, and solids measurements. URS Corporation, the major contractor, provided a majority of the measurement equipment and technical expertise to operate that equipment. Along with Southern Research Institute, URS was also contracted to conduct offsite liquid and solids measurements. URS also operated the CaBr2 injection equipment. Particulate Control Technologies operated the 2 MW pilot wet FGD during Phase II. Data used in the present study were compiled from a number of sources, including data provided by URS in project reports. The data historian of Alabama Power Company provided additional operational information. Southern Company Services provided information about the boiler and environmental control equipment. 1.6 Research Hypotheses The goal of the research program consisted of testing the following research hypotheses: 9 1. Burning PRB coal results in baseline Hg oxidation levels below 50% under all operating conditions. 2. Sufficient CaBr2 addition at a unit burning PRB coal results in Hg oxidation levels in excess of 90%. 3. CaBr2 addition can result in Hg capture efficiencies exceeding 90% when a wet FGD system is present. 4. The difference in average Hg emissions rates using CaBr2 addition, when compared to not employing CaBr2 addition, is statistically significant. 5. Hg emission rates achieved during the use of CaBr2 addition are sufficiently low to meet the MATS rule Hg limit of 1.2 lb/TBtu on a 30-day rolling average. 6. The presence of an SCR reactor can greatly reduce the application cost of CaBr2 injection technology and dramatically improve the cost benefit of utilizing the approach, when compared to activated carbon injection into an existing cold-side ESP. By examining these hypotheses, the investigator evaluated CaBr2 injection technology performance, provided information useful in the design of the full-scale system, and increased knowledge about the technology application costs at a unit burning PRB coal. 1.7 Research Limitations Unlike traditional research efforts conducted under simulated flue gas conditions at laboratory scale, full-scale implementation makes it impossible to control many of 10 independent variables that affect technology performance. The lack of control of the independent variables dictates a need for fundamental understanding of the process to better describe the behavior of the dependent variables (i.e., Hg emissions). An exhaustive literature search was done to better understand and quantify technology performance. The combination of fundamental understanding and technology performance in a real situation will enable utilities to decide whether this approach meets the performance and risk thresholds required for adoption. The availability of full-scale results in the absence of fundamental understanding likely translates into slower technology adoption rates. Likewise, only having a fundamental understanding without full-scale testing information also results in slow adoption rates. It is hoped that the results from this effort will be combined with existing and future fundamentally-based research programs to provide a better understanding of the approach and to accelerate adoption of the technology. 11 CHAPTER 2 LITERATURE REVIEW AND BACKGROUND INFORMATION 2.1 Introduction During the literature search conducted to establish the parameters for analysis of the data during this study, the emphasis was on establishing a basic understanding of Hg oxidation and the subsequent removal of oxidized Hg in a wet FGD. The goal was to determine what was already know about the applicability of CaBr2 addition for enhanced Hg oxidation in a full-scale boiler for potential compliance with the MATS rule. The MATS rule will require that existing coal-fired utility boilers control Hg emission to an emission rate below 1.2 lb/TBtu on a 30-day rolling average. The literature review is divided into two main sections: Hg oxidation and capture of Hg in wet FGDs. In terms of compliance, these two processes are of equal importance because both must be optimized to ensure compliance with the MATS rule. The literature appeared in many different types of publications, including technical journals, Electric Power Research Institute reports, Department of Energy National Energy Technology Laboratory reports, and conference proceedings. The different types of publications were given equal weight in the review. The literature dated from the early 1990s to the present, with the majority of the material published in the last ten years. A recent increase in publishing activity on the subject of Hg oxidation and capture from flue gas indicates an increased level of interest in this area. 12 2.2 Hg Oxidation Elemental Hg (Hgel) oxidation in coal-fired boiler furnace flue gases has received a tremendous amount of study over the past twenty years. In earlier years, the studies focused primarily on the ability of chlorine to oxidize Hg and on the subsequent removal of the oxidized Hg in a wet FGD. This phenomenon is often referred to in the industry as Hg co-benefit removal. In a report Congress, EPA (1997) highlighted the potential for utilizing the combination of SCR reactors and wet FGD systems to remove Hg from flue gas. The report summarized a number of studies documenting the removal of oxidized Hg in wet FGDs. In 1999, the EPA initiated an Information Collection Request (ICR) designed to compile an inventory of Hg emissions from coal-fired boilers. The ICR required owners/operators of coal-fired electric utility units to report the quantity of coal consumed and the Hg content of that coal. In addition, 84 power plants, randomly selected on the basis of 36 categories of coal type, SO2 controls and particulate controls, were instructed to measure the concentration and species of its Hg emissions. In an analysis of the ICR data conducted by EPRI, it was determined that the Hg speciation and removal were functions of coal chlorine (Cl) content and the presence of a wet FGD (Chu and Levin, 2001). Senior (2001), who also studied the ICR data, concluded that Hg removal by a wet FGD was a function of coal Cl content. This correlation led to a number of technical papers about the role of halogens floride (F), chloride (Cl), bromine (Br), iodide (I), and oxygen (O2), in the oxidation of Hg in coal combustion flue gases. The oxidation of Hg can occur by two distinct mechanisms: homogeneous oxidation and heterogeneous oxidation. The heterogeneous oxidation can occur in two distinct regimes: native heterogeneous oxidation, which occurs on the surfaces of 13 particles, such as flyash, unburned carbon, and activated carbon suspended in the flue gases (Niksa et al., 2010), and on engineered surfaces such as SCR catalyst, which can be designed to optimize Hg oxidation activity. 2.2.1 Homogeneous Oxidation Homogeneous Hg oxidation is the combination of vapor phase Hg with another species (mainly halogens) in a gas-phase reaction. The fraction of Hg that is homogeneously oxidized is a function of oxidant concentration, oxidant species, flue gas temperature, flue gas quench rate, the concentration of other flue gas constituents (SO2, CO, NO), and residence time. Wilcox (2004) reported that elemental Hg is thermodynamically favored in the high-temperature zone of a coal-fired boiler, which is normally approximately 1400 ◦C. As the gas cools, the state of Hg can be changed from its elemental form to an oxidized form, by reaction with the halogens (F, Cl, Br, and I) or oxygen. 2.2.1.1 Chlorine-Based Homogeneous Hg Oxidation Thermodynamic calculations predict that, in the reaction with chlorine, Hg oxidation occurs as the flue gas begins to cool, but only if sufficient chlorine, or other halogen, is present. Wilcox (2004) postulated that Hg oxidation occurs at temperatures below 700 ◦C and that all the Hg present should be completely oxidized at or below 450 ◦ C. However, stack measurements in real-world situations have shown that Hg is not completely oxidized at the lower temperatures. Wilcox (2004) concluded that the difference between the thermodynamic equilibrium predictions and the actual measured 14 results suggested that the homogeneous Hg oxidation reaction is kinetically limited. The mechanism for homogeneous oxidation of Hg developed by Xu et al. (2003) describes Hg oxidation as following a first-order chemical reaction, with a reaction rate expressed by the Arrhenius form of k = ATβexp –Ea/RT (R1) where T is the absolute temperature, A is the frequency factor, β is a correction factor for temperature, and Ea is the activation energy. The values of the parameters are obtained from laboratory experiments. Many flue gas constituents and characteristics have been found to affect the values of the parameters A, Ea and β. Studies of the effects of oxygen have shown that O2 only weakly promotes homogeneous Hg oxidation (Xu, 2003). Other studies have shown that the halogens (i.e., Br and Cl) are more effective homogeneous Hg oxidizers. When compared with O2, Cl was reported by Hall et al. (1991) to be more effective in homogeneously oxidizing Hg. Hall et al. (1991) proposed a set of reactions describing homogeneous Hg oxidation based on chlorine chemistry: 4HCl + O2 ↔ 2H2O + 2Cl2 (R2) SO2 + Cl2 + H2O ↔ SO3 + 2HCl (R3) SO2 + ½O2 ↔ SO3 (R4) Hg + Cl2 ↔ HgCl2 (R5) Wilcox (2004) concluded that when combusted coal chlorine is thermodynamically favored to exist as HCl. Procaccini et al. (2000) conducted experiments to determine the chlorine species present during coal combustion. Results revealed that 80% of the chlorine in flue gas existed as HCl, with up to 18% existing as Cl2. Procaccini et al. 15 (2000) also conducted thermodynamic modeling which revealed that up to 5% of the chlorine could exist as Cl radicals. Those values are likely an upper bound, because SO2 was not present in those experiments. The interplay of SO2 and Cl2 is a major factor in achieving high levels of homogeneous Hg oxidation. Bench-scale experiments conducted by Sterling et al. (2004) showed that SO2 had a large, inhibitory effect on Hg oxidation by Cl2. Silcox et al. (2008) also conducted thermodynamic modeling and concluded that HCl was the dominant Cl species at all flue gas temperatures. As Equation R2 indicates, a small portion of the HCl reacts with oxygen to form Cl2. This well-documented reaction, often referred to as the chlorine Deacon reaction, has been the basis of Cl2 production from HCl in the presence of a catalyst (Balcar, 1938) for more than eighty years. Cl2 shown in Equation R5 reacts with elemental Hg to form oxidized Hg. Vosteen et al. (2006) referred to Equation R5 as direct Hg chlorination. A limiting factor in the production of Cl2 is seen in Equation R3, in which sulfur dioxide (SO2) reacts with Cl2 to form sulfur trioxide (SO3) and HCl. This reaction is often called the chlorine Griffin reaction. In the case of coals that have relatively large amounts of sulfur (>1 wt %), less available Cl2 and thus lower extents of Hg oxidation via chlorine-based homogeneous reactions should be expected. Not shown in equations within this document, other researchers have proposed that chlorine ions (Cl-) constitute an important factor in the homogeneous oxidation of Hg. Edwards et al. (2001) postulated additional Hg oxidation reactions that included elementary reactions between chlorine radicals and Hg: Hg + Cl ↔ HgCl (R6) 16 HgCl + Cl ↔ HgCl2 (R7) Hg + Cl2 ↔ HgCl2 (R8) 2Cl ↔ Cl2 (R9) These equations reveal that not only is Cl2 important but that chlorine radicals (Cl) can serve as reactants for Hg oxidation. A simulation conducted by Edwards et al. (2001) showed that the extent of Hg oxidation is dictated by the interplay between Equations R6 and R9. It may be concluded that both chlorine radicals (Cl) and chlorine gas (Cl2) are necessary for the homogeneous Hg oxidation reaction to occur. Ghorishi (1998) found that the homogeneous oxidation of elemental Hg in the presence of HCl was slow and only proceeded at higher temperatures (>700 °C) and relatively with high HCl concentrations (>200 ppmv). Ghorishi (1998) also found that homogeneous oxidation of elemental Hg in the presence of Cl2 is very fast and suggested that the ratio of HCl/Cl2 might be a good key indicator of the effectiveness of homogeneous oxidation of elemental Hg by Cl. Vosteen et al. (2011) suggested that the ratio of Cl2 to total available chlorine in flue gas is very low in flue gases containing SO2. These points would suggest that homogeneous Hg oxidation by chlorine becomes less effective as the flue gas SO2 concentration increases. The presence of chlorine radicals is not only concentration dependent but temperature dependent. At high temperature, HCl is the most chemically stable chlorine species (Procaccini et al., 2000; and Silcox et al., 2008). Therefore, it is less likely that homogeneous Hg oxidation will occur in the boiler itself. As the flue gas begins to cool downstream from the boiler exit, Cl and Cl2 are formed. At lower temperatures, the formation of Cl2 in accordance with Equation R2 is favored. Vosteen et al. (2006) 17 proposed that, at 680 ◦C, the formation of Cl2 is complete. Vosteen et al. (2011) reported that consumption of Cl2 occurs subsequently via Equation R3, if SO2 is present. Cl2 is not thermodynamically favored at high temperatures. However, below 370 °C, a significant driving force exists toward the formation of Cl2 and below 260 °C, the formation of Cl2 begins to be favored over HCl formation. Gale (2004) suggested that Cl speciation is governed by equilibrium in furnace sections of coal-fired boilers, but is limited by kinetics and residence time downstream. Vosteen et al. (2006) postulated that the Hg oxidation reaction by chlorination (i.e., Cl2) ceases below 680 ◦C, which is the proposed lower-end of the range for Hg oxidation by Cl2. This would mean that while the formation of Cl2 is favored at the lower temperatures (i.e. 260 ◦C) the effect of higher concentrations of Cl2 on Hg oxidation would be very limited. The concentration of Cl present in the coal directly affects the fraction of Hg that is oxidized. Measurements during bench-scale laboratory testing revealed Hg oxidization percentages of 10% to 20% when HCl concentrations were below 200 ppmv and percentages up 40% when HCl concentrations were as high as 300 ppmv (Sterling, et al., 2004). Because these results were obtained without SO2 in the flue gas, they may represent upper bounds for homogeneous oxidation by HCl. Additional testing done in the absence of SO2 in the simulated flue gas revealed negligible homogeneous oxidation rates when HCl was not present, 20% of Hg oxidized in the presence of 200 ppmv HCl and 30% of Hg oxidized in the presence of 555 ppmv of HCl. The homogeneous oxidation of Hg in the presence of both HCl and SO2 was lower. The literature is not consistent on the effect of SO2 on Hg oxidation. For instance, in studies conducted by Smith et al. (2011), the presence of SO2 had a positive impact on 18 elemental Hg oxidation when SO2 concentrations were below 400 ppmv. An SO2 concentration of 300 ppmv is typical of flue gas from burning lower sulfur fuel such as PRB and may indicate that for lower sulfur coals SO2 may not pose a problem. Lighty et al. (2006) found that Hg oxidation by HCl was severely inhibited in the presence of SO2. Hg oxidation decreased from 70% to 0% when SO2 concentrations were increased from 0 ppmv to 300 ppmv. These results conflict with those obtained by Smith et al. (2011). Ghorishi (1998), who found that the inhibition effect of SO2 on Hg oxidation with HCl required the presence of sufficient water vapor, proposed that the inhibition effect of SO2 in the presence of water vapor may be related to a chlorine free radical scavenging effect by SO2 and water vapor. Fry (2008) conducted experiments with 600 to 1000 ppmv of Cl2 as a homogeneous elemental Hg oxidant and found that 90% of Hg was oxidized at Cl2 concentrations above 200 ppmv, that 80% of Hg was oxidized at 200 ppmv of Cl2, and that 20% of Hg was oxidized Hg at 100 ppmv Cl2, all in the absence of SO2. Fry et al. (2007) found that, as the flue gas quench rate changed, so did the effect of HCl on Hg oxidation. An increase in quench rate from -210 K/s to -440 K/s resulted in an increase in the extent of Hg oxidation from 34% to 86% at an HCl concentration of 300 ppmv. Fry et al. (2007) concluded that the chlorine radical concentration is sensitive to temperature, and therefore that oxidation kinetics are also dependent on quench rate. Building upon the work of Niksa et al. (2001), Fry (2008) modeled the effect of quench rate on Hg oxidation with chlorine species as oxidants. The model predicted that a high quench rate produced a greater extent of oxidation because of the longer residence time at temperatures below 650 ◦C and the presence of super-equilibrium concentrations of Cl radicals. 19 2.2.1.2 Bromine-Based Homogeneous Hg Oxidation Otten et al. (2011) concluded that, on an equivalent molar basis, Br proves more effective than other halogens (chlorine, fluoride, and iodide) in promoting homogeneous oxidation of Hg in coal combustion flue gases. The experiments conducted by Otten et. al. (2011) showed that the concentrations of HBr and Br are comparable at flame temperatures and that as the flue gas cools, the concentration of Br radicals equals that of HBr. In a study conducted by Jin et al. (2011) of halogen species during the combustion of municipal waste, some of which contained substantial concentrations of bromine (7 wt%), the researchers determined that the concentrations of HBr and Br2 were almost equal. The data seemed to suggest that higher temperatures and O2 levels tended to shift the bromine towards Br2 at the expense of HBr. Jin et al. (2011) also found, during the combustion of high bromine content municipal waste, that the presence of SO2 decreased the amount of Br2 in combustion products. Vosteen et al. (2006) reported that the following reactions are important for Hg oxidation by bromine: 4HBr + O2 ↔ 2H2O + 2Br2 (R10) SO2 + Br2 + H2O ↔ SO3 + 2HBr (R11) SO2 + Br2 + 2H2O ↔ H2SO4 + 2HBr (R12) Hg + Br2 ↔ HgBr2 (R13) Niksa et al. (2010) suggested that knowledge of intermediate reactions increases understanding of the ability of bromine radicals to homogeneously oxidize Hg and suggested these additional elementary reactions: Hg + Br ↔ HgBr (R14) 20 HgBr + Br2 ↔ HgBr2 + Br (R15) These reactions suggest that, similar to chlorine, bromine radical chemistry plays a vital role in homogeneous Hg oxidation by bromine. Vosteen et al. (2006) concluded that unlike chlorine radicals, bromine radicals are suppressed to a lesser extent by the presence of SO2, and that therefore, Equations R11 and R12 become less important. Although SO2 consumes Br2, it does so to a lesser extent when compared the effect of SO2 to Cl2. Niksa et al. (2010), Vosteen et al. (2006), Silcox et al. (2008), and Otten et al. (2011) all concluded that Br2 and Br radicals exist in the flue gas in rather large quantities and that, with the lack of sensitivity of bromine species to SO2, sufficient Br2 and Br radicals should exist to promote homogeneous Hg oxidation. In contrast, Buitrago et al. (2010) concluded from bench-scale tests that the presence of SO2 resulted in considerable reduction in homogeneous Hg oxidation by bromine when SO2 was present at concentrations as low as 50 ppmv. Niksa et al. (2010) reported that, in comparison with Cl, Br more effectively oxidizes Hg because HBr disassociates into more reactive species (i.e. Br2 and Br radicals) to a greater extent than HCl under typical post-flame conditions. Buitrago et al. (2010) reported that bromine was shown to be significantly more effective for post-flame, homogeneous oxidation of Hg than chlorine. Thermodynamic modeling performed by Vosteen et al. (2006) showed that, at 1000 ◦C, Br2 becomes the dominant bromine species. Results of similar studies by Silcox et al. (2008) revealed that Br2 became the dominant bromine species at flue gas temperatures below 400 ◦C. Silcox et al. (2008) conducted homogeneous oxidation experiments at 350 ◦C, to ascertain the relationship between Hg oxidation and bromine concentration. Silcox et al. 21 (2008) determined that 3.5 ppmv of bromine (as HBr) resulted in 10% Hg oxidation. Increasing the flue gas concentration of HBr to 10 ppmv increased Hg oxidation to 25%, and increasing the HBr concentration to 20 ppmv resulted in 60% Hg oxidation. At the highest HBr concentration of 45 ppmv, Hg oxidation was 80%. Otten et al. (2011) performed similar experiments, but excluded SO2 from the flue gas and observed similar extents of Hg oxidation. At a flue gas HBr concentration of 25 ppmv, Hg oxidation was found to be 40%. Similarly, when the HBr concentration was increased to 50 ppmv, Hg oxidation increased to 80% (Otten et al., 2011). Vosteen (2003) reported that in order to achieve 100% Hg oxidation by introducing a bromine compound, the bromine must be added in a mass ratio of bromine to Hg mass ratio (Br/Hg) in the coal of 100 to 10,000. A typical concentration of Hg in bituminous and subbituminous coals from the United States is 50 to 200 wt ppb. The guideline provided by Vosteen (2003) suggests that Br addition rates of 5 to 200 wt ppm in the dry coal would be required for bromine based homogenous Hg oxidation. Silcox et al. (2008) also investigated the effect of flue gas quench rate on Hg oxidation and their results indicated that a lower quench rate (-220 K/s) resulted in a higher extent of Hg oxidation at equivalent HBr concentrations. For example, at 20 ppmv of HBr ,the lower quench rate (-220 K/s) resulted in Hg oxidation level of 75%; however, at a higher quench rate (-440 K/s), only 50% oxidation was observed. 2.2.2 Heterogeneous Oxidation The oxidation of Hg does occur on the surface of particles. The surface acts as a catalyst to assist the chemical reaction. The Swedish chemist Jöns Jacob Berzelius, in 22 1836, first coined the term catalyst and defined it as any substance that directly alters the rate of a chemical reaction without entering into the net chemical reaction itself (Dartmouth, 2012). Flue gas contains a number of surfaces that have been demonstrated to catalyze the oxidation of Hg. Niksa and Fujiwara (2005) postulated that unburned carbon and fly ash can act as a catalyst to oxidize Hg. Engineered materials such as SCR catalyst, activated carbon particles, iron (Fe) particles, and noble metals such as gold and palladium can be introduced into the flue gas for that purpose. In essence, engineered materials can be used to oxidize Hg. Feely et al. (2003) reported that the combination of SCR and wet FGD showed promise for reducing Hg emissions and showed that the Hg emissions from coal-fired units with SCR and wet FGD were lower than those from units that did not have that combination of equipment. In short, the SCR promotes the oxidation of Hg, and the wet FGD scrubs the oxidized Hg from the flue gas. 2.2.2.1 SCR Reactors New regulations promulgated by the EPA over the past two decades have required that utilities operating coal-fired power plants install new technology to reduce nitrogen oxides (NOx) emissions. Many utilities have installed SCR reactors that can reduce NOx emissions up to 95%. In the process of reducing NOx, NH3 is added to the flue gas in the presence of an engineered catalyst. The NOx is transformed by reaction with NH3 into nitrogen and water vapor. The chemical reactions of the process are described by the following equations, (Sloss et al., 1992): 4NO + 4NH3 + O2 ↔ 4N2 + 6H2O (R16) NO + NO2 + 2NH3 ↔ N2 + 3H2O (R17) 23 2NO2 + 4NH3 + O2 ↔ 3N2 + 6H20 (R18) 6NO2 + 8NH3 ↔ 7N2 + 12H2O (R19) NH3, shown in Equations R16 – R19, is adsorbed onto the catalyst surface. The NOx diffuses from the gas stream to the surface of the catalyst, where it reacts to form the products H2O and N2. The products desorb, and the surface returns to its prior state for the process to repeat itself. The optimum temperature range for the reactions is 300 to 400 ◦C. Catalysts are designed to optimize the NOx and NH3 reaction while minimizing other reactions such as the oxidation of SO2 to SO3. This selectivity typically translates to a less active catalyst. SCR NOx reduction efficiency is a function of: inlet NOx concentration, flue gas temperature, the ratio of NH3 to NOx; oxygen concentration; various catalyst properties and reactor design characteristics, (e.g., space velocity; bulk catalyst composition; surface catalyst composition; and catalyst structural design). Each SCR is designed specifically for an individual situation in which a delicate balance ensures a high NOx removal efficiency within the desired constraints such as SO2 to SO3 oxidation. Table 2.1 provides a summary of the key design parameters for a SCR installation. The operation of an SCR system is typically evaluated on two major components: its ability to reduce NOx emissions and its ability to properly consume the injected NH3. Any NH3 that leaves the system is referred to as NH3 slip. In a typical SCR design, acceptable NH3 concentrations leaving the reactor are equal to or less than 2 ppm. Any unreacted NH3 can cause difficulties in plant operations. For example, unreacted NH3 could react with SO3 to form ammonium bisulfate (NH4HSO4), a sticky substance that could foul or corrode the air heater. The design of SCR ensures that the NH3 not reacted 24 in the systems is relatively low. Pritchard et al. (1995) reported that NH3 slip levels should not exceed 2 to 5 ppm at the end of the useful life of the catalyst. Although well designed catalyst is important in this regard, Pritchard et al. (1995) also discussed other ways to ensure the proper management of NH3 levels in the SCR, including both matching the NOx profile with the NH3 injection profile through lance injection design and maintaining control of the NH3 injection grid on a daily basis. The interplay between NH3 and Hg oxidation is important and will be discussed in further detail later in this section. SCR catalyst, a major component of the SCR system, is made from special materials for their specific properties. Sloss et al. (1992) reported that the SCR catalyst market is dominated by a titanium-oxide (TiO2) based catalyst in which vanadium pentoxide (V2O5) and tungsten oxide (WO3) are added to increase activity. Although many catalysts share common building blocks (TiO2, V2O5, WO3, and MoO3), the final formulation of a specific catalyst is dictated by individual plant flue gas composition and operating conditions. Catalyst activity degrades with time, and deactivation can occur via mechanical means (erosion and plugging) or chemical means (deposition). Catalyst activity decreases because of damage or blockage of active sites (i.e., the locations at which the chemical reaction occurs). Erosion and plugging cause the active sites to disappear or become inaccessible, meaning that they are covered and are no longer available to serve as an active site. During chemical degradation, active sites are blocked or deactivated by compounds such as arsenic (As), potassium (K), and calcium (Ca), and can no longer serve as active catalyst materials. 25 Table 2.1 SCR Key Design Parameters Description Symbol Units Formula Notes Reduction efficiency η n/a molNOx,in ! molNOx,out molNOx,in Flue gas flow Qg m3/h n/a Gas volume flow at treatment temperature Catalyst volume Vc m3 n/a SCR system design parameter Catalyst area Ac m2 n/a SCR system design parameter Catalyst specific surface area Asp m2/m3 n/a SCR catalyst design parameter Crucial SCR design parameter (typically 1,000– 3,000 h-1) Molar reduction efficiency Space velocity SV 1/h !! !! Area velocity AV m/h Qg Vc Asp Flow rate through a catalyst area divided by the surface area of the passages Laboratory measurement of catalyst ability to remove NOx from simulated flue gas Activity K n/a !Av ln(1! ! ) Original Activity K0 n/a n/a Activity Degradation n/a n/a K K0 Rector potential RP n/a ! !" Laboratory measured activity before catalyst is exposed to flue gas Used to benchmark SCR performance over time Measure of the overall ability of the SCR to reduce NOx Note: Table was created with information from Sloss et al. (1992) and Muzio et al. (2008) Jensen-Holm (2007) for instance, reported that alkali metal aerosols containing sodium (Na) and potassium (K) are of prime concern because the aerosols adhere to the catalyst surface and the elements are transported to the active sites by surface diffusion. 26 The impact of catalyst poisoning relates directly to the coal being burned at the site and the location at which the SCR is installed. SCRs are installed in three configurations: (1) a high-dust SCR installed just downstream of the boiler, (2) a lowdust SCR, installed downstream of a hot-side electrostatic precipitator, and (3) a tail-end SCR which is installed downstream of the wet FGD. In the tail-end configuration, the flue gas is reheated between 300 to 400 °C. The high-dust SCR has the largest potential for catalyst deactivation because of both physical plugging and chemical degradation can occur. The low-dust SCR is less susceptible to physical plugging and the tail-end SCR carries the lowest potential for catalyst degradation because the upstream environmental control equipment (i.e. cold-side ESP and wet FGD) removes contaminants. For Hg oxidation, the tail-end SCR is not important because any oxidized Hg created would be discharged to the atmosphere. A basic knowledge of SCR operations for NOx removal may provide some understanding of the SCR’s ability to oxidize Hg. Current SCRs are optimized to remove NOx and consideration is not given to Hg oxidation. At this time, the SCRs ability to oxidize Hg is an ancillary benefit. The next sections contain discussions of key technical terms to enhance understanding of the symbiotic relationship between NOx removal and Hg oxidation. 2.2.2.1.1 Hg Oxidation Reaction Mechanisms Currently no clear fundamental understanding exists of the mechanism causing Hg oxidation within an SCR catalyst. Authors of the various scientific studies presented 27 here discussed three main possible reaction mechanisms: Eley-Rideal, LangmuirHinshelwood, and Mars-Maessen. The Eley-Rideal mechanism describes the interaction between an adsorbed species and a gas-phase species according to the following reactions (Tong 2009). A(g) ↔ A(ads) (R20) A(ads) + B(g) ↔ AB(g) (R21) Senior (2006) performed extensive computer modeling using the Eley-Rideal mechanism in combination with publicly and privately held, full-scale SCR operational data and concluded that the model provided Hg oxidation predictive results that compared favorably with actual data from eight different catalysts, including both monolith and plate catalysts. Hong et al. (2010) experimentally determined that HCl is adsorbed on the SCR surface and reacts with gas phase Hg to form HgCl2. Hong et al. (2010) reported that HCl competes with NH3 for the active sites and that NH3 was preferentially adsorbed on the catalyst. In earlier work Granite and Presto (2006) found that NH3 adsorbs strongly to the V2O5 active sites. The Eiley-Rideal mechanism dictates that the NH3 concentration must decrease before sufficient Hg oxidation can occur, which assumes that NH3 and HCl are competing for the same active sites. A sufficient gas phase concentration of halogens (i.e., HCl, Cl2, Br2, HBr) is needed for the Hg oxidation reaction to occur. The production of Cl2 from adsorbed HCl proceeds under the Deacon reaction as described in Equation R2. The adsorption of HCl onto the catalyst surface is an important step in the oxidation of Hg. Dranga et al. (2012) provided the following equations to describe the Eley-Rideal mechanism for Cl and Hg: 2HCl(g) + 2V-O-V(s) ↔ 2V-OH-V-Cl(s) 28 (R22) 2V-OH-V-Cl(s) + Hg(g) ↔ 2V-OH-V(s) + HgCl2(g) 2V-OH-V(s) + ½ O2(g) ↔ 2V-O-V(s) + H2O(g) (R23) (R24) Dranga et al. (2012) found the Eley-Rideal mechanism highly unlikely to be the governing mechanism, on the basis of their analysis of the available experimental results. Their conclusion was grounded in the fact that Hg was found to adsorb onto the catalyst surface. According to the second possible reaction mechanism, the LangmuirHinshelwood mechanism, reaction occurs between two adsorbed species on the surface of a catalyst. Piling and Seakins (1995) described this mechanism by the following equations: A(g) ↔ A(ads) (R25) B(g) ↔ B(ads) (R26) A(ads) + B(ads) ↔ AB(ads) (R27) AB(ads) ↔ AB(g) (R28) He (2009) conducted surface analyses using X-ray photoelectron spectroscopy (XPS) and fourier transform infrared spectroscopy (FTIR) of SCR catalyst and confirmed the presence of HCl on the surface. Experiments showed that the catalyst adsorbed Hg when HCl was absent in the flue gas. When HCl was added to the flue gas, Hg was observed to desorb, indicating weak adsorption of Hg to the vanadia active sites. Both observations support the Langmuir-Hinshelwood mechanism as a plausible reaction process for Hg oxidation. According to the mechanisms shown in Equations R29 to R32, HCl and Hg first adsorb onto vanadia sites, HCl and Hg reacts to form intermediate species which react with Cl to form HgCl2 and V-OH species. The HgCl2 then desorbs to the flue gas 29 and the re-oxidation of the V-OH species by oxygen follows to form V=O and H2O (He, 2009). He (2009) proposed the following reactions to describe Hg oxidation via the Langmuir-Hinshelwood mechanism. Hg(ads) + Cl(ads) ↔ HgCl(ads) (R29) HgCl(ads) + Cl(ads) ↔ HgCl2(g) (R30) HgCl(ads) + HCl(ads) ↔ HgCl2(g) + H (R31) HgCl(ads) + Cl2(ads) ↔ HgCl2(g) + Cl (R32) In other experiments, Qiao (2009) suggested that an intermediate reaction takes place once HCl and Hg are adsorbed onto the vanadia active site. Qiao (2009) also found that the activation energy for the reaction with Cl2 was lower than the activation energy required for the HCl reaction. Thus, Hg oxidation behavior, while achievable with HCl, might proceed to a greater extent in the presence of Cl2. The chlorine Deacon reaction takes place at about 350 to 450 °C in the presence of copper, chromium, vanadium, and ruthenium(IV) oxide catalyst (Dranga et al., 2012). An increase in Cl or Cl2, transformed from HCl, could occur if a catalyst containing copper (Cu) or cadmium (Cd) were present. Hranisavljevic and Fontijn (1997) showed by experiment that Cl radical production can occur in flue gas when HCl or Cl2 is present along with Cd. Additional experiments by Hisham (1995) demonstrated the ability of Cu to promote the production of Cl2 from HCl in accordance with Equation R2. After analyzing results for Hg oxidation in the presence of noble metal catalysts, Granite and Presto (2008) suggested that a Langmuir-Hinshelwood mechanism might explain the reaction kinetics in the presence of a platinum-based catalyst. Eom et al. (2008) used transmission electron microscopy with energy dispersive X-ray (TEM-EDX) 30 analyses and X-ray photoelectron spectroscopy (XPS) to verify reaction pathways on the surface of SCR catalyst used for Hg oxidation. The study revealed that elemental Hg and HCl were both present on the surface of the catalyst. Eom et al. (2008) observed the presence of multiple layers of HgCl2 on the surface. This finding clearly indicates that the Langmuir-Hinshelwood reaction pathway is plausible. Ghorishi et al. (2005) found experimentally that higher levels of CaO in the coal led to slightly lower rates of heterogeneous Hg oxidation. These lower rates could result from the consumption of HCl through chemical reaction with CaO to form CaCl2. The consumption of available HCl by CaO could be important at plants that burn PRB coals with fly-ashes high in calcium (up to 20 wt% Ca). Dranga et al. (2012) postulated, from a comprehensive review of the literature, that the Mars-Maessen mechanism is the most likely pathway for Hg oxidation in the presence of a metal, oxide-based catalyst. In this mechanism, elemental Hg is first adsorbed onto the catalyst surface, and then reacts with lattice oxygen from the catalyst to form an adsorbed mercuric oxide. The catalyst surface is re-oxidized with gaseous oxygen. The HgO(ads) reacts with HCl or HBr to form the volatile Hg halides, which are released from the catalyst surface. Liu (2011) postulated the following Mars-Maessen reactions for a CoO/TiO2 metal oxide catalyst: Hg(g) ↔ Hg(ads) (R33) Hg(ads) + CoxOy(s) ↔ HgO-CoxOy-1(s) (R34) HgO-CoxOy-1(s) + ½O2 ↔ HgO(ads) + CoxOy(s) (R35) HgO(ads) + 2HCl(g) ↔ HgCl2(g) + H2O (R36) HgO(ads) + 2HBr(g) ↔ HgBr2(g) + H2O (R37) 31 Straube et al. (2008) suggested a similar set of reactions for oxidation on active vanadium sites. Hg(ads) + catalyst – O ↔ HgO(ads) (R38) HgO(ads) + 2HCl(g) ↔ HgCl2(g) + H2O (R39) Straube et al. (2008) postulated that Hg is deposited on the surface of the catalyst at an active vanadium site, where it reacts with O2 to form an intermediate species. The intermediate species reacts with HCl to form the volatile HgCl2. In a study of nanoFe2O3-based oxidation catalysts, Kong et al. (2011) proposed that the first step of the catalytic reaction consists of losing one oxygen atom from Fe2O3 to adsorbed elemental Hg to form HgO. The proposed mechanism by Kong (2011) is consistent with the Mars Maessen reaction pathway. Lee and Bae (2009) conducted X-ray photoelectron spectroscopy analysis of nano-sized catalyst after the removal of elemental Hg during experiments. The analysis revealed that the elemental Hg had been transformed to HgO by vanadates, a finding which is consistent with the Mars-Maessen mechanism. During the experiments, oxidized Hg was not liberated as HgO, but rather remained captured on the surface (Lee and Bae, 2009). Gutberlet et al. (2008) hypothesized that the NOx reaction causes the reduction of V5+ to V4+ and that the active site typically is re-oxidized by oxygen, but might possibly be oxidized by oxidized Hg. The Gutberlet (2008) hypotheses supports Mars-Maessen as a plausible mechanism. It is plausible that all three mechanisms occur within the SCR for Hg oxidation to occur. 32 2.2.2.1.2 SCR Governing Factors The oxidation of Hg within an SCR reactor depends on a number of factors. The design of the SCR catalyst itself plays a major part in its ability to produce high levels of oxidized Hg. SCR catalysts are generally designed for the coal application by using titanium dioxide (TiO2), supported vanadium pentoxide (V2O5) catalyst with tungsten (WO3) or molybdenum trioxide (MoO3) as a promoter. Laudal et al. (2002) reported that laboratory-scale testing indicated that metal oxides, including V2O5 and TiO2, promote the conversion of elemental Hg to oxidized Hg in simple flue gas mixtures. Straube et al. (2008) reported that because vanadia is active not only in the reduction of NOx but also in the undesired oxidation of SO2 to SO3, its content in SCR catalyst is generally kept low (i.e., 0.3 to 1.5 wt%). Casagrande (1999) suggested that, as an alternative to vanadia, WO3 could be employed in larger amounts (near 10 wt%) for enhanced Hg oxidation because WO3, a chemical promoter, also improves the mechanical and structural properties of the catalyst. Hong et al. (2010) performed bench-scale experiments with simulated flue gas and commercially available catalyst and found that a catalyst containing 1.68 wt% V2O5 and 7.6 wt%. WO3 achieved 100% Hg oxidation in the presence of 50 ppmv HCl and an NH3/NOx molar ratio of 0.8. Dranga et al. (2012) reported that 90% mercury oxidation was achieved when the V2O5 content was 1.1 to 1.2 wt% but that Hg oxidation was only 40% when the V2O5 content was 0.5 wt%. Gutberlet et al. (2008) provided information from bench-scale experiments that revealed 10% to 30% Hg oxidation with SCR catalyst that contained less than 0.75% V2O5 content. This rate was achieved with 60 ppmv HCl in the flue gas at 390 °C and without NH3, NO, or SO2 in the flue gas. This environment would have provided optimum conditions for Hg 33 oxidation. Under the same flue gas conditions, the V2O5 content was increased. With V2O5 content of 1 wt%, the Hg oxidation was above 50% and with V2O5 content of 2.5 wt%, the Hg oxidation was 90% (Gutberlet et al., 2008). Straube (2008) concluded, through experimental results, that Hg oxidation depends on the V2O5 content of SCR catalyst. In addition to the chemical makeup of the catalyst, its structural characteristics are also important to its ability to promote Hg oxidation. Gutberlet et al. (2008) found that SCR catalyst pitch significantly influenced Hg oxidation. The SCR pitch is defined as the catalyst wall thickness plus the width of the channel (Drabal et al., 1996). Gutberlet et al. (2008) found that smaller pitch was beneficial for Hg oxidation. Because mass transfer of the gaseous species to the catalyst surface is diffusion limited, a smaller pitch would increase the diffusion rate. However, Drabal et al. (1996) observed that smaller pitch results in higher pressure drop across the SCR reactor. An optimum balance likely exists among catalyst pitch, Hg oxidation, and process pressure drop. Gutberlet et al. (2008) also found that cell wall thickness exerted no effect on Hg oxidation. Svachula et al. (1993) reported that increasing wall thickness increased the oxidation of SO2 to SO3. Combination of the conclusions from Gutberlet et al. (2008) and Svachula (1993) likely means that SO2 to SO3 conversion could be managed by changing catalyst wall thickness without any significant effect on Hg Oxidation. Senior (2006) predicted, in modeling studies, that with NH3 present, plate and monolith catalysts would have similar levels of Hg oxidation in low-chlorine flue gas, but that the plate catalyst would have levels of Hg oxidation higher than those of the monolith catalyst when higher levels of HCl are present in the flue gas. 34 Laudal et al. (2002), suggested that catalyst space velocity was important in Hg oxidation and examined Hg oxidation behavior at four full-scale sites equipped with SCRs. All four plants burned coal having chlorine contents greater than 60 wt ppm, with a maximum of 1,910 wt ppm. Laudal et al. (2002) observed that Hg oxidation on a unit with an SCR space velocity of 3,930 h-1 was lower than that of another unit that had lower concentrations of chlorine in the coal and a space velocity of 1,800 h-1. This finding shows that catalyst volume is important to Hg oxidation because a higher space velocity translates to a lower volume of catalyst per unit flue gas volume. In another analysis of full-scale data and selected bench-scale tests, Senior and Linjewile (2004) showed that units having space velocities below 2,000 h-1 had Hg oxidation values >70%, much higher than those of SCRs with space velocities above 4,000 h-1, which achieved less than 40% Hg oxidation. Results of equilibrium modeling studies conducted by Senior (2006) revealed that Hg oxidation was a function of space velocity, with the lower values resulting in higher Hg oxidation levels for the same flue gas conditions. Decreasing space velocity requires an increase in installed catalyst volume. Once a SCR has been built, the ability to increase catalyst volume is limited at best. For optimum Hg oxidation, it is best that an SCR be designed initially with a low space velocity. The characteristics of the flue gas to which the SCR catalyst is exposed are other important factors in achieving high levels of Hg oxidation. One of the most important properties of the flue gas is the concentration of the halogen(s). These halogens act as Hg oxidants and must be present in sufficient concentration for Hg oxidation to reach the desired level. Dranga et al. (2012) observed that the activity of almost all Hg oxidation catalysts depends on a certain concentration of HCl or HBr in the flue gas to be treated. 35 Senior (2004) provided data showing that a high level of Hg oxidation was achievable when the Cl content of the coal exceeded 500 wt ppm. As the Cl content increased, Hg oxidation continued to increase asymptotically toward 100%. Catalysts do not effectively oxidize Hg when the coal contains low levels of halogens. Gutberlet et al. (2008) stated that, in comparison to HCl, HBr ten times more effectively oxidized Hg. In laboratory tests, the amount of HBr needed to achieve similar oxidation rates was one-tenth the amount of HCl required. Vosteen et al. (2006) reported that HBr proved to be more effective at oxidizing Hg because bromine radicals are more prevalent than chlorine radicals under similar conditions. Vosteen et al. (2006) also concluded that this behavior would be true for all types of coals, including those containing high levels of sulfur, because, unlike chlorine radicals, bromine radicals are not consumed when exposed to SO2. Vosteen (2003) concluded that Hg oxidation in the presence of bromine would be complete with a Br/Hg ratio (lb/lb) of 100:1 to 10,000:1. Cao et al. (2008), Eswaran and Stenger (2005), Ghorishi (2003), He (2009), Hong et al. (2010), Laudal et al. (2002), Senior (2006) and Straube (2007), have shown during bench-scale and full-scale tests, that Hg oxidation increased as the HCl concentration increased. Cao (2008), Niksa (2010), and Vosteen et al. (2006) found during both bench-scale tests and Hg oxidation chemistry modeling, that Hg oxidation increased as the concentration of HBr and HI in the flue gas increased. Cao (2008) concluded that Hg oxidation was enhanced by the addition of hydrogen halides in the following order: HBr, HI, then HCl and HF; which means that is HBr is more effective than HF, HI, and HCl in oxidizing Hg. 36 In addition to the halogen content, other flue gas constituents directly affect the ability of the SCR catalyst to promote Hg oxidation. For instance, Tong (2009) observed in bench-scale studies, that carbon monoxide (CO) inhibits Hg oxidation when the HCl content of the flue gas is below 10 ppmv. Zhuang et al. (2007) concluded that SO2 and SO3 influenced Hg oxidation because they compete with HCl for SCR catalyst active sites. Lei et al. (2008) proposed that, in comparison with SO2, Hg bonded only weakly to the active sites and that SO2 would be preferentially adsorbed. The temperature of the flue gas is another important operating parameter. SCRs operate in the optimum temperature range for the deNOx reaction, which is between 300 and 400 °C (Sloss et al. 1992). Granite and Presto (2006) reported that the chlorine Deacon reaction occurs at flue gas temperatures of 300 to 400 °C, the same temperature window of the SCR NOx–NH3 reaction. Hong et al. (2010), who discovered during bench-scale testing that Hg oxidation was sensitive to flue gas temperature, conducted testing at three temperatures (250, 300, and 350 °C), with HCl concentration of 50 ppmv and without NH3 and NOx in the flue gas. Hong et al. (2010) found that the highest Hg oxidation (70%) occurred at the temperature of 350 °C, and that the lowest oxidation (10%) was observed at the temperature of 250 °C. During a study of Hg oxidation behavior in full-scale SCRs, Senior and Linjewile (2004) found that when the effects of HCl concentration and coal sulfur content were taken into account, a clear correlation existed between higher flue gas temperatures and lower Hg oxidation within the SCR. Senior and Linjewile (2004) observed the highest level of Hg oxidation at a flue gas temperature of 330 °C. In a later heterogeneous oxidation modeling study, Senior (2006) found that, in comparison with performance at 370 °C, higher extents of Hg oxidation 37 occurred at flue gas temperatures of 320 °C. Lee and Bae (2009) suggested that at higher SCR temperatures, Hg might adsorb less readily on the SCR catalyst. To a large extent, NH3 concentrations in the SCR inhibit the ability of the SCR to catalyze the Hg oxidation reaction. In a study of Hg oxidation data from a bench-scale SCR, Senior and Linjewile (2004) concluded that oxidation decreased in the presence of NH3. Hong et al. (2010) conducted bench-scale tests experiments with constant HCl, NOx, and Hg concentrations and varied the NH3 injection rate by varying the α ratio. The testing revealed that, for lower values of α (<0.4), Hg oxidation was 100%. The Hg oxidation efficiency decreased as the α ratio increased, with a final Hg oxidation efficiency of 65% at a ratio of α =1.0. In a bench-scale study, Gutberlet et al. (2008) also observed that increasing the α ratio negatively impacted Hg oxidation. However, consideration must be given to the fact that the NH3 concentration does not remain constant in an SCR reactor. As the flue gas travels through the reactor, NH3 is consumed in its reaction with NOx. In fact, although inlet levels of NH3 can exceed 500 ppmv, the outlet NH3 concentration is typically below 2 ppmv (Jensen-Holm, 2007). The α ratio may not be the ideal parameter to monitor. Rather, the evaluation of local NH3 concentration may be the more appropriate condition to consider. Dragna (2012) developed the diagram shown in Figure 2.1 to illustrate the interplay among the NOx reaction, NH3 concentration, and Hg oxidation. As NH3 is consumed in the SCR by the deNOx reactions, more active vanadia sites become available on the catalyst for adsorption of HCl and Hg. Once adsorbed, the Hg can be oxidized via the Languimuir-Hilsherwood mechanism (by reaction with HCl or HBr) or via the Mars-Maessen mechanism (by reaction with lattice oxygen). In either case, the 38 consumption of NH3, or absence of NH3, promotes Hg oxidation. Hong et al. (2010) concluded that injection of NH3seems to cause Hg to desorb from the catalyst surface and that NH3 preferentially adsorbs onto the SCR catalyst surface when both NH3 and Hg components are present. Niksa and Fujiwara (2005) concluded that HCl competes for active sites with NH3, but this effect decreases as NH3 is consumed in the reactor. Figure 2.1 Schematic diagram of the changes in flue gas composition in an SCR Note: From “Oxidation Catalysts for Elemental Mercury in Flue Gases—A Review” by B. A. Dranga, L. Lazar and H. Koeser, 2012, Catalyst, 2, p. 158. Copyright 2012 by MPDI. Reprinted with permission. The age of the catalyst (i.e., how long it has been exposed to flue gas) also requires consideration. Different types of degradation of an SCR catalyst reduce its useful lifetime (Sloss et al., 1992). The degradation is quantified through laboratory measurement of a catalyst’s ability to reduce NOx emissions. The initial ability is defined as the original catalyst activity (Ko). The measurement is repeated and new values are computed (K). The relative ratio is computed (K/Ko). The catalyst reaction 39 activity (K) degrades over time (i.e. K/K0 <1), for a number of reasons: poisoning, deposition of solids, sintering, and erosion (Crowe and Ichiki, 2002). Eswaran and Stenger (2008), in bench-scale Hg oxidation tests with SCR catalyst and different flue gas exposure times (1,030 h, 1,450 h and 3,300 h), concluded that increasing catalyst age reduces Hg oxidation activity. In laboratory tests of exposed SCR catalyst, Gutberlet et al. (2008) observed behavior similar to that reported by Eswaran and Stenger (2008). The halogen concentration is another important factor to consider, Cao et al. (2008) reported that 3 ppmv HBr produced 80% oxidized Hg in a bench-scale SCR with PRB simulated flue gas. The tests were conducted at 360 °C, space velocity of 3,600 h-1, and catalyst containing of V2O5, WO3, and TiO2. Lee et al. (2008) reported that 20 ppmv HCl produced 88% oxidized Hg in a bench-scale reactor under simulated PRB flue gas conditions. The tests were conducted at 350 °C, space velocity of 2000 h-1, and the flue gas did not contain fly ash. Lee et al. (2008) also reported that the inclusion of fly ash reduced Hg oxidation by approximately 20%, and that the absence of NH3 resulted in higher levels of oxidized Hg. 2.2.2.2 Native Heterogeneous Oxidation The heterogeneous oxidation of Hg is dominated by in-situ fly ash and unburned carbon particles when a SCR is not present. During modeling studies to predict the oxidation of Hg, Niksa et al. (2002) modeled the extent of Hg oxidation in the exhausts from a bench-scale combustor fired with five different coals, concluded that unburned carbon played an essential role in heterogeneous Hg oxidation. Niska et al. (2002) found, in one test case, that sufficient concentrations of both chlorine and unburned carbon 40 produced a high rate of Hg oxidation (i.e., 90% oxidation). Although acknowledging the roles of the amount and characteristics of unburned carbon particles (size, total surface area) in heterogeneous oxidation, Niksa et al. (2002) also indicated that the concentrations of CO, hydrocarbons, H2O, O2, NOx, and SOx were important. Zhao et al. (2010), in a fixed-bed study of fly ash as an Hg oxidation catalyst, found Hg oxidation levels from 10.3% to 27.5% and reported that the Hg oxidation process was a byproduct of adsorption of Hg and an oxidant (i.e., HCl). Zhao et al. (2010) reported that, similar to the heterogeneous oxidation occurring in an SCR, heterogeneous oxidation by native fly ash and unburned carbon particles followed either an Eley-Rideal mechanism or a Mars-Maessen mechanism. In a fixed-bed study of fly ash as an Hg oxidation catalyst, Lee et al. (1997) found that CuO and Fe2O3 caused significant catalytic activity for oxidation of elemental Hg when the simulated flue gas contained 50 ppmv of HCl and when the gas temperature ranged from 150 to 200 °C. Lee et al. (1997) reported that Hg oxidation levels reached 95% when fly ash contained either 14 wt% Fe2O3 or 1.0 wt% CuO, levels of both oxides that are much higher than those typically found in fly ashes. The results also showed that SO2 and H2O decreased the Hg oxidation effectiveness of both oxides but did so to a lesser degree with the fly ash containing 1 wt% CuO. Bhardwaj et al. (2009) found, during fixed-bed fly ash oxidation testing, that increasing levels of unburned carbon and fly ash surface area resulted in improved Hg oxidation and that, at unburned carbon levels of 40 wt%, 150 °C, and 50 ppmv HCl, Hg oxidation levels of 42% were achievable. During fixed-bed oxidation tests with fly ash from PRB and bituminous coals, Norton (2002) observed that oxidation levels up to 32% were achievable in flue gas at 180 °C, 1600 ppmv SO2, and 50 ppmv 41 HCl. Norton (1999) observed that the ash itself did not play a critical role in oxidation, but might constitute a contributing factor but that the flue gas matrix itself was more critical to Hg oxidation. The literature suggests that native heterogeneous Hg oxidation can occur but that the level of oxidation depends on many factors. Although high levels of oxidation are observed under ideal conditions, native heterogeneous oxidation is likely to be too dependent on fly ash characteristics such as Fe2O3 content, CuO content, and unburned carbon content to be considered a reliable means of Hg oxidation. 2.3 Hg Capture in Wet FGD The ability of a wet FGD to remove Hg from flue gas is directly related to the speciation of Hg compounds entering the wet FGD and to the dynamic state of the Hg until it is removed from the wet FGD. For example, if the flue gas at the wet FGD inlet contains HgCl2 (a water soluble form), the exiting flue gas will be free of HgCl2, which is captured in the wet FGD sump. As long as the compound does not change chemically, HgCl2 should be discharged along with the wet FGD blowdown or with the gypsum. Additional important reactions likely take place within the wet FGD sump that govern the final state of the Hg. There are three likely outcomes or combinations of outcomes: (1) captured Hg stays in solution and is discharged along with the wet FGD blowdown, (2) captured Hg is reduced to its elemental form, is re-introduced into the flue gas stream, and is emitted from the stack, and (3) captured Hg is adsorbed or precipitated with the gypsum or other solids and exits the wet FGD along with the gypsum. In a wet FGD, all three scenarios may occur simultaneously to varying degrees. 42 2.3.1 Wet FGD Hg Removal Performance Data Mejj (1991), in a study of Hg emissions from boilers equipped with wet FGDs in the Netherlands, reported that 50% to 70% of the Hg was removed from the flue gas across the wet FGD. The boilers studied by Mejj (1991) were not equipped with SCRs to control NOx, a fact that likely limited the oxidized Hg present and resulted in lower removals of Hg. In a study of EPA’s Information Collection Request (EPA ICR) data, Senior (2001) found a removal rate of 90% of the measured oxidized Hg across wet FGDs. The EPA ICR data included results from 19 units equipped with wet FGD and thus provided a good, diverse dataset from which Senior (2001) drew those conclusions. Senior (2007) later reported that elemental Hg emission sometimes increased across a wet FGD. In a study of Hg removal at ten power plants, eight of which were equipped with wet FGDs, Withum (2006) found that the SCR-wet FGD combination removed a substantial fraction of Hg from the flue gas. The coal-to-stack removals ranged from 65% to 97% for units equipped with an SCR and from 57% to 87% for units without an SCR. Withum (2006) reported that oxidized Hg removal across the wet FGD was not a function of wet FGD type. Jingjing et al. (2009) also reported that oxidized Hg removal was independent of wet FGD type. In the Withum (2006) study, the results revealed that, in some instances, the elemental Hg concentration in flue gas actually increased across the wet FGD. Such an increase is referred to as Hg reemission because captured Hg is actually reemitted from the FGD sump. During a reemission event, a chemical reaction within the wet FGD results in the transformation of absorbed oxidized Hg to elemental Hg. Because of its low solubility, elemental Hg is desorbed from the liquid to the gas and emitted from the stack (Omine et al., 2012). Blythe et al. (2005), in a pilot study of low- 43 temperature oxidation catalyst, discovered that 100% of oxidized Hg was removed in the wet FGD and that overall Hg removal was hindered by Hg reemission. In their report, Blythe et al. (2005) stated that 84% overall Hg removal should have been achieved but that Hg reemission resulted in an overall Hg removal rate of only 79%. 2.3.2 Solubility The solubility of Hg in water varies with its chemical composition. Hg in flue gases exits in various forms, such as Hg0, HgCl2, HgBr2, HgI2, and HgO, and each of these compounds has unique water solubility. The solubility of the compounds varies as a function of temperature, ionic strength, and the concentrations of other species. The oxidized Hg and, to a much lesser extent, elemental Hg, are scrubbed from the flue gas and enter the wet FGD liquor. The extent to which the Hg compounds are scrubbed is largely a function of their solubility. Table 2.2 summarizes solubility data for various Hg compounds. Thomas (1939) discovered during experiments that the solubility of HgCl2 in water increased as the concentration of dissolved CaCl2 increased. Thomas (1939) found that, in comparison with HgCl2 solubility without CaCl2 present, the solubility increased by 41% when the concentration of CaCl2 in the solvent (i.e., water) was raised to 0.1068 mol/kg (roughly 11,000 wt ppm) and by 219% when the CaCl2 concentration was raised to 0.6043 mol/kg (roughly 66,000 wt ppm). Blythe et al. (2008), found, in bench-scale studies, that high concentrations of chlorides beneficially reduced the propensity of Hg to be reemitted once captured, and that a higher chloride concentration dramatically slowed Hg reemission. Caro (2009) reported that the amount of air in a solution affected the 44 solubility of elemental Hg. In fact, a large concentration of dissolved air could increase the solubility of elemental Hg by 700 times, which would make it as soluble as HgO, as can be observed in Table 2.2. Table 2.2 Solubility of Various Hg Compounds in Water Molality Molecular at Compound Compound Weight 298.15 K Name Formula (g/mol) (mol/kg) Elemental Hg0 200.59 3.03 x 10-7 Mercurya Molality at 323.15 K (mol/kg) Comparative Solubility at 298.15 K 5.91 x 10-7 1 Mercury(II) chlorideb HgCl2 271.50 0.259 0.467 854,785 Mercury(II) Bromideb HgBr2 360.40 1.7 x 10-2 3.55 x 10-2 56,106 Mercury(II) Oxideb HgO 216.59 2.447 x 10-4 not found 808 Mercury(II) Iodideb HgI2 454.40 1.21 x 10-4 4.38 x 10-4 400 Mercury Sulfidec HgS 232.60 1.2 x 10-25 not found 4 x 10-19 Note: Information for developing table was compiled from three separate sources: a. Seidell (1917), b. Cleaver et al. (1985), and c. Audeh (1993) Note: From Tables 4, 8, 13, 17 “Solubility of Mercury and Mercury Salts in Water and Aqueous Solutions” by H.L. Clever, S.A. Johnson and M.E. Derrick, 1985, J. Phys. Chem Ref. Data,14, No 3, 1985. Copyright 1985 by ACS. Reprinted with permission. The low solubility of HgS has been used to remove Hg from wet FGD liquors. Ghorishi (2006) tested the effect of forming HgS by injecting sodium hydrosulfide (NaHS) into the FGD sump. The compound would dissolve and react with the Hg to 45 form HgS, which would precipitate from solution. The precipitation of HgS would provide dual benefits: (1) reduce the risk of reemissions and (2) limit the Hg concentration of the wet FGD wastewater blowdown. In addition to NaHS, there are a number of chemical compounds that can be used to precipitate Hg. 2.3.3 Role of Hg Reemission Reemission of Hg from wet FGDs plays an important role in the use of SCR and wet FGD as a compliance strategy for meeting Hg emission regulations. Several researchers studying actual, full-scale, wet FGD Hg removal data have reported Hg reemission (Blythe et al. 2005; Chang and Ghorishi 2003; and Senior 2001). If not controlled, Hg reemission events could cause plant emissions to exceed regulatory levels. A study of atmospheric chemistry by Munthe (1991), revealed that oxidized Hg was reduced to its elemental form in clouds. Munthe (1991) postulated that HSO3- (bisulfite) and pH played an important role in the reduction of oxidized Hg. Loon (2000) confirmed the finding by Munthe (1991) and determined reaction rate constants for the reduction of oxidized Hg under atmospheric conditions. Blythe et al. (2008), in their laboratory study, investigated the proposed oxidized Hg reaction pathways and conducted experiments to determine reaction rate constants. The results indicated that the reduction of oxidized Hg was a complicated process, likely involving a number of potential reduction pathways, and that chloride, sulfite, and pH have major effects on the reaction rates and mechanisms. Through experimentation at the bench scale, Blythe et al. (2008) determined that higher concentrations of chlorides lowered the potential for Hg reemission and postulated that the relationship of Hg reemission to pH and sulfite was 46 complex. For example, where sulfite and chloride were taken into account, Hg reemission was found to increase with increasing pH. In a study to determine whether adding aluminum salts to a wet FGD could limit Hg reemission, Gonzalez et al. (2012) found that lower wet FGD pH resulted in a higher overall Hg removal efficiency. This finding could support the earlier finding by Blythe et al. (2008). The ability to remove oxidized Hg remained constant in both cases; however, lower pH reduced the propensity of the captured Hg to be reemitted, thereby resulting in an Hg removal greater than that found in the higher pH case. Schuetze et al. (2012) found that Hg reemissions were dampened by the presence of chloride and bromide ions, when the pH of the solution was below 7, and postulated that both chloride and bromides form stable ionic tetrahalogenide complexes that reduce the potential for Hg reemission to occur. Wet FGDs operating at higher concentrations of chlorides or bromides would have lower Hg reemission and thus, would have higher overall Hg collection efficiency. Blythe et al. (2008) presented Figure 2.2 to describe the potential Hg reemission reaction pathways. Omine et al. (2012) confirmed, during a bench-scale study, that oxidized Hg reduction in wet FGDs was a function of pH, Hg concentration, total sulfite, and liquor chloride and bromine concentrations. Omine et al. (2012) found that Hg reemission occurred when sulfite concentrations were below 2 millimol/L (mM) and that, when sulfite concentrations exceeded 9 mM, Hg reemission approached zero. In a review of the literature, Senior (2007) surmised that the reduction of Hg by sulfite began when the pH of the liquor exceeded 5. The operating pH range in most utility-style wet FGDs is 5 to 6. Schuetze et al. (2012) determined that pH levels greater than 5 increased the 47 occurrence of reemissions and concluded that, as pH increased, Hg reacted with OH- ions to form HgX(OH) or Hg(OH)2 . Schuetze et al. (2012) determined that the reemission caused by pH could be mitigated by increased concentrations of chlorides. Figure 2.2 Schematic diagram of Hg reemission reaction pathways Note: From Figure 51 “Bench-scale Kinetics Study of Mercury Reactions in FGD Liquors” by G.M.Blythe, J. Currie and D.W. DeBerry, 2008, Final Report DE-FC2604NT42314. p. 65. Copyright 2008 by URS Corporation. Reprinted with permission Omine et al. (2011) reported that increased ionic strength of the wet FGD slurry solution by the presence of excess chlorine and bromine, reduced the likelihood that reemission events would occur. Schuetze et al. (2012) conducted bench-scale tests showing that increased concentration of chlorine in the wet FGD slurry solution reduces Hg remission, supporting the conclusions by Omine et al. (2011). Chlorine and bromine 48 concentrations exceeding 2000 mg/L were shown to be sufficient to reduce the occurrence of Hg reemissions (Omine et al., (2011). Transition metal ions are also present in wet FGD slurries, from the influx of fly ash and from the limestone used to capture the sulfur dioxide (SO2). Such metals might also play a role in reducing Hg. In their bench-scale study, Chengli et al. (2010) found the following reduction capabilities of ions in the solution: Pb2+ > Cu+ > Fe2+ > AsO2- > Ni2+. The reductive effect of transition metals could prove beneficial by causing the formation of insoluble Hg compounds that precipitate instead of being reemitted. For example, Somoano et al. (2005) concluded that the addition of solid oxides (e.g., CaO, MgO, Al2O3, Fe2O3 and V2O5) enhanced Hg capture in wet FGD by precipitating Hg onto gypsum (CaSO4) particles to a larger extent. 2.3.4 Partitioning of Hg within the Wet FGD Once collected in the wet FGD system the final fate of the absorbed oxidized Hg has three possible outcomes, reemitted as elemental Hg, remain in the slurry as oxidized Hg or colloidal particles, precipitate as a solid, or adsorb onto a solid (fly ash or gypsum). Blythe and Richardson (2010) conducted a month-long characterization study of a fullscale wet FGDs to determine the partitioning of Hg among various effluent streams. All of the solid and liquid streams were analyzed. The boiler studied by Blythe and Richardson (2010) was burning an eastern bituminous coal, and was not equipped with an SCR, but was equipped with a limestone forced oxidation (LSFO) scrubber (i.e., wet FGD). Blythe and Richardson (2010) found that the wet FGD had very low concentrations of Hg in the liquid (0.38–1.36 µg/L) and similar concentrations in the 49 solids (0.81–0.890 µg/g) but 99.5% of the total Hg was found in the solids. The low concentration of Hg in solution precluded Blythe and Richardson (2010) from confirming the presence of colloidal Hg in the slurry. In an examination of the solids, Blythe and Richardson (2010) determined that 75% of the Hg was found in the fine solids. Blythe et al. (2004) determined that, although Hg likely reports to the solids, the evidence suggests that Hg could remain in solution under some wet FGD conditions, though the conditions that cause Hg to remain in solution remain poorly understood. In a report of results from their study of a full-scale pulverized coal-fired plant equipped with a wet FGD, Cordoba et al. (2012) stated that 99% of the Hg captured by the wet FGD was found in the wet FGD solids (i.e., gypsum) and that the remaining 1% was found in the liquid. Laudal et al. (2000), in a study of two, full-scale pulverized coal-fired plants, equipped with wet FGDs, determined that the majority of the Hg in the wet FGD was associated with the solids. Senior et al., (2009) reported that Hg appeared to be concentrated in the fine particles of the wet FGD solids that were predominately iron oxyhydroxides and were not strongly associated with the solid calcium sulfate, CaSO4. Although mounting evidence indicates that most of the Hg will partition to the solids, Ochoa et al. (2009), who studied Hg behavior in full-scale wet FGDs, reported that 78% to 81% of the Hg entering the wet FGD was found in the liquid phase and that only 15% of the Hg left the scrubber in the gypsum solids. Sanderson et al. (2008) found a correlation between Hg concentration in the wet FGD liquor and each of the following elements: chloride concentrations in the wet FGD liquor, acid insoluble inerts in the wet FGD slurry solids, and the Hg content of the raw gypsum. Consequently, Sanderson et al. 50 (2008) postulated that wet FGDs with high blowdown rates had an absence of fine particles and therefore Hg remained in solution. 2.4 Literature Review Synopsis A literature search yielded current theories concerning the oxidation of Hg and its subsequent removal in wet FGDs. Although vast and deep, the literature spans more than 20 years, a significant number of reports were published during the past 5 years. Information related to the behavior of Hg in the presence of bromine was not as extensive as the literature concerning the relationship between Hg oxidation and chlorine. The review of the literature led to the following general conclusions: • Under proper conditions, Hg oxidation can occur via homogeneous and heterogeneous means. • Halogen type and concentration are the most important factors in oxidizing Hg in all situations. • Halogen addition effectively raises the potential for Hg oxidation to occur under all oxidation schemes. • Homogeneous Hg oxidation typically does provide sufficient Hg oxidation to support MATS rule compliance. • All halogens support Hg oxidation but do so to differing degrees. The hierarchy of oxidation effectiveness is HBr > HCl > HI > HF. • Bromine-based homogeneous oxidation can produce oxidized Hg in amounts greater than those resulting from other forms of halogen-based homogeneous 51 Hg oxidation. It may be possible with low-sulfur coals to use homogeneous oxidation to achieve nearly 100% Hg oxidation with bromine addition alone. • SO2 concentration in the flue gas affects both homogeneous and heterogeneous oxidation but affects the latter to a lesser extent. • Higher concentrations of SO2 in flue gas can severely limit chlorine-based homogeneous Hg oxidation but affects bromine-based homogeneous oxidation to a lesser extent. At some concentration of SO2, bromine-based homogeneous oxidation may become limited. The actual SO2 concentration, at which this limiting effect occurs, with both chlorine and bromine, remains poorly understood. • Flue gas temperature has an effect on both homogeneous and heterogeneous Hg oxidation. • The literature supports the use of the Eley-Rideal, Languimuir-Hinshelwood or Mars-Maessen mechanisms to describe reaction pathways in an SCR reactor. • Native heterogeneous oxidation occurs as a function of the unburned carbon, Fe2O3, and Cu concentrations in fly ash. Native heterogeneous oxidation is not a major factor in achieving high levels of oxidation. Oxidation catalyzed by particles in the flue gas likely constitutes only a small percentage of the total Hg oxidation that occurs. • The design and operation of an SCR can be optimized to achieve high levels of Hg oxidation, if sufficient levels of halogens are present. 52 • SCR design parameters such as space velocity, catalyst vanadium content, catalyst activity, and catalyst pitch are important in determining the ability of the SCR to support high levels of Hg oxidation. • SCR operating parameters affect the optimization of Hg oxidation. NOx reduction is the dominant reaction, and NH3 must be consumed in the deNOx reaction before the Hg oxidation reaction can proceed. As a result, Hg oxidation occurs in the later sections of the SCR after consumption of the NH3 has occurred. • SCR-based (i.e., heterogeneous) oxidation of Hg is less sensitive than gas phase (i.e. homogeneous) oxidation of Hg to flue gas constituents such as SO2, CO, NOx, and H2O. • Hg removals of up to 95% have been observed at full-scale, coal-fired units equipped with SCR and wet FGD, demonstrating that configuration as a viable compliance option. • Oxidized Hg (HgCl2, HgBr2, HgI2, and HgO) is soluble in water. In comparison with HgCl2, elemental Hg is over 850,000 times less soluble under certain conditions. • Once captured in a wet FGD, oxidized Hg can be reduced and reemitted as elemental Hg, because of chemical changes in the wet FGD. • The magnitude of Hg reemission is a function of wet FGD chemistry, including, but not limited to, slurry pH, sulfite concentration, ionic strength, wet FGD slurry Hg concentration, and the concentrations of transition metals. 53 • After oxidized Hg is collected in the wet FGD system, it can be reemitted as elemental Hg, remain in the slurry liquor as oxidized Hg or as colloidal particles; precipitate as a solid, or adsorb to solids (fly ash or gypsum) present in the slurry. 2.5 Critical Analysis Although extensive, the available literature does not provide a complete view of Hg oxidation and subsequent removal in a wet FGD. This section highlights the strengths and weaknesses in the literature and provides a viewpoint of the current work and how it is intended to fill information gaps, and what gaps still remain in the understanding of low-sulfur, low-halogen, co-benefit Hg removal. 2.5.1 Strengths of the Literature The literature on the behavior of Hg in coal-derived flue gas is extensive and contains information from many excellent academic and applied researchers. The behavior of Hg from the boiler to the stack is dependent on a number of factors that vary with coal type, boiler design and the configuration of pollution control equipment. The present dissertation is focused on a single coal type and equipment configuration, which means that much of the literature may not apply directly.. • The literature provides the basis for understanding the different potential outcomes from an application of CaBr2 injection as a compliance technology. Examples: 54 o CaBr2 injection may have applicability at power stations that burn lowsulfur, low-halogen coals, such as PRB, are equipped with SCR for deNOx purposes and include a wet FGD for SO2 removal. o CaBr2 injection is not likely to be needed to achieve high rates of Hg oxidation when high-chlorine coal is burned in a boiler equipped with an SCR and wet FGD. 2.5.2 Weaknesses of the Literature While extensive, the literature documenting experience at full-scale power plants does not provide enough variation in operating conditions to confirm results to those in the literature presenting the results from research at the bench-scale. Observation of the behavior of Hg in full-scale, coal-fired boilers are still rather novel. Additional test programs are needed to advance this area. • The bench-scale literature is unbalanced and focused on isolating dependent variables one at a time. Most of the published work was conducted at laboratory scale using simulated flue gases. In addition, a number of equilibrium chemistry studies are available. Although they provide valuable insights, neither approach explains sufficiently well the actual behavior that would occur under full-scale plant conditions. • The literature lacks sufficient detailed analysis of full-scale results that describe the observed behavior in terms of the fundamental chemistry and physics. 55 • The literature contains separate oxidation and removal studies. Although such programs are ideal for isolating singular behavior (i.e., the effects of temperature on Hg oxidation in a SCR) they do not put performance in the proper context. Compliance with EPA regulations will require that utilities not only oxidize Hg, but also remove it with high efficiency. • The literature contains little work describing the mechanisms that control Hg partitioning between solid and liquid phases in a wet FGD after the oxidized Hg has been captured. 2.5.3 Importance of the Current Work The current work is focused on demonstrating the performance of CaBr2 addition at full-scale in the actual environment of interest. The work connects both Hg oxidation and Hg removal in a wet FGD. Extensive analytical measurements were made and are discussed herein. • The present study provides data from a full-scale program and involves evaluation of the observed CaBr2 performance using the current level of fundamental technical understanding. • This study, completed over a four-year period, provides a true indication of the oxidized Hg removal that CaBr2 injection would provide under true operating conditions. • The information produced in this study can be used by fundamental researchers to test and validate hypotheses postulated for mechanisms of Hg oxidation and will also provide potential adopters of the technology a clear 56 indication of achievable Hg removal using CaBr2 addition in a unit burning low-sulfur, low-halogen coals, equipped with an SCR and a wet FGD. 2.5.4 Issues Not Addressed by the Current Work A problem with conducting research at full-sale operating power plants is the inability to control plant operations, to better understand dependent variable (e.g., Hg oxidation) behavior as a function of independent variables (e.g., SCR NH3 flow) due to the nature of the utility business. Power plants are operated for business purposes and controlling independent variables to gain fundamental understanding through research is not a high priority. Therefore, a combined approach of full-scale testing combined with bench-scale testing is the best way to fully understand the capabilities of this new technology. The work described within presents only a limited viewpoint of CaBr2 injection technology. • This study was designed to examine only one possible full-scale scenario. It would be ideal to replicate the same study at different full-scale sites using different coals, to benchmark laboratory-scale studies with measurements at full-scale. This important step can lead to a more widespread application of co-benefit Hg removal (i.e., SCR combined with wet FGD). • This study involved conducting test programs under normal plant operating conditions only. 57 CHAPTER 3 METHODS 3.1 Introduction The present work was designed to evaluate the potential commercial use of calcium bromide (CaBr2) as an additive to coal, to enhance the oxidation and removal of Hg in existing environmental control equipment, namely, an SCR and a wet FGD. Electric utility companies, conservative by nature, require independent technology evaluations to enable them to make compliance and technology investment decisions. The determination by the EPA that it was prudent and necessary to control Hg emissions from electric generating units necessitates that utilities invest in new technologies to reduce future emissions. CaBr2 injection technology has been identified as a potentially cost-effective approach to controlling Hg emissions from coal-fired power plants. The technology involves the addition of a relatively small quantity of concentrated CaBr2 solution onto the coal, before to the coal enters the combustion zone, where the CaBr2 solution is volatized and decomposes into vapor phase forms of bromine (HBr, Br2, Br, and Br-) that are then available to transform elemental Hg into oxidized Hg (HgBr2), which is water-soluble. Henceforth, the terms CaBr2 addition and CaBr2 injection will be used interchangeably. The HgBr2 is then removed to low levels in conjunction with SO2 removal in the existing wet FGD. The technology is well suited for units burning PRB coals because those coals contain only low levels of native halogens (fluorine, chlorine, 58 bromine, and iodine). Utilities, as an industry, test new technologies thoroughly in a well-defined approach that aims to reduce the risk of adoption by testing at different scales with a wide range of varying flue gas conditions. The stages of the technology development process are shown in Figure 3.1. Figure 3.1 Electric utility technology development curve. Technologies are typically first tested at the bench-scale (i.e., in a laboratory setting with well controlled conditions using simulated flue gas), a step usually undertaken to test process chemistry and determine whether a process can reach a level of success in a controlled environment. This screening step can be accomplished at a relatively low cost, but success at bench scale may not mean success at the next level. The bench-scale test, using simulated flue gas, provides a technology with representative 59 test conditions and full control of independent variables that affect technology performance. Technologies not successful at this scale usually do not advance to the next level of evaluation, which consists of testing the process using actual flue gas from the combustion of coal. Testing at pilot scale involves exposing the technology to coal-derived flue gas, which can be quite challenging, because it exposes the technology to trace constituents found in coal that are not typically replicated in simulated flue gas laboratory studies. Those trace constituents can, at times, provide unique challenges to new processes. Testing at pilot scale also involves evaluating technology performance over a longer period and incorporating a wide-array of operating conditions to develop a well understood operating window. This phase dramatically increases the understanding of technology performance without risking power production of the full-scale power plant and keeps costs to a minimum. Demonstration at the pre-commercial scale follows to ensure that the process can be successfully scaled up. Process chemistry and process fundamentals are confirmed and verified. This stage reveals process changes needed before design of commercial systems is complete. The last phase, testing the approach at full scale, is done to evaluate long-term performance under actual conditions, including both normal and upset plant operating conditions. Evaluators sometimes repeat this step at multiple sites before a technology is considered to be commercial. This perspective may differ from that of original equipment manufacturers (OEM), who may declare a technology commercial after, or even before, the first full-scale test of the technology. However, exposing the technology 60 to different coals, different plant configurations, and different operating philosophies dramatically reduces the overall risk of adopting new technology. The present research program was designed around the utility technology development curve shown in Figure 3.1. One complication in evaluating CaBr2 injection technology was the need, for an integrated and cost-effective approach, to demonstrate both Hg oxidation and its subsequent removal in a wet FGD. A pilot-scale study could be completed at a test combustor (typically <1 MW) and would require that the combustor have a pilot wet FGD. The cost of conducting a pilot-scale test under these constraints would have been prohibitive. A decision was made to use a hybrid program containing both full-scale and pilotscale components. The program was accomplished in three distinct phases over a fouryear period. All three phases were conducted by using a full-scale boiler to produce the flue gas necessary to properly evaluate the approach. Phase I included only flue gas measurements to evaluate the ability of CaBr2 to affect Hg speciation. In Phase I, CaBr2 was introduced into the boiler in varying concentrations, and speciated Hg measurements were made at four locations in the flue gas stream to determine the dose–response of the system. Phases IIA and IIB included the installation of a pilot-scale wet FGD and replication of the conditions investigated during Phase I. During Phases IIA and IIB, the boiler with CaBr2 injection produced the flue gas containing bromine and oxidized mercury (HgBr2), and the installation of the pilot-scale wet FGD enabled a detailed parametric study of HgBr2 removal. Experiments on wet FGD chemistry were conducted to determine the impact, if any, on the removal of HgBr2 in the wet FGD. Phase III 61 included the addition of CaBr2 to the coal for an 83-day operating period and focused on the total Hg removal performance of the technology (i.e., both Hg oxidation and subsequent Hg removal in a wet FGD). During Phase III, the boiler was operated just as it would have been if a technical evaluation had not been under way, allowing the evaluation of technology performance under normal operating conditions. Between Phase I and Phase III, a full-scale wet FGD was installed. This test design proved ideal, because using the boiler to vaporize the CaBr2 posed virtually no risk to normal operation of the unit and provided a treated flue gas to support the technology evaluation. If the technology proved ineffective during Phase I, the evaluation would have been halted, a scenario also true for Phase II. A failure during Phase III would limit consideration of CaBr2 injection technology as a MATS rule compliance option for the site being tested. Each phase was designed to answer specific questions and provide critical evaluation information: Phase I determined the effectiveness of Hg oxidation chemistry, Phase II evaluated wet FGD removal performance, and Phase III established longer term technology performance. The data produced during the three phases were used to answer research hypotheses posed in Chapter 1. 3.2 Research Design 3.2.1 James H. Miller Steam Plant All three phases of the study were conducted at Alabama Power Company’s Miller Steam Plant, located in Quinton, Alabama. The site contains four coal-fired units that each burn PRB coal exclusively to generate electric power. The plant can produce 62 approximately 2,880 MW of electricity (gross). Each of the four units is rated at roughly 720 MW of electric power generation. At the start of the test program, all four units were equipped with SCRs and cold side-ESPs as environmental control equipment. During the course of the research program, each unit was outfitted with a high-efficiency, limestone forced oxidation (LSFO) wet FGD designed by Advatech (a joint venture between Mitsubishi Heavy Industries Americas and URS Corporation). 3.2.1.1 Plant Miller Unit 4 and Unit 3 Overview All of the testing associated with the present work was performed on Unit 4, a relatively new unit placed in service in 1991. The unit has a Babcock and Wilcox (B&W) opposed-wall-fired, dry-bottom boiler. Coal is fed from seven pulverizers, each with a dedicated silo and gravimetric feeder. The pulverizers are B&W roll-and-race style MPS 89 mills, designed to feed up to 61,700 kg/hr (136,000 lb/hr) of coal. Coal is loaded into the bunkers, one per pulverizer, twice per day and fed from the bunker using a gravimetric feeder. Primary combustion air (roughly 10% of the total combustion air) enters the pulverizer from the air heater. The primary air heats the coal from ambient temperature to roughly 70 ◦C and transports the pulverized coal to the boiler. After being ground to a size of 95 wt% passing 325 mesh (44 µm), the coal from each pulverizer is split into eight individual transport pipes and transported to the burners. The Unit 4 boiler has fifty-six burners. The front wall of the furnace contains four rows of eight burners, and the rear wall contains three rows of eight burners. One pulverizer feeds each row of burners. At full load, all seven pulverizers and all fifty-six burners are in service. The burner elevations are identified sequentially from Row A to Row G. The front face 63 of the boiler includes three burner elevations fed from Pulverizers B, G, and A from bottom to top. Burners fed from pulverizers F, D, E, and C, also listed from bottom to top, are located on the rear face of the boiler. At the time of the study, the heat rate of the unit was approximately 10,000 Btu/kWhr. The boiler was designed to provide 2,137,000 kg/hr (4,711,000 lb/hr) steam flow at 16.5 MPa (2,400 psig) and a boiler operating temperature of 1,400 ◦C. Once the flue gas leaves the boiler and the superheater section, it enters the economizer, which preheats boiler feedwater. The economizer reduces the flue gas temperature to roughly 538 ◦C. Upon leaving the economizer, the flue gas is divided into two equal streams for treatment in the downstream environmental control equipment. During Phase III, Unit 3 was used for Hg removal performance comparison. Unit 3 is a sister unit to Unit 4 and has the same boiler and emissions control equipment. Both units burn PRB coal from the same source. 3.2.1.2 Coal Type and Mass Flow Rate Unit 4 burned PRB coal exclusively during all three test phases. The PRB burned was from three different mines: Arch Coal’s Black Thunder, Peabody Coal’s North Antelope Rochelle, or Kennecott/Cloud Peak’s Antelope, which are all located in the Powder River Basin of Wyoming. The higher heating value of the coals delivered to the site range from 8,500 to 8,800 Btu/lb. The plant receives its coal via rail. Once on site, the coal is loaded directly from the train into the bunkers or is stored locally in a pile for later use. All four units at the site are fed from the same coal source via common coal 64 handling equipment. Table 3.1 lists the properties of the coal measured during the three test phases. A typical coal feed rate at 720 MW is approximately 363,000 kg/hr (800,000 lb/hr). Because of constraints on the SCR operating temperature, the minimum operating load on the unit is roughly 300 MW. Coal flow rate at 300 MW approximate 155,000 kg/hr (342,000 lb/hr). Table 3:1 Coal Analysis Plan Fuel property (dry basis, except as noted) Unit Phase I Phase II Phase III Btu/lb X X X Carbon wt% X X X Nitrogen wt% X X X Oxygen wt% X X X Ash wt% X X X Sulfur wt% X X X Moisture (as received) wt% X X X Mercury wt ppb X X X Chlorine wt ppb X X X Bromine wt ppb X X X Heating Value 3.2.1.3 Environmental Control Equipment The SCR reactor, designed to reduce NOx emissions by 90%, is housed in two separate casings. Ammonia (NH3) is added to the flue gas upstream from the SCR. The rate NH3 addition depends on the desired NOx emission rate. In practice, setting a desired 65 SCR outlet NOx emission concentration controls the NH3 flow, which changes in realtime on the basis of SCR inlet NOx concentration. The desired stack NOx emission rate at Unit 4 is 0.015 lb/MBtu. The Unit 4 SCR, designed to achieve 90% NOx removal with an NH3 slip of 2 ppmv and holding up to four layers of catalyst, was placed into commercial operation in May 2003. At that time, the SCR was filled with three layers of 9.2 mm honeycomb catalyst manufactured by Cormetech. The SCR operated at a minimum operating temperature of 310 ◦C and a normal operating temperature of 380 ◦C. The original catalyst loaded in 2003 had not been replaced at the time of the current tests. During Fall 2009, a fourth layer of catalyst was added. Historically, the SCR was placed in service during the ozone season (May 1 to September 31) from 2003 through 2009. Operation during an ozone season corresponds to 3,696 potential hours of flue gas exposure. Starting in January 2010, as a result of the Clean Air Interstate Rule, continuous SCR operation was required. From the outlet of each SCR housing, the flue gas travels to a Ljungstrom-style air heater, where heat rejected from the flue gas is transferred to the incoming combustion air to improve process efficiency. The flue gas temperature exiting the air heater typically ranges from 155 ◦C (311 ◦F) to 165 ◦C (330 ◦F). The flue gas passes from the air preheater to a cold-side ESP, which removes fly ash from the flue gas. Two cold-side ESP casings accept flue gas from the corresponding SCR housing. The cold-side ESP is an ABB-Flakt European-style design that contains high-voltage electrodes having rigid frames with spiral discharge electrodes and traditional transformer rectifier sets. The rapping system uses tumbling hammer rappers on the high-voltage discharge electrodes and collecting plates. Generously designed, the 66 cold-side ESP has a specific collecting area of 1000 (ft2 min)/(1000 ft3) (SCA equals ft2 of collecting area/1000 actual ft3/min of flue gas). The Unit 4 SCA has almost three times the average specific collecting area typically found in cold-side ESPs in the United States. Each cold-side ESP casing has six rows of hoppers and four individual hoppers per row, for a total of forty-eight hoppers. Each cold-side ESP casing has six electric fields in the direction of gas flow with two transformer rectifiers per electrical field, for a total of twenty-four transformer rectifiers. Historical filterable particulate matter emissions from the ESP are low. The Title V filterable particulate matter emissions limit is 0.03 lb/MBtu. During Phases I, IIA, and IIB, the flue gas from the ESP was exhausted to the atmosphere via a 210 m tall stack. During Phase III, the cold-side ESP was followed by a wet FGD. During Phase II, a single tower 2 MW pilot-scale Advatech scrubber was installed downstream of the A casing of the cold-side ESP. The wet FGD was installed downstream from the cold-side ESP but was plumbed across the full-scale induced draft (ID) fan. The outlet of the pilot-scale wet FGD connected to ductwork upstream of the ID fan inlet and the inlet of the pilot-scale wet FGD connected to ductwork downstream of the ID fan outlet. Because the flue gas processed by the pilot-scale wet FGD was equivalent to only 2 MW of the 88 MW of flue gas passing through that ID fan, any effects; such as Hg concentration, flue gas moisture content, halogen content, and flue gas temperature, of the pilot-scale wet FGD had on the flue gas were deemed negligible. This arrangement allowed the wet FGD to be operated without a dedicated wet induced draft fan or a dry booster fan and reduced the complexity of the installation and overall cost of the test program. 67 The pilot scale wet FGD was operated as a limestone forced oxidation wet FGD. Plant compressed air was supplied to the wet FGD sump via an MHI proprietary jet air sparger system that uses the discharge from the wet FGD slurry recycle pump and an educator to introduce air into the sump. The amount of air introduced into the sump exceeded the stoichiometric molar flow rate of O2 required by the reaction of sulfur dioxide (SO2) with calcium carbonate (CaCO3) to form calcium sulfate (CaSO4). The recycle pump provided limestone slurry to the slurry nozzles. Makeup water to the wet FGD was also added on a periodic basis to keep the mist eliminators clean and was added to the sump to replace evaporated water lost to the flue gas. Wet FGD slurry was constantly introduced to a hydrocyclone, which split the slurry into two streams, the underflow (50 wt % coarse solids) and the overflow (1 to 3 wt % finer solids). Both streams were recombined and returned to the system until solids needed removing from the system, at which time, the hydrocyclone underflow was directed to an external storage tote. The gypsum crystals settled within the external storage tote via natural gravity. The supernatant liquid above the solids was then pumped back to the sump, and the settled gypsum crystals were disposed of, in the as-found condition, onsite in a dry solid landfill. Limestone slurry consisted of pre-ground limestone combined with makeup water. The feed rate of the limestone slurry was controlled via a real-time pH measurement. Instruments were installed to continuously monitor the 2 MW wet FGD oxidization-reduction potential (ORP) and pH. The system was operated at a pH of 5.5 and a solids concentration of approximately 20 wt %. The concentration of solids was determined by manual gravimetric sampling. The system was designed to achieve 90% 68 SO2 removal. SO2 removal efficiency was monitored in real-time using inlet and outlet SO2 measurements. The flue gas exiting the 2 MW wet FGD was reheated, with the use of an electric heater made by Chromolox, from roughly 57 to 107 ◦C before being reintroduced into the flue gas stream of the full-scale unit. All inlet flue gas concentration measurements (i.e., Hg semi-continuous emission monitor, SO2, and EPA Method 26) for Hg, SO2, and halogen concentration were made in front of the wet FGD inlet. Outlet flue gas measurements (i.e., Hg semi continuous emission monitor, SO2, and EPA Method 26) for Hg, SO2, and halogen concentration were made downstream from the wet FGD plenum, but in front of the flue gas heater. A damper used at the exit of the heater assembly controlled the pressure drop across the wet FGD and therefore allowed positive control of flue gas flow rate. A venturi type flowmeter at the inlet to the wet FGD enabled the investigators to determine the flow rate of gas being treated by the system. The output from the flow meter served as a control variable for the adjustment of the control damper. A diagram of the 2 MW wet FGD is shown in Figure 3.2. During Phase III, the flue gas leaving the cold side ESP was treated in a full-scale wet FGD before exiting a 150 m tall wet stack. The wet FGD is a state-of-the-art limestone forced oxidation scrubber (LSFO) designed for 98% average SO2 removal and sited to treat 80,700 m3/min (2,850,000 ft3/min) of flue gas. The 2 MW pilot-scale wet FGD used during Phases IIA and IIB and the full-scale wet FGD are both single tower double contact flow type wet FGDs made by Advatech. 69 Figure 3.2 Diagram of 2 MW slipstream pilot-scale wet FGD installed for testing at Plant Miller Unit 4. 3.2.2 CaBr2 Feed Rates and Coal Br Concentrations A concentrated solution of CaBr2 was used to introduce bromine to the system. During all three phases, the CaBr2 solution was evenly split and added to the coal in the F and G feeders. The CaBr2 solution provided the bromine (Br) that was needed to augment the low halogen content of the coal. The Br concentration was determined as the ratio of the mass flow of Br, provided by the CaBr2 solution, to the mass flow rate of dry coal. Equation 1 was used to calculate the Br concentration (wt ppm on the dry coal) with the use of information from Table 3.2. An emphasis was placed on the coal Br concentration, and the mass flow of CaBr2 solution was not highlighted because the 70 solution flow rate required to reach a certain Br concentration on the coal can vary, depending on the CaBr2 concentration in the solution. !" = !!!"#! !!"# !!!"#! ! ! !"#$% !"!!"#! !"# !!"#! !"!" ! !!"#$ !!!!"#$%&'( 10! (E1) By using coal Br concentration (wt ppm on the dry coal), changes in the CaBr2 solution concentration are compensated by adjusting the solution flow rate. Table 3.2 Information Used to Calculate Coal Bromine Concentration Parameter Value Units Symbol CaBr2 Solution Density 14.092 lb solution/gal ρsol CaBr2 Concentration various lb CaBr2/lb solution CCaBr2 CaBr2 Molecular Weight 200 lb/lbmol MWCaBr2 Br Atomic Weight 80 lb/lbmol MWBr Full Load Coal Flow 13,333 lb coal/min mcoal Typical Coal Moisture Content 0.28 lb H2O/lb coal Cmoisture CaBr2 Volumetric flow various gal solution/min VCaBr2 3.2.3 Description of the Test Phases The research program spanned a four-year period from fall 2006 to fall 2010. Phase I ended in fall 2006, Phase II was conducted in two parts (IIA and IIB) in the spring and fall of 2007, and Phase III ended in fall 2010. The phased approach to testing reduced risk, enhanced ability to evaluate the impact of specific technical aspects on Hg 71 oxidation and removal (i.e., bromine dose-response, Hg reemissions, impact of wet FGD ORP), and reduced the cost of the technology evaluation. 3.2.3.1 Phase I: Hg Oxidation Measurements Only During October of 2006, seventeen days of testing were conducted at Plant Miller Unit 4 to evaluate the potential of CaBr2 injection to oxidize mercury. Preparation of the CaBr2 solution involved mixing 52 wt% CaBr2 stock solution with filtered water to reach desired concentration. The diluted mixtures were stored in large plastic totes having a total capacity of 2,500 gallons. When desired, the CaBr2 solution was pumped to the F and G coal feeders. An injection lance introduced the CaBr2 solution into the feeder, and the CaBr2 mixed with the coal as the coal fell from the gravemetric feeder belt into the top of the pulverizer. The total coal flow rate, the desired Br concentration (wt ppm on the dry coal), and the concentration of the CaBr2 solution, which were all known, determined the desired solution feed rate. A pumping skid having a capacity of 350 to 8,300 cm3/minute conveyed the CaBr2 solution to the feeders. To evaluate the performance of the technology, specially designed semicontinuous emissions monitors (SCEM) were used to measure speciated Hg in the flue gas. Hg SCEMs were located at the SCR inlet, SCR outlet, cold-side ESP inlet, and the ESP outlet. These measurement locations provided the ability to determine the effect of flue gas temperature, equipment (i.e., SCR and cold-side ESP), and Br concentration on Hg oxidation performance. Samples of coal, bottom ash, and fly ash were taken for future analysis. Gas-phase measurements of halogen concentrations were made, using EPA Method 26A, to verify the concentration of halogen added to the flue gas stream. The Br 72 concentrations investigated included 0, 3, 7, 18, 23, 33, 71, 84, 85, 165, and 328 wt ppm on the dry coal. The duration of the tests ranged from 2 to 6 h. The SCR was in operation with NH3 injection. NH3 injection rates were adjusted in real time and were managed to maintain an average NOx emission rate of 0.015 lb/MBtu. Table 3.3 summarizes the Phase I test conditions. Table 3.3 Phase I Test Conditions Br Concentration (wt ppm on the dry coal) SCR in service NH3 Injection on/off SCR Inlet Hg SCEM in service SCR Wet FGD Wet FGD Outlet Inlet Outlet Hg Hg Hg SCEM SCEM SCEM in service in service in service 328 bypass off yes yes yes yes 165 bypass off yes yes yes yes 85 bypass off yes yes yes yes 84 yes on yes yes yes yes 71 yes on yes yes yes yes 33 yes on yes yes yes yes 23 yes on no no yes yes 18 yes on yes yes yes yes 7 yes on yes yes yes yes 3 yes on yes yes yes yes 0 yes on yes yes yes yes Note: Adapted from Table 6 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2007 p. 2-9. Copyright 2007 by EPRI. Reprinted with permission. 73 3.2.3.2 Phase IIA Spring 2007 During spring 2007, a 24-day test program was completed at Plant Miller Unit 4 to determine the ability of CaBr2 to oxidize Hg and to evaluate the subsequent oxidized Hg removal in a 2 MW pilot-scale wet FGD. During Phase IIA, a 52 wt % solution of CaBr2 was added to the coal to achieve the desired Br concentration (wt ppm on the dry coal). Although the location of the injection was the same as in Phase I, in Phase IIA the concentrated 52% CaBr2 solution was utilized rather than the diluted solution used in Phase I. The CaBr2 solution was brought onsite in 208-liter (55 gallon) drums, and a peristaltic pump delivered equal volumes of solution to the F and G coal feeders. A manual metering system was used to measure the volumetric flow rate of solution. Daily manual calibrations verified the solution flow rates. During testing, the pump calibration curves changed over time, because of fatigue of the tubing in the peristaltic pump. Periodic adjustment of the flow rate of CaBr2 solution compensated for this effect. A pumping system greatly simplified from that used in Phase I allowed rapid changes in coal Br concentration. An injection lance on each coal feeder introduced the CaBr2 solution and the coal and solution were mixed as the coal fell from the weigh feeder belt into the top of the pulverizer. The 2 MW pilot-scale wet FGD was manned during 24 hours per day operations. Phase IIA was divided into two parts. In the first part, Hg oxidation measurements were made using Hg SCEMs at the SCR inlet, SCR outlet, ESP inlet and ESP outlet to verify the oxidation behavior that was observed during Phase I. Testing was conducted both with the SCR bypassed and with the SCR not bypassed, but without NH3 injection. 74 In the second part of Phase IIA, extended testing ensued after determination of the optimum Br concentration, operationally defined as the lowest Br concentration (wt ppm on the dry coal) that resulted in the highest Hg oxidation percentage during parametric testing. The extended test period spanned two weeks of continuous testing. During that time, a constant Br concentration of 25 wt ppm was added to the coal for 7 days and 50 wt ppm was added for another 7 days. Testing was conducted with the SCR in service but without NH3 injection. Table 3.4 specifies the conditions evaluated during the Phase IIA test program. Table 3.4 Phase IIA Test Conditions NH3 Injection on / off SCR Inlet Hg SCEM in service SCR Outlet Hg SCEM in service Wet FGD Inlet Hg SCEM in service Wet FGD Outlet Hg SCEM in service bypass off yes yes yes yes 100 bypass off yes yes yes yes 30 bypass off yes yes yes yes 50 yes off yes yes yes yes 50 a yes off no no yes yes 30 yes off yes yes yes yes 25a yes off no no yes yes 15 yes off yes yes yes yes 5 yes off yes yes yes yes 2 yes off yes yes yes yes Br Concentration (wt ppm on the dry coal) SCR in service 250 a. denotes longer-term test condition Note: Adapted from Table 7 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. 2-8. Copyright 2009 by EPRI. Reprinted with permission. 75 3.2.3.3 Phase IIB Fall 2007 During fall 2007, a 10-day test program was completed at Unit 4 to determine the ability of CaBr2 to oxidize Hg and evaluate the subsequent Hg removal in a 2 MW pilotscale wet FGD. Unlike the Phase IIA test completed in spring 2007, SCR operation in fall 2007 included NH3 injection. The absence of NH3 in the flue gas in the SCR can provide the better Hg oxidation performance. Table 3.5 shows the conditions that were evaluated during Phase IIB of the test program. Table 3.5 Phase IIB Test Conditions Br Concentration (wt ppm on the dry coal) NH3 Operation Injection in service on/off SCR ACI Injection duct or sump ACI Rate lb/106 acf Wet FGD Inlet Hg SCEM in service Wet FGD Outlet Hg SCEM in service 17 yes on no 0 yes yes 25 yes on no 0 yes yes 0 yes on duct 3 yes yes 0 yes on duct 5.2 yes yes 0 yes on duct 10.1 yes yes a yes yes 0 yes on sump 1.6 6 a. The lb/10 acf injection rate for the sump condition reported in the table is calculated as if the lb/hr rate were injected into the duct (lb/Macf versus lb/gal, or wt ppm). Note: Adapted from Table 6 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. 2-7. Copyright 2009 by EPRI. Reprinted with permission. Senior (2004) concluded from an analysis of full-scale data that NH3 reduced the overall effectiveness of the SCR in supporting Hg oxidation. Phase IIB was undertaken 76 to determine whether the addition of NH3 would impact the ability of CaBr2 addition to oxidize Hg. The Phase IIA CaBr2 injection system was used during Phase IIB. In addition to determining CaBr2 injection effectiveness, an activated carbon injection into the wet FGD sump screening test was conducted. The activated carbon tests were done to determine activated carbon’s ability to remove captured Hg from wet FGD slurry. The results of the activated carbon tests are not included as part of the dissertation analysis and discussion but are mentioned here for the sake of completeness in describing testing details. 3.2.3.4 Phase III: 83-Day Full-Scale Demonstration In fall 2010, an 83-day injection test program was conducted. During this test program, Unit 4 operated in a fashion that reflected normal plant operations, that is load was allowed to vary to meet electricity demand. As was done in Phases IIA and IIB, CaBr2 solution was added to the F and G coal feeders but with one minor change. In Phases IIA and IIB, the CaBr2 solution was contained in 208-liter (55-gallon) drums; however, in Phase III, the drums were replaced with 1,040-liter (275-gallon) totes. Monitoring of the injection system was not done on a continuous basis. The CaBr2 flow rate was maintained to achieve a Br concentration of 20 wt ppm on the dry coal at fullload conditions. During periods of lower load, the CaBr2 addition rate remained the same, raising the Br concentration on the coal. Higher Br concentrations were not expected to negatively impact the results. All other environmental control equipment (SCR with NH3 injection, cold side ESP, and wet FGD) operated under customary operating procedures and conditions. A permanently installed Hg monitoring system 77 determined wet FGD stack gas Hg concentrations. Table 3.6 specifies the test conditions used during Phase III. Table 3.6 Phase III Test Conditions Br Concentration (wt ppm on the dry coal) SCR in service NH3 Injection on/off SCR Inlet Hg Monitor in service SCR Outlet Hg Monitor in service Wet FGD Inlet Hg Monitor in service Wet FGD Outlet Hg Monitor in service 0 yes on no no no yes 20 yes on no no no yes 10 yes on no no no yes 8 yes on no no no yes 2 yes on no no no yes Note: Adapted from Table 2-4 “Three-Month Evaluation of Furnace Addition of Calcium Bromide for Mercury Emissions Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2011 p. 2-5. Copyright 2011 by Southern Company Services. Reprinted with permission. 3.3 Measurement Techniques 3.3.1 Flue Gas Measurement Techniques During the three phases of the research program, the use of various measurement techniques provided data on the efficacy of CaBr2 injection technology in reaching the goals of the program. Measurements were made of the solids (i.e., coal, fly ash, limestone, and gypsum), flue gas, and liquids (i.e., wet FGD slurry). This section provides details of the techniques used. 78 3.3.1.1 Hg Semi-Continuous Emission Monitoring System During Phases I, IIA, and IIB, Hg SCEMs measured the concentration and species of Hg present in the flue gas. CaBr2 injection is designed to alter the species distribution of Hg by converting elemental Hg to oxidized Hg. The Hg SCEMs used during the evaluations were designed and built at URS Corporation, and run by qualified operators from URS. The basis of the URS Hg SCEMs is cold vapor atomic adsorption spectrometry, coupled with a gold pre-concentration amalgamation system. A sample of flue gas is introduced into the system using a pump, via a Quick Silver Inertial Separation (QSISTM) Probe, which separates fly ash particles from the gas sample before it enters the measurement system (Sjostrom et al., 2004). Because the Hg SCEM can only measure elemental Hg, two measurement techniques were used: (1) oxidized Hg was scrubbed from the flue gas and the elemental Hg in the flue gas was determined, (2) the oxidized Hg was reduced to the elemental form and the total Hg present in the flue gas was determined. The difference between the two measurements is the concentration of oxidized Hg. In both measurement approaches, elemental mercury passes through a cell where the Hg is captured on a piece of gold. This process continues until Hg is collected on the gold trap. A heated stream of air then passes over the gold trap, raising its temperature to over 400 ◦C, and releasing the captured Hg from the gold for measurement. A qualified person operated each Hg SCEM during the experiments. To ensure positive quality control of the Hg speciation data, Hg spike-and-recovery checks were conducted several times daily. During a spike and recovery check, the operator injected a known quantity of elemental Hg into the sample line. The Hg cold-vapor atomic 79 adsorption analyzer then interrogated the modified sample. A value of +/-10% of the expected value enabled the system to pass the quality control step (Dombrowski et al., 2007). 3.3.1.2 Continuous Hg Monitoring System (CMMS) During the installation of the full-scale wet FGDs, Plant Miller was outfitted with permanent Hg measurement systems on the wet stacks of all four units. The Mercury Freedom Systems from Thermo Scientific, designed to measure Hg on a continuous basis, are composed of four major components: (1) 80i Hg analyzer, (2) 81i Hg calibrator, (3) 82i probe controller, and (4) 83i probe/converter. The sample is drawn from the stack through the model 83i inertial probe, which dilutes the sample at dilution ratios from 25:1 to 100:1, then accelerates the flue gas through a curved loop to separate any entrained particles from the gas. Before the flue gas is returned to the duct or stack, a portion is bled off and becomes the sample to be analyzed for Hg concentration. The sample is drawn through a proprietary dry conversion chamber where oxidized Hg is converted to the elemental form. Converting the Hg at the stack avoids potential loss or changes in oxidized Hg in the sample line. The flue gas sample travels from the probe via a heated umbilical line to the 80i Hg analyzer. The 80i Hg analyzer contains a coldvapor atomic fluorescence (CVAF) analyzer that makes a direct measurement of Hg concentration in the sample, a procedure that allows the analyzer to perform a continuous measurement of Hg concentration. The analyzer, which makes an Hg concentration measurement every 10 s (Whorton 2011), can measure total gaseous Hg (oxidized and elemental) concentration or just elemental Hg concentration. To measure only the 80 elemental concentration, the analyzer does not convert the oxidized portion in the dry conversion chamber. As a result, the device can determine the percentage of oxidized Hg in the flue gas by subtracting the elemental Hg measurement from the total Hg measurement. The Model 80i Hg analyzer has a lower detection limit of 1 ng/m3 and an upper detection limit of 50 µg/m3. The Model 81i Hg calibrator utilizes a vapor generator that allows standard calibration and dynamic spiking into the sample extraction probe. A wide calibration range, from 3 µg/m3 to 50 µg/m3, allows calibration of the analyzer at post dilution concentrations (Thermo Scientific, 2009a). The calibration is ideally suited for daily zero and span checks, routine converter efficiency checks, and linearity testing. The Model 82i probe controller uses a microprocessor and is connected by an umbilical line to the stack probe and Hg converter. The controller automates probe calibration and dynamic spiking and confirms auto dilution. In addition, it monitors the probe temperature, measures flow rates and pressure in the sample loop, and enables automated filter blowback (Thermo Scientific, 2009b). The Thermo Scientific Mercury Freedom System is designed to meet or exceed performance specifications outlined in U.S. EPA PS-12A and/or Part 75 provisions for CMMs (Thermo Scientific, 2012). Site personnel maintain the systems daily, and the data are collected and stored in a site-wide data collection system. 3.3.1.3 EPA Method 30B Measurement EPA Method 30B measures total vapor-phase Hg emissions from coal-fired combustion sources using sorbent trap sampling and an ex-situ analytical technique 81 (EPA, 2008). A known volume of flue gas is drawn through a known mass of activated carbon, in a non-reactive glass tube, referred to as a sorbent trap. The measurement of Hg in the sorbent trap can be done by using either digestive or thermal desorption techniques (Laudal and Schultz, 2007). The method quantifies the mass concentration of total vapor-phase Hg in flue gas, including elemental and oxidized forms. The analytical range for oxidized and elemental Hg is typically from 0.1 to 50 micrograms per dry standard cubic meter (µg/dsm3) (EPA, 2008). Although not providing a real-time Hg concentration measurement, Method 30B does yield additional post-test for comparison with Hg SCEM and CMMs measurements. In the method, a specified volume of flue gas is extracted from a stack or duct through paired, in-stack sorbent media traps at an appropriate flow rate. The traps are arranged in two stages. The first stage, filled with iodated carbon, serves as the primary measurement section and is spiked with a known mass of Hg to provide a reference amount of Hg for quality control. The second stage, also filled with iodated carbon, is used for quality assurance purposes and permits determination of breakthrough from the first stage. If no Hg breakthrough occurs, the second stage does contain any Hg. Each sorbent trap is mounted at the entrance to, or within, the probe, so the gas sample directly enters the trap. Mounting the trap at the outermost tip of the probe ensures that the sorbent trap is heated to flue gas temperatures and the sampling error is minimal, since the Hg does not have an opportunity to react or deposit within the sampling system. The probe and sorbent trap assembly are also heated, using auxiliary heat, to a temperature sufficient to prevent liquid condensation in the sampling train. 82 From the heater, the sample passes through a knockout chamber and desiccant to remove water from the sample. The gas volume is measured using a flow meter. The gas flow is used to calculate the concentration of Hg in the flue gas once the mass of Hg in the sorbent trap has been determined. The Hg measurement technique used for the sorbent trap analysis was the Wet Acid Digest/US EPA Method 1631. This method calls for the sorbent materials to be digested by using a mixture of HNO3 / H2SO4 and the use of BrCl to completely oxidize Hg. The oxidized Hg is reduced to elemental Hg using SnCl2. After purging the samples, the Hg is passed over a gold trap. Thermal desorption is then used to liberate the Hg from the gold and the Hg concentration is determined by cold-vapor atomic fluorescence. 3.3.1.4 Ontario Hydro Hg Measurement This Hg measurement technique was conducted according to ASTM Method D6784-02, which applies to the determination of elemental, oxidized, particulate-bound, and total Hg emissions from coal-fired stationary sources. The method can be used for flue gas concentration of Hg from 0.5 µg/m3 to 100 µg/m3 under normal conditions (ASTM, 2008). In the Ontario Hydro method, a sample is drawn isokinetically through a probe and filter system maintained at 120 °C, then through a set of impingers in an ice bath. Particulate-bound Hg is captured in the front part of the system on a glass or quartz filter. Oxidized Hg is collected in impingers containing chilled aqueous potassium chloride (KCl) solution. Elemental Hg is collected in subsequent impingers, one of which 83 contains a chilled aqueous solution of hydrogen peroxide (H2O2) and three of which contain chilled aqueous solutions of potassium permanganate (KMnO4). After recovery, the impinger solutions are sent to a laboratory where they are digested and analyzed for Hg with the use of either cold vapor atomic absorption or cold vapor atomic fluorescence. 3.3.1.5 Flue Gas Adsorbent Mercury Speciation Method The Flue Gas Adsorbent Mercury Speciation (FAMS) method utilizes a specially designed multiple-stage dry sorbent trap to collect Hg species from flue gas streams. The technique selectively and sequentially captures particulate Hg, vapor phase oxidized Hg, and vapor phase elemental Hg in separate sections of a trap and produces three concentrations of different Hg species from a single trap. A FAMS trap is mounted at the entrance to or within the probe, so that the gas being sampled directly enters the trap. The temperature of the FAMS trap is held at 95 °C ± 5 °C to prevent water condensation. Elemental Hg is chemically and physically adsorbed onto iodine impregnated carbon (Brunette et al., 2004). Particulate-bound Hg is captured in a particulate trap, and the oxidized Hg is physically adsorbed onto potassium chloride (KCl) treated carbon. The sample volume that can be drawn through the trap before saturation of Hg occurs ranges from 15 to 5,000 L and is a function of the flue gas Hg concentration. After sampling is complete, the FAMS traps are sent to a laboratory for digestion and for analysis using EPA Method 1631 Revision E. As with the other sorbent trap Hg measurement techniques, this method provides no real-time flue gas Hg measurement, but provides an additional measurement for comparison with Hg concentrations derived from Hg SCEM and CMMS. 84 3.3.1.6 EPA Method 26A EPA Method 26A determines emissions of hydrogen halides (HCl, HBr, and HF) and halogens (Cl2 and Br2) from stationary sources. Gas and suspended particles are withdrawn isokinetically from the source and drawn through a sampling train containing an optional cyclone, a filter, and impingers that contain absorbing solutions. The cyclone collects liquid droplets; the filter collects particulate matter, including halide salts, and the acidic and alkaline absorbing solutions collect the gaseous hydrogen halides and halogens, respectively. The hydrogen halides, solubilized in the acidic solution, form chloride (Cl-), bromide (Br-), and fluoride (F-) ions. The halogens have a low solubility in the acidic solution and pass through to the alkaline solution, where they are hydrolyzed to form a proton (H+), the halide ions, and hypohalous acid (HClO or HBrO). Sodium thiosulfate, added to the alkaline solution, ensures reaction with the hypohalous acids to form a second halide ion so two halide ions are formed for each molecule of halogen gas. The halide ions in the separate solutions are then measured by ion chromatography. A typical analytical detection limit for HCl is 0.2 µg/mL, and detection limits for the other species should approach this limit. Method 26A has a possible negative bias below 20 ppm HCl, perhaps resulting from reaction with small amounts of moisture in the probe and filter. Similar bias for the other hydrogen halides is possible (EPA, 2008). Sun et al. (2000) reported that Cl2 precisely using Method 26A was difficult at concentrations less than 5 ppmv. Method 26A remains invalidated for use in flue gas streams having halide contents less than 20 ppmv (Dombrowski et al., 2008). Because flue gas concentrations of halogens during the 85 present test are expected to be below the validated threshold of 20 ppmv, the data from Method 26A were only used to make general observations. 3.3.1.7 EPA Method 17 During Phases I and IIA, mass concentrations of particulate matter emissions were measured at the inlet of the the cold-side ESP A casing using EPA Method 17. In conjunction with the data from the fly ash analytical methods, the particulate matter mass emission data enabled the determination of the Hg mass flow rate entering the ESP. Method 17 applies to the determination of PM emissions and within the procedure, particulate matter, suspended within the flue gas, is withdrawn isokinetically from the source and collected on a glass or quartz fiber filter maintained at stack temperature. The particulate matter mass that has been collected on the filter is determined gravimetrically after the removal of uncombined water through heating of the sample (EPA, 2000b). 3.3.2 Liquid and Solid Measurement Techniques 3.3.2.1 Wet FGD Slurry Analytical Techniques During Phase II of the program, wet FGD slurry samples were taken daily. Analyses for pH, ORP, and sulfite concentration were performed at the site. Additional liquid samples were sent to a laboratory for further analyses for Hg, sulfur and nitrogen compounds, cations, and anions. Table 3.7 provides a summary of techniques used in analyzing the wet FGD slurry. 86 Table 3.7 Wet FGD Slurry Analytical Methods Method Method Title Species/Property Portable meter n/a pH Portable meter n/a Oxidation Reduction Potential (ORP) Ion chromatography a n/a Sulfite ASTM D6414a Standard Test Methods for Total Mercury in Coal and Coal Combustion Residues by Acid Extraction or Wet Oxidation/Cold Vapor Atomic Absorption Mercury Ion chromatography a n/a Sulfur-nitrogen compounds a n/a Cations and anions Ion chromatography a. Measurements conducted by URS Austin Mercury Analytical Laboratory 3.3.2.2 Coal Analytical Techniques During Phases I, IIA, and IIB, coal samples were taken at the exit of the pulverizer using a coal fineness extraction tool. This technique involves inserting a probe into a tap on one of the eight coal conveying pipes leaving the pulverizer. Because coal was assumed to be uniform across all of the pulverizers, no preference was given to which pulverizers were sampled. After removal from three of the seven pulverizers, the samples were mixed and made into a composite sample. Because the samples were extracted at the exit of the pulverizer, a reduction in Hg from the coal as received at the plant was expected. During the coal pulverization process, pyrites are rejected, and pyrites are well known to contain Hg. During Phase III, the coal samples were taken 87 from the bulk coal loaded into the bunkers (i.e., before the pulverizer). In that case, the reported Hg values include the pyritic portion of the Hg. During all three phases of the research program, coal samples were analyzed for Hg concentration, halogen concentration and sulfur in addition to their ultimate and proximate analysis. Table 3.8 provides a summary of the ASTM testing used. Table 3.8 Coal Analytical Methodsa Method Method Title Properties ASTM D2013 Standard Practice for Preparing Coal Samples for Analysis Sample preparation ASTM D5142 Standard Test Methods for Proximate Analysis of the Analysis Sample of Coal and Coke by Instrumental Procedures Moisture Volatile Matter Ash Fixed Carbon ASTM D5373 Standard Test Methods for Instrumental Carbon Determination of Carbon, Hydrogen, and Hydrogen Nitrogen in Laboratory Samples of Coal Nitrogen ASTM D4239 Standard Test Method for Sulfur in the Analysis Sample of Coal and Coke Using High-Temperature Tube Furnace Combustion Sulfur ASTM D5865 Standard Test Method for Gross Calorific Value of Coal and Coke Heating value (Btu/lb) ASTM D6721 Standard Test Method for Determination of Chlorine in Coal by Oxidative Hydrolysis Microcoulometry Chlorine Bromine ASTM D6722 Standard Test Method for Total Mercury in Coal and Coal Combustion Residues by Direct Combustion Analysis Mercury a. All analyses were performed by Consol Laboratories in Phases I, IIA, IIB, and III. 88 3.2.2.3 Gypsum Analytical Techniques During Phase II of the program, gypsum solids were extracted from the slurry of the 2 MW pilot wet FGD and sent to a laboratory for analysis of the mass fractions of gypsum [CaSO42H2O], calcium carbonate [CaCO3], and inerts, and of Hg, and halogens. During Phase III, the solids were collected from the discharge of the Unit 3 and Unit 4 gypsum vacuum belt. Due to design constraints at the site, it was not possible to only obtain gypsum samples from Unit 4. During Phase III, gypsum samples were taken twice per week. Table 3.9 provides a summary of the analytical techniques that were used in analyzing the gypsum. Table 3.9 Gypsum Analytical Methods Method Method Title Species/Property Atomic Gypsum Purity Testing Adsorption, Ion Chromatography, and Coulimetrics Various ASTM D7348a Standard Test Methods for Loss on Ignition (LOI) of Solid Combustion Residues Loss on Ignition ASTM D6414a Standard Test Methods for Total Mercury in Coal and Coal Combustion Residues by Acid Extraction or Wet Oxidation/Cold Vapor Atomic Absorption Mercury Neutron Activationb n/a Bromine a. Analysis performed by URS Austin Mercury Analytical Laboratory in Phases I, II and III. b. Performed by McMaster University, Ontario, Canada. 89 3.2.2.4 Fly Ash Measurement Methods The Unit 4 cold-side ESP consists of two separate housings A and B. In Phases I, IIA, and IIB, the fly ash samples were taken from the middle two hoppers of the first and second rows of Housing A. A composite sample was sent to a laboratory for analysis of Hg content and loss on ignition (LOI). Table 3.10 summarizes the test methods used. Table 3.10 Fly Ash Analytical Methods Method Method Title Species/Property ASTM D7348a Standard Test Methods for Loss on Ignition (LOI) of Solid Combustion Residues Loss on Ignition ASTM D6414a Standard Test Methods for Total Mercury in Coal and Coal Combustion Residues by Acid Extraction or Wet Oxidation/Cold Vapor Atomic Absorption Mercury Neutron Activationb N/A Bromine a. Analysis conducted by URS Austin Mercury Analytical Laboratory in Phases I, II and III. b. Performed by McMaster University of Ontario, Canada. 3.4 Statistical Methods 3.4.1 Description of the Data The statistical significance of the effect of CaBr2 injection, during Phase III, on Hg emissions was determined by using various test methods. Table 3.11 provides a 90 listing of the independent and dependent variables used to determine the statistical significance of the effect of CaBr2 injection on Hg emissions from wet FGDs. Load magnitude, in Table 3.11, describes the mass flow of Hg into the system (i.e., coal flow is linearly proportional to load); unit load directly impacts the temperature of the flue gas. Phase III load data were transformed from scale data to nominal data by grouping load (MW) into three different ranges: (1) 600 MW < X < 720 MW, (2) 500 < X < 600 MW, and (3) X < 500 MW. Hg oxidation is partially dependent on flue gas temperature, which is directly related to unit load. CaBr2 injection status during Phase III was used as the second independent variable. For the entire Phase III test period, CaBr2 was added to the coal at a constant rate. For this reason, the data were transformed from a scalar value to a nominal value representing on or off. The Phase III Hg emissions in terms of concentration and emission rate were the dependent variables. The Hg emissions from Unit 4 were compared with those of Unit 3, which was never treated with CaBr2 during the research program. Unit 3 served as the control, allowing a comparison with Hg emission from an untreated unit burning the same coal and having a similar process train (e.g., boiler, SCR, cold-side ESP, and wet FGD). 91 Table 3.11 Independent and Dependent Variables Used to Tests for Statistical Significance of the Effect of CaBr2 Injection on Hg Emissions from Wet FGD Variable Type Variable Description Independent Load Independent CaBr2 Addition Dependent Unit 4 Hg Emissions Concentration Hourly Hg emissions expressed in µg/m3 measured at the wet FGD stack. Dependent Unit 3 Hg Emissions Concentration Hourly Hg emissions expressed in µg/m3 measured at the wet FGD stack Unit 4 Hg Emission Rate 30-day Rolling Average Calculated 30-day rolling average Hg emission rate measured at the wet FGD stack during CaBr2 addition on Unit 4. Unit 3 Hg Emission Rate 30-day Rolling Average Calculated 30-day rolling average Hg emission rate measured at the wet FGD stack during CaBr2 addition on Unit 4. Dependent Dependent Data Transformation Codes 1 – 600MW – 720 MW 2 – 501 MW – 599 MW 3 – 300 MW – 500 MW 1 – Off 2 - On The installation of permanent CMMS on Unit 3 and Unit 4 provides a unique opportunity to view Hg emissions for both units before, during, and after the CaBr2 injection testing. Table 3.12 provides a summary of the various periods for which data were collected on the independent and dependent variables listed in Table 3.11. 92 Table 3.12 Time Periods During Which Independent and Dependent Data Were Collected for Statistical Significance Analysis Time Period Activity September 1-September 30, 2010 Pre-CaBr2 Injection Period October 5-December 12, 2010 Continuous CaBr2 Injection January 1-January 30, 2011 Post CaBr2 Injection Period 3.4.2 Descriptive Statistics Statistical measurements, including the sample mean, standard deviation, kurtosis, and skewness coefficients, were used to describe the Hg measurements. Histograms and probability–probability plots (P-P plot) were used as visual aids in determining the normality of Hg emission rate and concentration data from Units 3 and 4. The JarqueBera statistic a numerical measure of normality was used (Allen, 2011). 3.4.3 Statistical Tests Used to Evaluate Population Means In the evaluation of statistical significance three main test procedures were used: (1) unpaired (i.e., independent) t-test (2) paired t-test, and (3) Wilcox Ranked Sign test. A t-test can be used to test for statistical significance if the data meet the following criteria: (1) the dependent variable is continuous (2) each observation of the dependent variable is independent of the other observations of the dependent variable, and (3) the dependent variable is normally distributed. The t-test has been shown to remain valid even if the dataset has minor deviations from normality (Lumley et al., 2002). 93 The Wilcox Ranked Sign test is a non-parametric statistical hypothesis test used when comparing two related samples, matched samples, or repeated measurements on a single sample to assess whether their population means differ. The conditions for this test are: (1) samples does not have to follow a random distribution, (2) independence exists between the two random samples, and (3) populations do not have to be normally distributed. Statistical significance determines the likelihood that an observed finding could have occurred by chance. The test of significance does not say anything about the magnitude of the effect. The magnitude of effect describes how much of the dependent variable can be controlled, predicted, or explained by the independent variable (Snyder and Lawson, 1993). Cohen’s d statistic was used to describe the magnitude of effect for the independent variable of interest. Cohen’s d is an appropriate effect size measure for the comparison between two means and can be coupled with the results of a t-test to show the degree of differences between the two means by the independent variable. Cohen's d is computed by dividing the mean difference between groups by the pooled standard deviation. A Cohen’s d value of 0.2 means that the difference in the means is small (i.e., a small degree of difference), whereas a Cohen’s d greater than 0.8 indicates a large degree of difference. (Weinberg and Abromowitz, 2008). The partial eta squared was computed as another measure of degree of effect and provides a quantifiable measure of the correlation between an independent and a dependent variable (Barnette, 2006). A large value of eta squared indicates that the differences between two means is largely explained and is correlated to the independent variable. 94 3.4.3.1 Statistical Tests for Hypotheses 4 and 5 Table 3.13 provides a summary of the statistical tests used to evaluate the statistical significance of the effect of the independent variables (load and CaBr2 injection on/off) on wet FGD stack Hg concentrations and emission rates. The table includes the independent and dependent variables used in the analysis, the statistical methods used, the null hypotheses tested, the significance levels serving as the criteria for significance. 95 Table 3.13 Statistical Tests Performed in Evaluating Hypothesis 4 and Hypothesis 5 Hypothesis Tested Independent Variable Dependent Variable(s) Null Hypothesis Test Type Significance Level 4 CaBr2 addition on/off Unit 3 wet Stack Hg Concentration µBr = µno Bra Independent t-Test 99% 4 Time period Unit 4 wet Stack Hg Concentration µSep = µJanb Independent t-Test 99% 4 CaBr2 addition on/off Unit 4 wet Stack Hg Concentration µBr = µno Brc Independent t-Test 99% 4 CaBr2 addition on/off Unit 3 and Unit 4 wet Stack Hg Concentration µU3Br = µU4Brd Paired t-Test 99% 5 CaBr2 addition on/off Unit 3/Unit 4 30-day rolling average Hg Emission Rate Wilcox Ranked Sign Test 99% µU3Br = µU4Br d Notes: µBr - mean during CaBr2 addition; µno Br - mean without CaBr2 addition; µSep – mean during month of September; µJan- mean during month of January; µU3Br- Unit 3 mean during CaBr2 addition; and µU4Br – Unit 4 mean during CaBr2 addition. a. Comparison of means of Unit 3 dependent variable when CaBr2 was being added on Unit 4 and was not being added on Unit 4. b. Comparison of means of Unit 4 dependent variable during months of September and January, when CaBr2 was not being added to Unit 4. c. Comparison of means of Unit 4 dependent variable when CaBr2 was being added on Unit 4 and was not being added on Unit 4. d. Comparison of means of Unit 3 and Unit 4 dependent variables when CaBr2 was being added on Unit 4. 96 CHAPTER 4 RESULTS 4.1 Introduction Although each phase was conducted independently, this section handles as one large data set the data produced during the study. Hypotheses-based analysis was used to determine whether CaBr2 injection technology enhances the ability of coal-fired units burning PRB coal, which is low in halogens, to meet the MATS rule. The analysis was undertaken to answer four global questions: • Can coal-fired boilers that burn PRB coal and are equipped with SCR, coldside ESP and wet FGD meet federal regulations for Hg emissions without the need for additional control technology? • Can CaBr2 injection be utilized on a pulverized-coal boiler burning PRB coal to increase the fraction of oxidized Hg? • Can the oxidized Hg created via CaBr2 injection be effectively removed from the flue gas in sufficient quantities to meet a 30-day Hg emissions rolling average of 1.2 lb/TBtu? • Can the presence of an SCR improve the cost effectiveness of CaBr2 injection technology? To conclusively answer these questions, six hypotheses are investigated in detail within this chapter. 97 4.2 Hypothesis 1: Burning PRB Coal Results In Baseline Hg Oxidation Levels Below 50% Under All Operating Conditions. 4.2.1 Baseline Hg Oxidation Analysis Figure 4.1 provides a graphical representation of Unit 4 Hg oxidation behavior during baseline conditions in all phases. The Hg oxidation ratio plotted on the vertical axis and defined as the ratio of oxidized Hg to total Hg (Coxidized / Ctotal), effectively normalizes the oxidized Hg present by the total Hg concentration in the flue gas. This ratio provides insight into data trends while the overall concentration of Hg changes. An Hg oxidation ratio of 1 indicates that all of the Hg present is in the oxidized form, and a value of zero indicates that all of the Hg present is in the elemental form. The horizontal axis in Figure 4.1 represents the location at which the various speciated Hg measurements were made. The data are grouped by the operating conditions of the SCR as follows: (1) the SCR was in service with NH3 injected to reduce NOx emissions, (2) the SCR was in service without NH3 injection, and (3) the SCR was bypassed (i.e., not in service). Figure 4.1 illustrates that Hg oxidation increases as the flue gas travels through the system. The fraction of oxidized Hg is greater at the wet FGD inlet than at the SCR inlet for all given test conditions. The lowest oxidation ratio (0.05) is found at the SCR inlet, and the highest ratio (0.85) occurs at the wet FGD inlet. This represents a wide range of oxidation ratios. 98 Figure 4.1 Hg oxidation at baseline conditions (i.e., no CaBr2 addition to the coal) as a function of the location of Hg concentration measurement and of SCR operating condition. The SCR inlet Hg oxidation ratio values range from a minimum of 0.05 to a maximum of 0.42. A closer inspection of the data used to create Figure 4.1, which can be found in Appendix A, and reveals that the highest two Hg oxidation ratios (>0.30) at the SCR inlet were measured during Phase I, when the native bromine concentration in the coals was the highest. Hg oxidation at the SCR inlet would result from homogeneous and native particle heterogeneous oxidation. Native particle heterogeneous oxidation contribution may be small because unburned carbon levels at this plant are below 0.5 wt 99 % as a result of efficient combustion. Bhardwaj et al. (2009) reported that 40 wt % UBC was needed to achieve 42% Hg oxidation at 150 °C and 50 ppmv HCl. The oxidation of Hg requires chlorine, bromine, or another halogen, either from native concentrations in the coal or added via external means. Table 4.1 provides a summary of the coal chlorine and bromine content as well as other coal summary information during the three phases. As Table 4.1 shows, measurable concentrations of bromine were found in the coal samples during Phase I but not during the other phases. Besides Phase I, the bromine concentrations reported in the table are the detection limit of the measurement technique used. The detection limits were used to calculate the Br/Hg ratio (lb/lb), Br/Hg ratio average and standard deviation. Hence, those values of Br/Hg ratio should be viewed as generous because the actual bromine level in the coal is probably lower. Gutberlet et al. (2008) postulated that the Hg oxidation potentials of chlorine and bromine are different and that on a molar basis, bromine proved 10 times more effective than chlorine at oxidizing Hg. A calculated molar Cl/Br ratio of 10 would mean a flue gas where bromine and chlorine have the same oxidative abilities. However, the concentration of bromine and chlorine found in the coal during this study indicates that baseline Hg oxidation via chlorine was more likely during Phases IIA, IIB and III since on a molar basis in the coal, higher concentrations of chlorine are found. During Phase I, baseline Hg oxidation was more likely to occur from bromine since the Cl/Br molar ratio was less than 10. The molar ratio of Cl/Br ranged from a low of 6 in Phase I to approximately 30 in Phase IIB and III and a high of 60 in Phase IIA. 100 Table 4.1 Coal Characteristics Summary Units Phase I Phase IIA Phase IIB Phase III No. of samples Dimensionless 8 8 6 11 Sulfur average wt% 0.33 0.35 0.31 0.40 Hg average wt ppm 0.073 0.051 0.068 0.047 Hg standard deviation wt ppm 0.021 0.007 0.019 0.013 Cl average wt ppm 14.50 25.75 13.17 19.55 Cl standard deviation wt ppm 14.77 8.19 1.72 3.56 a a Description Br average wt ppm 5.82 <1.0 <1.0 <1.3a Br standard deviation wt ppm 1.23 n/a n/a n/a Br/Hg ratio lb/lb 87.82 20.14b 15.34b 29.42b Br/Hg standard deviation lb/lb 36.29 2.81b 3.13b 8.08 a. detection limit of measurement technique b. calculated based on detection limit as highest concentration of bromine present Column 3 Adapted from Table B-8 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2007 p. B-7. Copyright 2007 by EPRI. Reprinted with permission. Column 4 Adapted from Table 33 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. 3-51. Copyright 2009 by EPRI. Reprinted with permission. Column 5 Adapted from Table B-13 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. B-14. Copyright 2009 by EPRI. Reprinted with permission. Column 6 Adapted from Table B-14 “Three-Month Evaluation of Furnace Addition of Calcium Bromide for Mercury Emissions Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2011 p. B-16. Copyright 2011 by Southern Company Serivces. Reprinted with permission. 101 The fraction of oxidized Hg during baseline conditions indicate that the native halogen content in the coal was sufficient to support relatively high oxidation of Hg at the wet FGD inlet (ranged from 0.42 to 0.85). It is unclear if chlorine or bromine or a combination of both was responsible for the oxidation. It is interesting to note that at the wet FGD inlet the Hg oxidation ratios were highest when NH3 was not present in the SCR. Vosteen et al. (2003) stated that a Br/Hg ratio (lb/lb) of 100:1 was needed to achieve 100%Hg oxidation with bromine. Table 4.1 includes a calculated value for the mass ratio of Br to Hg, hereafter referred to as the Br/Hg ratio (lb/lb). During Phase I, the Br/Hg ratio averaged 87.82, with a standard deviation of 36.29. Therefore, at some point during Phase I, the Br/Hg ratio exceeded 100:1. Vosteen et al. (2006) did not indicate the precise Br/Hg ratio at which high levels of Hg oxidation would be observed for specific coals, but the wide range of values provided (100:1 to 10,000:1) might lead to the conclusion that observed Hg oxidation behavior might be dependent on other factors, as well. During Phases IIA, IIB, and III, the Br/Hg ratios were well below the 100:1 guidance for achieving high levels of Hg oxidation via bromine. The SCR outlet Hg oxidation ratios ranged from a minimum value of 0.17 to a maximum value of 0.58. The presence of the SCR should increase the fraction of oxidized Hg present and thereby increase the Hg oxidation ratio. While in service, the ability of an SCR to affect Hg oxidation will be a function of a number of factors such as coal chlorine and bromine content, catalyst pitch, space velocity, flue gas temperature, 102 NH3 flow; and catalyst activity. As Figure 4.1 shows, the Hg oxidation ratios do increase across the SCR, as expected. As Figure 4.shows, the largest fraction of oxidized Hg was observed at the wet FGD inlet, when the SCR was in service but without NH3 addition. The range of Hg oxidation ratios diverge for the SCR with NH3 and for the SCR without NH3. The SCR without NH3 configuration should provide the best oxidation behavior because the NH3, oxidant (bromine or chlorine), and Hg all compete for the same active sites on the surface of the catalyst. He et al. (2009) suggested that, in an SCR, the Hg oxidation occurred via the Langmuir-Hinshelwood mechanism, as shown in R29–R32. During these reactions, the Hg and oxidant (bromine or chlorine) adsorb onto an active site on the catalyst surface. After adsorption is complete, R31 occurs, and the newly formed oxidized Hg is liberated from the catalyst site to the flue gas. Hong et al. (2010) concluded that NH3 dominantly adsorbs onto the SCR catalyst surface and precludes the optimum absorption or retention of absorbed Hg on the catalyst surface. Senior and Linjewile (2004) concluded from an analysis of bench-scale data that Hg oxidation across the SCR decreased in the presence of NH3. From the literature, one concludes that Hg oxidation performance should improve when NH3 is not present. Figure 4.1 supports this conclusion. In fact the Hg oxidation ratio was highest (0.85) at the wet FGD inlet during baseline conditions when the SCR was in service without NH3 present. Ignoring the results from the SCR without NH3 test conditions at the wet FGD inlet, during Phase I the highest fractions of oxidized Hg were achieved at the wet FGD inlet, from 0.56 to 0.67. This result may indicate an ability of the SCR to aid in the oxidization of Hg at very low halogen concentrations with the absence of NH3. This result indicates that the SCR may 103 produce chlorine or bromine species (e.g., Cl2, Cl, Br2, and/or Br) that remain active in Hg oxidation reactions downstream of the SCR. Figure 4.1 also reveals that Hg oxidation continues downstream of the SCR, and that, for a given test day, the fraction of oxidized Hg is greater at the ESP inlet than at the SCR outlet. Hg oxidation continues to occur before the wet FGD inlet, and in some cases, at substantial levels, that is, 50% of the Hg oxidation happens downstream of the SCR. Explanations in the literature may provide some insight into this behavior. Fry et al. (2007) found that, as the flue gas quench rate changed, so did the effectiveness of HCl as an Hg oxidant. The quench rate describes the flue gas-cooling rate downstream of the boiler to the cold-side ESP. The quench rate at Miller Unit 4 typifies that of a full-scale boiler. Fry et al. (2007) concluded that boilers with a typical boiler quench rate (-440 K/s) continued to oxidize Hg until reaching the cold-side ESP temperature. Fry et al. (2007) concluded from their analysis that the quench rate was important for homogeneous Hg oxidation by chlorine radicals. Because Hg oxidation continued to occur downstream of the SCR during all three phases of the research program, completed under different conditions and at different times, the oxidation behavior can be considered repeatable and consistent. The two trendlines in Figure 4.1 represent the impact of the SCR in Hg oxidation with and without an SCR. The steeper line represents Hg oxidation when NH3 is not present (i.e., more complete oxidation). In both cases, during baseline conditions, Hg oxidation continues to occur as the flue gas travels through the system. In the case of an SCR without NH3, the level of Hg oxidation proceeds to a higher extent. 104 4.2.2 Equipment Configuration Impacts on Baseline Hg Oxidation The equipment installed and the specific design of that equipment can affect the ability of a system to promote or inhibit Hg oxidation. For example, the efficiency of the combustion process can inhibit or enhance the Hg oxidation process. Inefficient combustion leads to higher concentrations of UBC in the fly ash, which can act as an Hg oxidation catalytic surface (Niksa et al., 2001). Additionally, the SCR directly affects the ability of the system to oxidize Hg, as depicted in Figure 4.1. This effect depends on factors such as coal chlorine and bromine content, catalyst pitch, space velocity, flue gas temperature, catalyst age, NH3 flow, and catalyst activity. Table 4.2 provides a summary of the important Unit 4 SCR equipment design and operational parameters that impact Hg oxidation behavior. Senior and Linjewile (2004) concluded that SCR space velocity below 2,000 h-1 yielded Hg oxidation values much higher than those values found for SCR space velocity above 4,000 h-1. As shown in Table 4.2, the SCR at Miller Unit 4 had a space velocity of 1,974 h-1 during Phases I, IIA, and IIB and a space velocity of 1,480 h-1 during Phase III. This result suggests that the ability of the SCR to aid oxidation was ideal because the space velocity during all phases remained below the 2,000 h-1 threshold limit suggested by Senior and Linjewile (2004). From a space velocity perspective, the Unit 4 SCR is generously designed and will promote Hg oxidation. The literature does not suggest an ideal space velocity but indicated that lower SCR space velocity (< 2,000 h-1) promotes Hg oxidation. Eswaran and Stenger (2008) concluded that catalyst age reduces Hg oxidation catalyst activity. The exposure hours for the catalyst in service at Unit 4 exceeded the 105 exposure hour experience available in the literature. The most exposed SCR catalyst tested at bench scale by Eswaran and Stenger (2008) involved only 3,300 h of exposure. The Unit 4 catalyst had been exposed to flue gas for 13,250 h during the Phase I testing. During Phase III, three of the four catalyst layers were exposed to flue gas for 27,500 h, and the fourth layer had 6,000 h of flue gas exposure. The literature provided little information on the relationship between catalyst age and Hg oxidation but did include general conclusions that the ability of a catalyst to aid in the oxidation of Hg decreased as time of catalyst exposure to flue gas increased. In comparison with catalyst age, relative NOx catalyst activity (K/Ko) may more accurately measure the ability of a catalyst to oxidize Hg because some flue gases contain more or fewer contaminants (such as potassium and arsenic) that affect catalyst performance. The relative NOx catalyst activity shown in Table 4.2 exceeds 0.70 over the life of the program but did decrease with time, from 0.79 during Phase I to 0.75 during Phases IIA and IIB. By Phase III, the relative catalyst activity of the first two layers decreased to 0.50, but the addition of the new layer of catalyst with a relative catalyst activity of 1.0 brought the average relative catalyst activity of the entire SCR to 0.72. The new layer of catalyst brought the total number of layers in the SCR to four. The change in relative NOx catalyst activity during the research program did not affect the ability of the system to support Hg oxidation. This conclusion is based solely on the results of this study because the literature provided no guidance in this matter. 106 Table 4.2 Important Equipment Design and Operating Data Values that Affect Hg Oxidation Item Symbol Units Value Catalyst type n/a n/a Honeycomb Catalyst pitch n/a mm 9.2 SCR normal operating temperature T °C 380 SCR flue gas flow under standard conditions V m3/h 2,700,000 Phase I & II catalyst volume V m3 1,368 Phase III catalyst volume V m3 1,824 Phase I & II catalyst layers n/a n/a 3 Phase III catalyst layers n/a n/a 4 Phase I & II SCR space velocity SV h-1 1,974 Phase III SCR space velocity SV h-1 1,480 Phase I catalyst age n/a h 13,250a Phase I catalyst activity ! !! Dimensionless 0.79c Phase IIB catalyst age n/a h 15,000a Phase IIB catalyst activity ! !! Dimensionless 0.75c Phase III catalyst age n/a h Phase III catalyst activity ! !! 27,500a 6,000b Dimensionless 0.72c NOx set point n/a lb/MBtu 0.1 α mol/mol 0.9 UBC wt% 0.40d Design NOx/NH3 molar ratio Unburned carbon a. b. c. d. Operating hours since catalyst was loaded in 2003. Operating hours of new 4th layer added in January 2010. K/K0 is the arithmetic mean of the K/K0 for each layer. Average of unburned carbon values for all three phases. 107 Designed to operate at 380 °C during full-load conditions (720 MW), the Unit 4 SCR has a minimum continuous operating temperature set point of 310 °C. During Phases I, IIA, and IIB, the SCR operated mostly at 380 °C (i.e., at full-load conditions). During Phase III testing, when the boiler was operated normally (i.e., load was allowed to vary to meet electricity demand), the SCR operated between 380 °C and 310 °C. Hong et al. (2010) postulated that Hg oxidation was sensitive to SCR operating temperature. Senior (2006) concluded from data analysis of full-scale operating SCRs, that Hg oxidation rates across an SCR were higher at 320 °C than at 370 °C. When Hg oxidation levels resulting from the actual SCR operating temperature used in this study were compared with those reported in the literature, it was discovered that the Unit 4 SCR operating temperature does not overly constrain baseline Hg oxidation. Figure 4.1 shows that the Hg oxidation ratio at the SCR outlet ranged from 0.18 to 0.60. Unfortunately, speciated Hg measurements were not made at the SCR inlet during Phase III when lower SCR temperatures were observed. Using the guidance of Senior (2006), one might have expected higher fractions of oxidized Hg at lower SCR temperatures, however this possibility was not investigated during the research program. 4.2.3 Effect of SO2 Concentration The concentration of fuel sulfur is another parameter to consider when evaluating a system for Hg oxidation performance. Sulfur is converted to SO2 during the combustion process. During bench-scale testing, SO2 has been shown to negatively impact the ability of chlorine and bromine compounds to oxidize Hg. Sterling et al. (2004) showed that SO2 greatly inhibited Hg oxidation by Cl2. In their report, Lighty et 108 al. (2006) stated that increased SO2 concentration, via the Griffin reaction, affected Cl2 based homogeneous Hg oxidation. Buitrago et al. (2010) found in their bench-scale studies that SO2 could also negatively impact bromine based homogeneous oxidation. Vosteen et al. (2006) reported that SO2 negligibly affects Hg oxidation when bromine is the Hg oxidant. The literature does not provide clear guidance for describing conclusively the effect of SO2 on the heterogeneous oxidation regime. In terms of sulfur content found in US coals, PRB coals contain some of the lowest fractions of sulfur (Energy Information Agency, 1993). A review of Table 4.1 shows that the percentage of sulfur in the coal during the research program ranged from 0.27 wt% to 0.56 wt%, with an average value of 0.35 wt%. This average sulfur input into the combustion process at Unit 4 represents a SO2 flue gas concentration of approximately 350 ppmv. When the low levels of sulfur in the coal used during this study and the guidance from Vosteen et al. (2006) are considered, it may be safe to conclude that the SO2 levels expected at Unit 4 would not adversely impact Hg oxidation when sufficient levels of bromine are present. 4.2.4 Effect of Flue Gas HBr and HCl Concentration on Baseline Hg Oxidation In accordance with the baseline coal concentrations of bromine shown in Table 4.1, the expected flue gas concentration of HBr ranged 0.04 to 0.25 ppmv during Phases I and IIA. Table 4.3 summarizes the baseline concentrations of halogens measured by Method 26A. 109 Table 4.3 Flue Gas HCl, HBr, Cl2, and Br2 Concentrations During Baseline Conditions Compound Units Phase I Phase IIA Phase IIB Phase III HBr ppmv <0.08 0.047 not tested not tested Br2 ppmv <0.03 0.003 not tested not tested HCl ppmv 1.08 0.950 not tested not tested Cl2 ppmv 2.01 0.012 not tested not tested Notes: Concentrations on a dry basis at 3% O2 Column 3 Adapted from Table B-7 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2007 p. B-6. Copyright 2007 by EPRI. Reprinted with permission. Column 4 Adapted from Table B-9 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. B-7. Copyright 2009 by EPRI. Reprinted with permission. Baseline halogen flue gas concentrations were low and likely insufficient to support sustained high Hg oxidation rates. Results of the Method 26A performed yielded low concentrations of HBr, Br2, HCl, and Cl2; however the accuracy of these speciated measurements remains unknown. Sun et al. (2000) reported that Cl2 measurement and accuracy in quantifying HX or X2 by using Method 26A are difficult to achieve at Cl2 concentrations <5 ppm. In a broader sense, the total concentration of bromine (HBr and Br2) and chlorine (HCl and Cl2) is likely the proper context in which to interpret the information. Even in this broader view, the bromine and chlorine concentrations are low. The bromine and chlorine compound concentrations reported in Table 4.3 are lower than those reported in the literature to support high levels of Hg oxidation. For instance, Silcox et al. (2008) concluded that 50 ppmv of HCl was needed to achieve a high rate of (>80%) homogeneous based Hg oxidation and that at least 20 ppmv of HBr would be needed to achieve at least 60% homogeneous oxidation. Additionally, Cao et 110 al. (2008) reported that 3 ppmv HBr produced 80% oxidized Hg in a bench-scale SCR with PRB simulated flue gas, and Lee et al. (2008) reported that 20 ppmv HCl produced 88% oxidized Hg in a bench-scale reactor under simulated PRB flue gas conditions. The measured chlorine and bromine flue gas concentrations were at least two orders of magnitude below those demonstrated in the literature to support high fractions of oxidized Hg. If the 100:1 Br/Hg ratio (lb/lb) guidance by Vosteen et al. (2003) and the Phase I coal Hg content are used, approximately 0.35 ppmv of HBr (7.5 wt ppm of Br on the dry coal) would be needed for full Hg oxidation to occur. The measured HBr concentration was one order of magnitude below what was required. On the basis of the literature and the guidance by Vosteen et al. (2003), one should expect Hg oxidation rates below 90% under all baseline conditions. 4.2.5 Operational Impacts on Hg Oxidation The operating conditions of a power plant affect its ability to promote or hinder Hg oxidation. For Phases I, IIA, and IIB, Unit 4 was operated under full-load conditions. During Phase III, the unit was operated under normal conditions (i.e., the unit responded to the demand for electricity). Chapter 3 contains a detailed description of all test conditions. Figure 4.2 depicts a Box and Whisker Plot of key operational parameters during Phase I. The plot shows the 25%, 50%, and 75% quartile values (box) for each parameter of interest, as well as bars (whisker) that indicate the maximum and minimum values of the dataset. Plots may include data points outside the whiskers that have been labeled as 111 extreme values in the data set as defined by SPSS, the statistical software package used to generate the plots. Figure 4.2 Phase I summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), SCR inlet and outlet NOx concentrations (ppmv), and stack SO2 concentration (ppmv) used to illustrate consistency or variability of operating conditions when SCR is in service and with NH3 injection. Figure 4.2 shows that, for the duration of the Phase I program, operation conditions were held constant. The operating range, listed in parentheses, was close for each of the following operational parameters: unit load (702-715 MW), SCR inlet temperature (364-378 °C), SCR outlet temperature (357-375 °C), SCR inlet NOx (170200 ppmv), and SCR outlet NOx (31-33 ppmv). Stack SO2 did have a wider operating 112 range, but half of the SO2 emissions (75% quartile to 25% quartile) fell between 381 ppmv and 317 ppmv. The consistent operations during this phase limited the impact of operating conditions on Hg oxidation behavior. Figure 4.3 is a summary plot of Phase IIA operational data during two separate testing conditions: when the SCR was bypassed and when the SCR was in service but without NH3 injection. Figure 4.3 Phase IIA summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), SCR outlet NOx concentration (ppmv), and stack SO2 concentration (ppmv) used to illustrate consistency or variability of operating conditions during periods when SCR is bypassed and when SCR is in service without NH3 injection. 113 The load during both SCR conditions was above 715 MW 75% of the time, with a few lower-load conditions occurring outside test periods. SCR inlet NOx information was unavailable during the test, however because NH3 was not injected during Phase IIA, inlet NOx concentration would have been identical to the observed range of outlet NOx concentration, which were 109 to 155 ppmv. SCR inlet and outlet temperatures were fairly constant during the test program, reaching a maximum value of 380 °C and 375 °C, respectively. The average SCR temperature during Phase IIA was 362 °C. The SO2 concentrations generally exceeded those observed during Phase I. With the SCR bypassed, the 75% quartile concentration was 477 ppmv, and the 25% quartile concentration was 340 ppmv; the maximum concentration was 631 ppmv. With the SCR in service, the 75% quartile concentration was 427 ppmv, the 25% quartile concentration was 328 ppmv; the maximum concentration was 634 ppmv. These SO2 concentrations may be sufficiently high to impact Hg oxidation via the Griffin reaction. Vosteen et al. (2006) reported that bromine is affected by SO2 to a lesser extent than chlorine, but bromine is affected nevertheless. The exact SO2 concentration in which bromine is adversely affected is not well understood. As the flue gas SO2 concentration increases so does the risk that the bromine Griffin reaction (R11) will occur. Although outside the scope of this research, the impact of SO2 concentration on Hg oxidation behavior is of keen interest and should be investigated further. Figure 4.4 depicts a summary plot of Phase IIB operating conditions when the SCR was in service with NH3 injection to control NOx emissions. The figure shows that for the duration of the Phase IIB program, operation conditions were held fairly constant. 114 The operating range, with minimum and maximum listed in parentheses, was relatively close for each of the following operational parameters: unit load (699-725 MW), SCR inlet temperature (367-382 °C), SCR outlet temperature (363-377 °C), SCR inlet NOx (164-208 ppmv), and SCR outlet NOx (24-48 ppmv). The SO2 concentrations were not available in the plant historian for this period and are not shown. Figure 4.4 Phase IIB summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), and SCR inlet and outlet NOx concentrations (ppmv) used to illustrate consistency or variability of operating conditions during a period when SCR was in service with NH3 injection. Figure 4.5 is a Box and Whisker summary plot of operating conditions during Phase III, when Unit 4 was operated normally (i.e., operated to meet electricity demand). 115 Because the load was not held constant, Figure 4.5 reveals a much wider load-operating window and the data also include a shutdown and start-up event. Figure 4.5 Phase III summary Box and Whisker Plot of load (MW), SCR inlet and outlet temperatures (°C), SCR inlet and outlet NOx concentrations (ppmv), wet FGD inlet SO2, and outlet SO2 concentrations (ppmv) used to illustrate consistency or variability of operating conditions during a period when SCR was in service with NH3 injection. The SCR inlet and outlet full-load operating temperature ranges (i.e., 75% and 25% quartiles) were of the magnitude seen in the earlier phases (i.e., SCR inlet 355 to 365 °C and SCR outlet 351 to 361 °C). The SCR did experience lower temperatures during periods of lower load and reached a temperature of 310 ºC during those periods. 116 According to Senior (2006), the lower operating temperature should support higher Hg oxidation. The inlet wet FGD SO2 concentrations during Phase III were the lowest observed during the research program, with a 75% quartile concentration of 213 ppmv, a 25% quartile concentration of 171 ppmv, and a maximum observed concentration of 357 ppmv. The lower SO2 concentration should lessen the impact, via the Griffin reaction, on Hg oxidation behavior if in case impact to Hg oxidation occurred at the higher concentrations of SO2. In terms of SO2 concentration, Phase III conditions are ideal to support Hg oxidation. An examination of the SCR data revealed that average outlet NOx emission levels were slightly higher than those found for Phase I. The NOx relative catalyst activity (K/Ko) was highest (0.79) during Phase I and lowest (0.72) during Phase III. During Phase I, the average outlet NOx emissions were 32 ppmv, with an average inlet concentration of 182 ppmv (82% removal efficiency). During Phase III, the average outlet NOx emissions reached 40 ppmv, while the average inlet NOx emissions were 167 ppmv (76% removal efficiency). These values suggest that NOx removal efficiency decreased between the two phases, which may also imply a slightly less effective SCR for supporting Hg oxidation. 4.2.6 Summary An analysis of baseline data did not support the hypothesis that Hg oxidation levels would be observed below 50% under all conditions. It is possible to attain baseline Hg oxidation rates above 50% while burning PRB coal at Plant Miller Unit 4. In fact, at the wet FGD inlet, a majority (i.e., >50%) of the Hg found during the various test periods was oxidized (see Figure 4.1). A thorough analysis determined that several elements of 117 the Miller Unit 4 system promote Hg oxidation. In addition to showing that the hypothesis was incorrect, the analysis led to the following generalizations: • The halogen content of the coal was highlighted as inadequate to support complete Hg oxidation. The addition of halogens to the coal before combustion could correct this deficiency. • During all three phases, Hg oxidation continued to occur downstream of the SCR. • The hours of Unit 4 SCR catalyst exposure to flue gas and the effect of these hours of exposure on Hg oxidation were outside what was investigated and documented in the literature. By Phase III, the first three layers of catalyst had been exposed to flue gas for more than 27,000 h, but an addition of a new catalyst layer before Phase III may have mitigated any impact on Hg oxidation. • Based on current technical understanding, Unit 4 SCR space velocity of <2000 h-1 is ideal for promoting Hg oxidation. • The NOx relative catalyst activity (K/Ko) decreased slightly during the program, from 0.79 at the start of Phase I to 0.72 at the start of Phase III and this decrease may slightly impact the ability of the SCR to promote Hg oxidation. • The SCR design operating temperature (380 °C) did not adversely impact Hg oxidation across the SCR. It is anticipated that lower SCR temperatures would improve baseline Hg oxidation behavior. 118 Examining baseline Hg oxidation behavior, enabled the development of an understanding of ability of the system to promote Hg oxidation. Table 4.4 provides a qualitative overview of the ability of Plant Miller Unit 4 to promote Hg oxidation. Table 4.4 Qualitative Summary of Miller Unit 4 Ability to Support Hg Oxidation Topic of Interest Favorable for Hg Oxidation Description Fuel sulfur Yes Griffin reaction impact is low because of low flue gas SO2 concentrations. Coal halogen No Low concentration of bromine and chlorine. SCR operating temperature SCR catalyst design Relative NOx catalyst activity Neutral Yes Neutral Maximum operating SCR temperatures are below 380 ºC. Pitch of 9.2 mm supports Hg oxidation. Maintained K/K0 above 0.7, which is sufficient to support Hg oxidation. SCR space velocity Yes Space velocity < 2,000 h-1 has been shown to promote Hg oxidation. Catalyst age No SCR reactor contains catalyst with extended exposure to flue gas. Yes Data supports the continued occurrence of Hg oxidation downstream of SCR and before wet FGD. Quench rate Unburned carbon Neutral Efficient combustion keeps unburned carbon levels below 0.5 wt% (UBC/fly ash). 119 4.3 Hypothesis 2: Sufficient CaBr2 Addition at a Unit Burning PRB Coal Results in Hg Oxidation Levels in Excess of 90% Under the best scenario during baseline conditions, the Hg oxidation ratio did not reach 0.90 (i.e., 90% Hg oxidation). As Table 4.4 indicates, Miller Unit 4 has a number of characteristics that promote Hg oxidation. One major deficiency found related to the low concentrations of bromine and chlorine in the coal. The addition of either would likely address that particular deficiency. During the research program, CaBr2 was added to the coal at various rates, and speciated Hg measurements were made at various locations in the flue gas stream to determine whether the elemental Hg could be converted to oxidize Hg by addition of bromine. 4.3.1 CaBr2 Addition Rate Strategy CaBr2 addition rates were chosen at random to determine the dose-response of Hg oxidation. Phase I involved varying CaBr2 addition rates to achieve Br concentrations from 2 to 328 wt ppm on the dry coal (calculation procedures to determine Br concentration can be found in Chapter 3). The goal consisted of determining the Hg oxidation behavior as a function of Br concentration. Placing the SCR in and out of service enabled determination of the effect of the SCR on Hg oxidation behavior after the addition of CaBr2. During Phase IIA, research protocol included a short replication of Phase I and operation of the unit for a longer period at 25 and 50 wt ppm Br concentrations (on the dry coal) with the SCR in service without NH3 injection. During Phase IIB, Br concentrations of 17 and 25 wt ppm (on the dry coal) were investigated with the SCR in service with NH3 injection. 120 This section contains analyses of data from Phases I, IIA and IIB. These analyses were undertaken to determine the behavior of elemental Hg in the presence of different Br concentrations (wt ppm on the dry coal). 4.3.1.1 Impact of Br/Hg Injection Ratio on Hg Oxidation Table 4.5 was constructed from the combination of Br coal concentrations, results from Hg coal analyses, and wet FGD inlet Hg speciation measurements. Table 4.5 provides insight into the proper Br/Hg ratio needed to achieve Hg oxidation rates above 90% with the use of PRB coal. As the information in Table 4.5 indicates, the Br/Hg ratio needed to obtain high fractions of oxidized Hg depends on the availability of an SCR. At Br/Hg ratios below 1,200, the Hg oxidation ratio was less than 0.60 at the SCR inlet. Upstream of the SCR inlet, homogeneous oxidation is the dominant oxidation mechanism. In the case of homogeneous oxidation, achieving Hg oxidation rates above 90% requires more available bromine. As the Br/Hg ratio continues to increase, the Hg oxidation ratio at the SCR inlet increases. In the case of SCR bypassed, the Hg oxidation ratio at the economizer exit nears unity once the Br/Hg ratio reaches 3,000. Hg oxidation continues to occur downstream of the SCR. This continued oxidation should be considered during the determination of the optimal Br/Hg ratio for use in the absence of an SCR. Table 4.5 lists four Hg oxidation ratios at the wet FGD inlet when the SCR was bypassed. At the lowest Br/Hg ratio of 652, the Hg oxidation ratio did not reach 0.90. The table lists three wet FGD inlet Hg oxidation ratios >0.9 when the SCR was bypassed. 121 Table 4.5 Summary of Hg Oxidation Ratios as a Function of Br/Hg Ratio Hg in Coal (wt ppm) Br Concentration (wt ppm) Br/Hg Ratio (lb/lb) SCR Inlet Hg Oxidation Ratio Coxidized/CTotal Wet FGD Inlet Hg Oxidation Ratio Coxidized/CTotal SCR in Service 0.059 3 51 0.27 0.86 Yes 0.091 7 77 0.18 0.92 Yes 0.058 6 103 0.07 Not measured Yes 0.105 25 238 Not measured 0.98 Yes 0.057 18 316 0.41 0.89 Yes 0.070 25 357 Not measured 0.97 Yes 0.085 33 388 0.47 0.94 Yes 0.054 25 463 Not measured 0.97 Yes 0.045 25 556 Not measured 0.83 Yes 0.046 30 652 Not measured 0.70 No 0.057 50 877 Not measured 0.99 Yes 0.080 84 1,050 0.57 0.96 Yes 0.045 50 1,111 Not measured 0.96 Yes 0.060 71 1,183 0.55 0.91 No 0.056 165 2,946 0.98 0.93 No 0.107 328 3,065 0.96 0.95 No Adapted from Tables 6 and B-8 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2007 p. 2-9 and B-7. Copyright 2007 by EPRI. Reprinted with permission. Adapted from Tables 7 and 33 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. 2-8 and 3-51. Copyright 2009 by EPRI. Reprinted with permission. Adapted from Tables 6 and B-13 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. 2-7 and B-14. Copyright 2009 by EPRI. Reprinted with permission. 122 The data suggest that, with a Br/Hg ratio of 1,183, oxidized Hg fractions above 0.9 at the wet FGD inlet are plausible. The figure also shows that without an SCR at a Br/Hg ratio (lb/lb) of 1,100 that at the wet FGD inlet the Hg oxidation ratio is above 0.9. Hg continues to oxidize downstream of the SCR and reaches the desired 0.9 oxidized Hg fraction goal. One could recommend a Br/Hg ratio (lb/lb) of only 1,100 or greater to attain full oxidation but would be doing so with some risk. Without a more fundamental technical understanding of this behavior it is likely too risky to make such a recommendation. Future scientific work to better understand this phenomenon could result in the reduction of bromine injected to achieve the same level of oxidized Hg. In an effort to reduce risk, taking a more conservative viewpoint would involve requiring an oxidized Hg fraction above 0.90 at the SCR inlet. Using this constraint and the available data resulted in a suggested minimum Br/Hg ratio of 2,946. When an SCR is present, Hg oxidation behavior changes. In this case, heterogeneous oxidation is the dominant mechanism of Hg oxidation. The lowest Br/Hg ratio in Table 4.5, with a value of 51, resulted in an Hg oxidation ratio of 0.86 at the wet FGD inlet, which is slightly lower than the 0.9 goal. Once the Br/Hg ratio exceeded 100, the corresponding Hg oxidation ratios at the wet FGD inlet were above 0.9. The data support the assertion by Vosteen et al. (2003) that high rates of Hg oxidation necessitate a Br/Hg ratio of 100:1. Based on the data in Table 4.5, a conservative Br/Hg ratio > 250 is recommended for a unit firing PRB coal with a well designed and maintained SCR. For a unit burning PRB coal, guidance is provided in Table 4.6 for achieving a Hg oxidation ratio > 0.9 at the inlet of a wet FGD. 123 Table 4.6 Guidance on Br/Hg Ratio to Achieve Oxidation Ratios Greater Than 0.9 While Firing PRB Coal as a Function of SCR Status Equipment Configuration Recommended Br/Hg Ratio With SCR >250 No SCR available / SCR bypassed >3,000 Figure 4.6 graphically represents the Hg oxidation ratio and its relationship to Br/Hg ratio. The figure groups the data by SCR operating condition, with a transparent yellow box surrounding the Br/Hg ratios when the SCR was bypassed (i.e., not in service). Figure 4.6 Hg oxidation ratio versus Br/Hg ratio (lb/lb) with and without the SCR in service. Figure was developed with the use of data from Phases I, IIA, and IIB. 124 When the Br/Hg ratio reaches 3,000 the Hg oxidation ratios converge at the SCR inlet and the wet FGD inlet; that is, the SCR bypassed Hg oxidation ratio equals the SCR Hg oxidation ratio at the wet FGD inlet. 4.3.2 Heterogeneous versus Homogeneous Oxidation The SCR plays a vital role in the oxidation of Hg with the use of CaBr2 as a coal chemical amendment to raise the halogen content of the flue gas. The earlier analysis of baseline Hg oxidation behavior demonstrated that the Miller Unit 4 SCR is well designed for promoting the oxidation of Hg. Figure 4.7 illustrates the oxidation behavior with various Br concentrations (wt ppm on the dry coal) when the SCR was in service and with NH3 injection for the control of NOx. The figure shows that the Hg oxidation ratio increases at the SCR inlet as the Br concentration in the coal increases. Situated just downstream of the economizer exit, the SCR inlet represents the location at which homogeneous oxidation is the main oxidation pathway. In laboratory studies, Otten et al. (2011) achieved Hg oxidation ratios greater than 0.8 solely with homogeneous oxidation with HBr. Theoretically, a Br concentration of 328 wt ppm in the dry coal yields 12 ppmv (dry at 3% O2) of HBr on Miller Unit 4. Silcox et al. (2008) and Otten et al. (2011) reported oxidation ratios below 0.80 with 12 ppmv HBr concentration. Figure 4.6 shows that a Br concentration of 328 wt ppm on the dry coal, the Hg oxidation ratio at the wet FGD inlet was near one. Since Silcox et al. (2008) and Otten et al. (2011) both excluded particles from their experiments; the difference from the laboratory and Unit 4 results may be attributed to their exclusion of native heterogeneous oxidation. Cao et al. (2008) 125 in experiments that included heterogeneous oxidation via SCR catalyst, reported that 3 ppmv HBr produced 0.8 fraction of oxidized Hg with PRB simulated flue gas. Figure 4.7 Hg oxidation ratio versus Br concentration (wt ppm on the dry coal) with SCR in service with NH3 injection to control NOx. At low Br concentrations in the dry coal (2 to17 wt ppm), the Hg oxidation ratio at the SCR outlet exceeds 0.90. This demonstrates that heterogeneous Hg oxidation efficiency, fraction of Hg oxidized by available halogen, surpasses homogeneous oxidation efficiency. Similar fractions of oxidized Hg can be achieved via both reaction pathways, but high Hg oxidation fractions are achievable via CaBr2 addition through heterogeneous oxidation with low concentrations of bromine. 126 At Br concentrations greater than 150 wt ppm in the dry coal, the Hg oxidation ratio appears to decrease across the SCR. This relationship may imply a Br concentration exists to support the reduction of Hg within the SCR. Figure 4.7 shows that, at a Br concentration of 328 wt ppm in the dry coal, the Hg oxidation ratio decreases from 0.96 at the SCR inlet to 0.79 at the SCR outlet. In this case, the Hg oxidation ratio increases to 0.95 due to further Hg oxidation downstream of the SCR. This potential phenomenon has not been discussed in the literature and may warrant further investigation. Similar behavior was observed at a Br concentration of 165 wt ppm on the dry coal but to a lower extent. 4.3.2.1 Role of NH3 in SCR Oxidation Behavior Dranga et al. (2012) studied the impact of NH3 on Hg oxidation in an SCR. Dranga et al. (2012) concluded that NH3 preferentially adsorbs to the active vanadia sites and precludes the adsorption of bromine and Hg on those same sites for R13, R14, and R15 to occur. Figure 4.8 shows a plot of wet FGD inlet Hg oxidation ratio versus Br concentration in the dry coal when the SCR was in service with and without NH3. The solid black trendline represents a power series data fit to the Hg oxidation ratio values in the absence of NH3. The dotted black trendline represents a power series data fit to the Hg oxidation ratio values in the presence of NH3. There is a small difference in the magnitude of Hg oxidation ratios at a given Br concentration in the dry coal; although the similar slopes suggest an identical response in Hg oxidation for a corresponding increase in Br concentration. Additionally, the 127 trendlines show that for the SCR with NH3 case, to achieve the same fraction of oxidation for a given Hg oxidation ratio, a higher Br concentration is required. Figure 4.8 Hg oxidation ratio versus Br concentration (wt ppm in the dry coal) at the wet FGD inlet as a function of SCR operational status. For example, Figure 4.8 includes a solid blue line representing an Hg oxidation ratio of 0.94. The figure shows that for both cases, SCR with and without NH3, both achieve this fraction of Hg oxidation, but they do so at different Br concentration (wt ppm on the dry coal). Figure 4.8 illustrates the adverse effect of NH3 on Hg oxidation can be countered by increasing the bromine concentration. Using the power fit equations in Figure 4.8, the Br concentration to achieve a Hg oxidation ratio of 0.94 (i.e., 128 intersecting the blue line) was 50 wt ppm on the dry coal for the SCR with NH3 case and 16 wt ppm on the dry coal for the SCR without NH3. The results may also suggest that, to promote Hg oxidation, a higher relative catalytic (K/Ko) NOx activity is required. The higher relative catalytic (K/Ko) NOx activity will allow a faster consumption of NH3. Once enough NH3 has been consumed in reactions R16, R17, R18 and R19, the remaining active vanadia sites in the SCR are available for Hg oxidation reactions. Figure 4.9 provides a set of Hg oxidation scenarios in the case of various relative NOx catalytic activity (K/K0) values (1.0, 0.7, and 0.5). Figure 4.9, although not based on data, provides a possible explanation of the role NH3 plays in Hg oxidation with an SCR. Using the figure to describe possible behavior results in the following scenario: when K/Ko equals 1.0, NH3 is consumed fairly quickly within the SCR; as a result, over half (0.5) of the catalyst is available to support Hg oxidation reactions, represented by Point A in the left diagram of Figure 4.9. Point A represents the largest extent of Hg oxidation. The Hg oxidation does not begin to occur in earnest until the NH3 concentration drops below some level. The SCR depth remaining to support Hg oxidation is represented by a depth scale at the extreme right of the figure. When K/Ko is reduced to 0.7, the outlet NH3 concentration remains the same, represented by Point a in the center diagram of Figure 4.9; however, only 30% of the reactor remains to support Hg oxidation reactions. Hg is oxidized but to a lower extent, represented by Point B in the middle diagram of Figure 4.9. In the middle diagram of Figure 4.9, Point B is close to Point A; therefore, little change in Hg oxidation is observed. When K/Ko is reduced to 0.5, outlet NH3 concentration remains the same, 129 represented again by Point a in the right diagram of Figure 4.9; however now only 10% of the reactor remains to support Hg oxidation. Outlet NH3 concentrations remain the same, represented by Point a; however, Hg is oxidized but to a much lower extent, represented by Point C in the right diagram of Figure 4.9. Figure 4.9 Illustration of NH3 consumption and its effect on Hg oxidation behavior in an SCR. Because relative NOx catalyst activity in the Miller Unit 4 SCR remains relatively high (K/K0=0.7), a slight difference in Hg oxidation ratio with and without NH3 present seems plausible. More research is needed regarding the relationship among NOx relative catalyst activities (K/Ko) and Hg oxidation. The results of such research would aid in developing catalyst management plans that account for optimizing both NOx removal and Hg oxidation. 130 4.3.3 Summary Hypothesis 2 was proven to be correct. CaBr2 addition promoted Hg oxidation levels in excess of 90%. In addition to proving the hypothesis, the analysis of the data supports the following generalizations: • The presence of an SCR increased the efficiency of CaBr2. With a well designed and operating SCR in service, a ten fold-reduction in CaBr2 additive was observed to achieve bypassed SCR Hg oxidation levels. • A Br/Hg ratio above 3,000:1 (lb/lb) is needed when an SCR is bypassed/not available, but that Br/Hg ratio can be reduced to 250:1 (lb/lb) when a welldesigned and maintained SCR is available. • The relative NOx catalytic activity (K/K0) plays an active role in the level of optimization that can be achieved with an SCR present. As the relative NOx catalytic activity ratio, K/Ko, decreases, more CaBr2 will be needed to compensate for less active catalyst. • CaBr2 addition systems should be designed to compensate for catalyst degradation and should accommodate the ability to inject based on a Br/Hg ratio of 250:1 (lb/lb) under optimum conditions and on a Br/Hg ratio of 3,000:1 (lb/lb) when the SCR is bypassed or when the SCR catalyst is seriously degraded. 131 4.4 Hypothesis 3: CaBr2 Addition Can Result in Hg Capture Efficiencies Exceeding 90% When a Wet FGD System Is Present 4.4.1 Wet FGD Hg Removal Efficiency Testing this hypothesis involved analyzing data from Phases IIA and IIB. Data from Phase I were excluded because a wet FGD was not installed during that test program, and Phase III data were excluded because that phase did not include measuring the Hg concentration entering the wet FGD. Figure 4.10 graphically represents observed Hg removal across the 2 MW pilot wet FGD versus the Br concentration (wt ppm in the dry coal) and was created with the use of data provided in Table 4.7. The data are plotted in three separate series on the basis of the SCR operating condition: SCR in service with NH3 injection, SCR in service without NH3 injection, and SCR bypassed. Figure 4.10 includes a solid line that represents 90% removal across the wet FGD. Data obtained during baseline and CaBr2 addition are shown for relative comparison. For the basis of testing the hypothesis, any native removal of Hg upstream of the wet FGD is ignored. Without CaBr2 addition to the coal (i.e., baseline conditions), in all cases the Hg removal efficiencies were less than 90%. The baseline removals of Hg are sensitive to SCR condition (in service or bypassed). Based on the analysis of the baseline Hg oxidation behavior as discussed earlier, these lower rates of Hg removal were expected. During baseline conditions, the highest Hg removal efficiency of (85% removal, occurred with SCR in service but without NH3. The absence of NH3 provides the largest volume of available catalyst surface to aid Hg oxidation reactions. During the other two conditions, SCR in service with NH3 and SCR bypassed, the baseline Hg removals were 132 below 60%. The baseline tests demonstrated the inability of the system to reach Hg emission removal rates above 90%. Figure 4.10 Total Hg removal across a 2 MW pilot-scale wet FGD as a function of Br concentration (wt ppm on the dry coal) and SCR operational condition. The Hg removal observed with the SCR bypassed related strongly to the Br concentration (wt ppm in the dry coal). The SCR bypassed condition presents a difficult scenario for Hg oxidation because all of the bromine enhancement occurs in the gas (i.e., homogeneous oxidation). With the SCR bypassed, Hg removal progresses from 40% at a Br concentration of 30 wt ppm on the dry coal to 86% at 90 wt ppm Br concentration on the dry coal to a maximum value of 98% at 234 wt ppm Br concentration on the dry coal. 133 Table 4.7 Hg Oxidation and Removal Information Collected During Phases IIA and IIB. Phase IIB IIB IIB IIB IIB IIB IIB IIB IIB IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA IIA SCR Equipment Setup Br Concentration (wt ppm) A A A A A A A A A B B B B B B B B B B B B B B B B B C C C C C C C C 0 0 0 17 17 17 25 25 25 0 0 0 2 25 25 25 25 25 25 25 28 50 50 50 50 54 0 0 0 0 0 30 90 234 Hg Oxidation Ratio at wet FGD Inlet (Coxidized /Ctotal) 0.30 0.42 0.46 0.92 0.97 0.95 0.98 0.97 0.98 0.81 0.66 0.85 0.95 0.87 0.83 0.92 0.92 0.97 0.97 0.97 0.99 0.98 0.99 0.99 0.96 0.96 0.46 0.34 0.55 0.51 0.38 0.70 0.88 0.97 Wet FGD Hg Removal (CinletCoutlet)/Cinlet) Reemission Parameter Hg SCEM Averaging Time (h) 0.30 0.47 0.41 0.77 0.91 0.91 0.92 0.86 0.94 0.79 0.70 0.85 0.88 0.90 0.93 0.94 0.93 0.92 0.92 0.93 0.97 0.93 0.94 0.95 No value 0.94 0.54 0.27 0.50 0.23 0.19 0.40 0.86 0.98 1.00 1.11 0.88 0.84 0.94 0.95 0.94 0.89 0.97 0.97 1.06 0.99 0.92 1.04 1.12 1.03 1.01 0.95 0.94 0.97 0.98 0.95 0.95 0.96 No value 0.98 1.16 0.81 0.92 0.45 0.50 0.57 0.98 1.01 9.00 9.00 9.00 11.75 24.00 12.00 24.00 24.00 24.00 6.00 5.00 6.00 1.50 12.00 24.00 24.00 24.00 24.00 24.00 12.00 3.00 9.00 24.00 24.00 12.00 3.00 8.50 10.00 10.00 7.25 7.00 3.00 4.30 5.00 A = SCR with NH3; B = SCR with no NH3; C = No SCR. SCEM – Hg Semicontinous Emission Monitor Reemission parameter is a measure of the likelihood that an Hg reemission event occurred during a particular test; a value below 1 indicates that a reemission event may have occurred. 134 These results demonstrate that, without the presence of an SCR, Hg removal efficiencies can exceed 90%. With the SCR in service and without NH3 injection, the Hg removal efficiency surpassed 90% once the Br concentration reached 25 wt ppm on the dry coal. Additionally, a Br concentration of 50 wt ppm on the dry coal provided removal efficiencies greater than 90%. The Hg removal results described here, in the absence of NH3 in the SCR, support the assertions of Dragna et al. (2012) that NH3 impacts Hg oxidation. However, because of regulatory constraints, Unit 4 will operate a vast majority of the time with the SCR in service and with NH3 injection for the control of NOx emissions. This fact makes analysis of the SCR with NH3 injection configuration the most applicable from the standpoint of Hg removal performance. A review of Table 4.7 and Figure 4.10 reveals only six discrete data points related to the configuration of SCR with NH3 injection. The data do show that, for this equipment configuration, the observed Hg removed exceeded 90% once the Br concentration reached 17 wt ppm on the dry coal. Of the six data points available for this configuration, four exceeded 90% removal, and one was near 90%. The data provided during Phases IIA and IIB testing support the conclusion that CaBr2 addition to the coal can support Hg removal efficiencies greater than 90%. 4.4.2 Evaluation of Hg Reemission Hg reemission occurs when elemental Hg emissions leaving the wet FGD exceed wet FGD inlet elemental Hg emissions. This condition can only occur if Hg present (i.e., dissolved in solution) or adsorbed to a solid particle is reduced from the soluble form (oxidized Hg) to the insoluble form (elemental Hg). 135 To quickly evaluate whether a reemission had occurred during the Phases IIA and IIB research programs, a numerical value, called the reemission parameter (RP) was calculated. Equation 2 is used to calculate the RP. RP = wet FGD Hg Removal/Hg Oxidation Ratio (E2) RP < 1 indicates possible Hg reemission from the wet FGD; that is, the amount of Hg removal observed is less than the amount of oxidized Hg available for removal. RP = 1 signifies that Hg reemission has not been observed; in other words, the Hg removal observed equals the amount of available oxidized Hg. Last, RP > 1 indicates that observed Hg removal exceeds the amount of available oxidized Hg, indicating some removal of elemental Hg across the wet FGD. Table 4.7 contains summary information on the Br concentration (wt ppm on the dry coal), Hg oxidation ratio at the wet FGD inlet, observed Hg removal across the wet FGD, and calculated value of the RP. In addition to this performance information, Table 4.7 contains information about the test period duration, which defines the averaging period for the Hg measurement, and about the SCR operating condition. A majority of the RP values are close to 1, indicating that reemission events did not happen frequently during the test program. A few data points have RP values much less than 1. RP values less than 0.9 may indicate a strong likelihood that a reemission event occurred. A closer examination of Table 4.6 reveals that the lowest RP values occurred when the SCR was out of service. Additionally, the RP values were lowest when the halogen concentration was lowest (e.g., without the addition of CaBr2 to the 136 coal or with a Br concentration of 30 wt ppm on the dry coal). This result may indicate that higher NOx emissions adversely affect the wet FGD chemistry or that a lack of halogen in the wet FGD results in a higher percentage of Hg reemissions. This behavior will be discussed in more detail later in this section. Figure 4.11 graphically represents the data provided in Table 4.7. The figure shows wet FGD Hg removal ratio plotted against the Hg oxidation ratio for a given data point. Ideally, all of the oxidized Hg is captured in the wet FGD; that is, fraction of Hg captured equals the fraction of oxidized Hg. If all oxidized Hg is removed, the respective data point in Figure 4.11 will intersect the 45-degree line. If a data point falls below the line, the Hg removal is below ideal and Hg was reemitted from the wet FGD slurry. If a data point is above the line, removal exceeds the amount of oxidized Hg present. Taking a reasonable measurement error (i.e., +/- 10%) into account, some of the data points might be located a small distance from the ideal condition (i.e., slightly above or below the line). Data points an extended distance away from the 45-degree line warrant close examination to better understand if Hg reemissions are indeed responsible for non-ideal removal behavior. Figure 4.11 also includes a vertical and horizontal dotted lines located at 0.9 that represent 90% Hg oxidation and removal, respectively. A data point located above the horizontal line represents the achievement of 90% Hg removal, and a data point to the right of the vertical line indicates the achievement of 90% or greater Hg oxidation. Data points in the top right corner of Figure 4.11, within the light-green box, show the occurrence of both greater than 90% oxidation and 90% removal. 137 Figure 4.11 Wet FGD Hg removal versus Hg oxidation ratio for differing SCR reactor operational conditions during Phase IIA and Phase IIB. A marker below the 45-degree line represents lower-than-expected Hg removal, and a marker above the 45-degree line represents better-than-expected Hg removal. A marker to the right of the vertical line represents 90% oxidation. A marker above the horizontal line represents 90% removal in the wet FGD. A marker within the green box represents at least 90% Hg oxidation and 90% Hg removal. The three points farthest away from the ideal condition (RP = 0.45, 0.5, and 0.57) occurred during Phase IIA when the SCR was not in service and when the Br concentration was low (i.e., under baseline conditions without CaBr2 addition and when the Br concentration was 30 wt ppm on the dry coal). All three data points represent low levels of Hg oxidation but also represent instances with the lowest Br concentration in the wet FGD sump. The other two lowest RP values (RP = 0.84 and 0.88) occurred during Phase IIB when the SCR was in service with NH3 injection but with low Br concentrations (wt ppm on the dry coal). Because all five potential reemission events 138 occurred during low levels of Br concentration in the system (i.e., in the flue gas and, more important, in the wet FGD sump), bromine in the wet FGD sump may assist the system in lowering the impact of Hg reemission. During Phases IIA and IIB, CaBr2 was spiked into the 2 MW wet FGD sump to replicate higher bromine concentrations in the wet FGD slurry. During Phase IIA, wet FGD slurry bromine concentrations of less then 200 ppm, greater than 1,300 ppm, and greater than 2,500 ppm were investigated; Phase IIB involved investigating wet FGD slurry bromine concentrations of less than 50 ppm and greater than 1,800 ppm. Each of the highlighted potential Hg reemission events occurred when the wet FGD slurry bromine concentrations were lowest (i.e., below 200 ppm during Phase IIA and below 50 ppm during Phase IIB). 4.4.3 Insights Into the Occurrence of Reemission An examination of the operational information collected during Phases IIA and IIB provided insights into Hg reemission events or nonevents occurring during the research program. Figure 4.12, which shows operational parameters associated with wet FGD Hg reemission events, was developed from observations in the literature and from the test data gathered during Phases IIA and IIB. The figure illustrates that Hg reemission is a function of wet FGD slurry characteristics such as suspended solids Hg concentration, liquor Hg concentration, sulfite concentration, combined chlorine and bromine concentration, and oxidation reduction potential (ORP). The combination of Hg concentration in the suspended solids and the slurry liquor represents the Hg available for reemission. The concentrations of chlorine, bromine and sulfites in the slurry are the 139 compounds known to form stable Hg complexes, which have a lower potential for Hg reemissions. The ORP measures the oxidation health of the wet FGD and expresses the likelihood for the scrubber to reduce (i.e., emit or precipitate Hg) or maintain oxidation (i.e., keep Hg in solution). Figure 4.12 is hereafter referred to as the Hg reemission probability diagram. Figure 4.12 is a pentagon with an axis for each parameter that affects the probability that an Hg reemission event will occur. The green circle at the center of the diagram represents operational conditions with a low likelihood of Hg reemission. Each parameter has its own axis and is represented equally (i.e., axis lengths are the same) because it is not currently known which parameter might dominate the occurrence or nonoccurrence of a reemission event. For example, sulfite concentration, measured in millimolar per liter (mM), increases the probability of occurrence of a reemission event as concentration decreases. Omine et al. (2012) reported that, in bench-scale test, no reemission was observed at 9 mM of sulfite, and that reemission events became more prevalent when sulfite concentrations were below 2 mM. Blythe et al. (2008) and Omine et al. (2012) observed that the presence of halogens in the liquid reduced the probability of a reemissions event. Omine et al. (2012) found that 2,000 mg/L (ppm) of chlorine or bromine was effective at reducing Hg reemission events. Omnie et al. (2012) also concluded that, at similar concentrations, bromine was more effective than chlorine at reducing Hg reemission events. 140 Figure 4.12 Wet FGD Hg Reemission Probability Diagram. Diagram demonstrates visually that the probability of reemitting Hg from a wet FGD sump is a function of slurry bromine and chlorine concentration, sulfite concentration, oxidation reduction potential, Hg concentration in solution, and Hg concentration in the total suspended solids. The likelihood of an Hg reemission event significantly decreases if Hg is not dissolved in the wet FGD slurry solution. In that sense, a 0 µg/L concentration of Hg in the slurry solution is the best scenario, that is, as the concentration of Hg in solution increases, so does the potential for an impactful reemission event to occur. Additionally, the concentration of Hg in the suspended solids represents a potential reemission source, 141 although a much less probable one than Hg dissolved in the wet FGD slurry solution constitutes. ORP represents the oxidation health of the scrubber and high values indicate that a wet FGD can keep Hg soluble (i.e., dissolved in solution). High ORP indicates that the wet FGD contains a higher concentration of transition metals (e.g, Mn, Fe, and Cu). Chengli et al. (2010) concluded from bench-scale tests that the presence of transition metals could be a key component in managing reemissions from wet FGDs. Lower ORP is actually more beneficial from a reemission perspective because the Hg is more likely to precipitate. Hg reemission is less likely to occur via a reduction reaction once Hg has precipitated. A reemission parameter qualitative ranking system, shown in Table 4.8, was developed incorporating information from the literature. In the ranking system, good denotes a low likelihood for a reemission to occur, neutral indicates that the parameter had no relative impact on whether a reemission would occur, and a rating of poor indicates that the parameter increased the likelihood for a reemission event to occur. A sulfite concentration of 2 mM or greater was evaluated as good, a value below 2 mM but greater than 1 mM was considered neutral and a sulfite concentration below 1 mM was evaluated as poor. The bench-scale results from Omine et al. (2012) were used to develop this guidance. The guidance of Omine et al. (2012) was used to assign ratings for chlorine and bromine concentration impact on Hg reemission. A combined chlorine and bromine concentration that exceeded 4,000 ppm was evaluated as good, a combined concentration 142 greater than 2,000 but less than 4,000 ppm was evaluated as neutral, and a combined concentration below 2000 ppm was evaluated as poor. Table 4.8 Reemission Parameter Qualitative Ranking System Unit Poor Neutral Good Sulfite concentration mM <1 1<X<2 >2 Combined bromine and chlorine concentration ppm <2000 2000 < X < 4000 >4000 ORP mV >400 400 < X < 200 0 < X < 200 % >2 0.5 < X < 2 <0.5 Wet FGD slurry concentration Chengli et al. (2010b) reported that ORP values less than 0 mV led to Hg reemissions and that Hg reemission did not occur when ORP was greater than 0 mV but less than 135 mV, which was the highest ORP value studied. On the basis of results from full-scale studies, Dombrowski and Richardson (2012) reported that Hg reemissions did not occur at ORP below 250 mV but were prevalent at ORP values greater than 400 mV. For Hg concentration, a relative ranking was used that was based not on any guidance from the literature but on the experience of the researcher. The literature review did not reveal research based on the impact of wet FGD slurry Hg concentration on Hg reemissions. If the Hg concentration in the slurry was less than 0.5% of the total Hg (i.e., Hg concentration in the wet FGD slurry and gypsum), then a ranking of good 143 was given; if the Hg concentration in the slurry was 0.5% to 2% a neutral ranking was given; if the Hg percentage in the slurry exceeded 2% a poor ranking was given. The converse would be true for Hg concentration in the solids: poor would equal <98% of total Hg in the solids, neutral would be given when the Hg concentration was greater than 98% but less than 99.5%, and a good score would be given when the Hg concentration was greater than 99.5%. To better understand the context of Hg reemission observed during Phases IIA and IIB, the researcher developed Table 4.9 to summarize data in terms of Figure 4.13 and to apply the qualitative ranking system in Table 4.8. Table 4.9 provides a summary of appropriate wet FGD conditions that existed on specific testing days during Phases IIA and IIB. Unfortunately, wet FGD chemistry data were not available for some days. As described earlier, the lowest values of RP (RP = 0.45, 0.5, and 0.57) were found on the days when the SCR was bypassed. Unfortunately, during those instances, wet FGD analytical samples were not taken. Table 4.9 provides wet FGD chemistry data for five days collected during Phases IIA and IIB. For example, although sulfite concentrations on October 12, 2008, received a poor rating, all other parameters were evaluated as good. The halogen concentration was high (>4,000 mg/L), the ORP was low (149 mV), and Hg concentration in the wet FGD slurry was low (<0.5%). These other parameters likely compensated for the low sulfite concentration. For the days that data were available, Hg reemission potential was low. Additional test programs are needed to assess the viability of the Hg reemission probability diagram (Figure 4.12) and the qualitative ranking system (Table 4.8). 144 Table 4.9 Summary Operational Information Describing the Potential for Hg Reemission Events to Occur Within the 2 MW Pilot Wet FGD During Phases IIA and IIB Testing Date Calculated Reemission Potential Sulfite (mM) Total Halogen (ppm) Oxidation Reduction Potential (mV) Slurry Hg Concentration (wt%) 2/22/2008 0.81 1.45 Neutral 3,049 Neutral 109 Good 0.1 Good 2/23/2008 0.92 1.6 Neutral 2,404 Neutral 117 Good 3/12/2008 0.97 1.54 Neutral 5,627 Good 159 Good 0.1 Good 0.1 Good 10/9/2008 1.11 1.71 Neutral 851 Poor 149 Good 0.2 Good 10/12/2008 0.94 0.975 Poor 4,499 Good 146 Good 0.1 Good Criteria for parameter ranking can be found in Table 4.8. 145 Although the diagram is based on the fundamentals derived from the literature and on researcher experience, the data collected during Phases IIA and IIB provides insufficient outliers to test the applicability of the concept. The conclusion drawn from the analysis of the data is reemission did not occur excessively during the research period and the results from the qualitative ranking system agree with observed behavior. 4.4.4 An Evaluation of Br/Hg Ratio In the previous section, ideal Br/Hg ratios were suggested for attaining high Hg oxidation ratios. Table 4.10 catalogs the effect of Br/Hg ratio on wet FGD Hg removal. For only a limited number of data points was all of the required information (Br/Hg ratio and wet FGD removal) available. Table 4.10 Wet FGD Hg Removal Ratio and Reemission Parameter as a Function of Br/Hg Ratio and SCR Condition Phase SCR in Service NH3 in Service Br Concentration (wt ppm) Br/Hg Ratio Wet FGD Hg Removal Reemission Parameter IIA No No 30 652 0.40 0.87 IIA Yes No 6 103 Not available Not available IIB Yes Yes 25 238 0.86 0.89 IIB Yes Yes 25 357 0.94 0.97 IIA Yes No 25 463 0.92 0.95 IIA Yes No 25 556 0.93 1.12 IIA Yes Yes No No 50 50 877 1,111 0.94 Not available 0.95 Not available IIA 146 Once the Br/Hg ratio was above 250, wet FGD Hg removal exceeded 90% with the SCR in service. With the SCR bypassed and with the Br/Hg ratio below 3,000, wet FGD Hg removal was less than 90%; however limited data were available to fully evaluate this configuration. These findings validate for a unit burning PRB coal, a Br/Hg recommendation for achieving 90% Hg oxidation for SCR applications: Br/Hg > 250 and suggest that for non-SCR applications: Br/Hg > 3,000 is an appropriate recommendation. Due to unavailability of data, results at higher Br/Hg ratios on Hg reemission were unavailable and therefore not included in Table 4.10. 4.4.5 Summary The hypothesis that CaBr2 injection can result in Hg capture efficiencies exceeding 90% with a wet FGD present held. CaBr2 addition successfully oxidized Hg, most likely in the form of HgBr2, which is readily soluble in water (Cleaver et al., 1985). The oxidized Hg was removed from the treated flue gas with high efficiency. In addition to proving the validity of the hypothesis, the analyses led to these general conclusions: • Combined with a well functioning SCR, a Br/Hg ratio > 250 will result in wet FGD Hg removal efficiencies exceeding 90% if Hg is not reemitted from the wet FGD sump. For a non-SCR application, a Br/Hg ratio > 3,000 is recommended for similar Hg removal efficiencies. • Hg reemissions are a function of many wet FGD slurry parameters such as sulfite concentration, chlorine and bromine concentration, liquid and solid Hg concentration, and ORP. 147 • Observed Hg reemission events when the wet FGD slurry bromine concentrations were lowest, that is less than 200 ppm during Phase IIA and less than 50 ppm during Phase IIB. 4.5 Hypothesis 4: The Difference in Average Hg Emissions Using CaBr2 Addition, When Compared to Not Employing CaBr2 Addition is Statistically Significant 4.5.1 Analysis of Phase III Hg Emissions Data from Phase III, which involved 83 days of continuous addition of CaBr2 to evaluate long-term performance, were used to test the hypothesis. Figure 4.13 depicts a chronological plot of Unit 3 and Unit 4 hourly average Hg emissions (µg/m3) from September 1, 2010, to January 30, 2011. This period includes the CaBr2 addition testing conducted on Unit 4 from October 1, to December 19, 2010. As Figure 4.13 shows, the Hg emissions from Unit 3 differ markedly from those of Unit 4 during the CaBr2 addition period, whereas the Hg emissions from the two units are similar before CaBr2 addition began and after CaBr2 addition ceased. A break in Hg emission values from December 20 to December 31 resulted from data unavailability. The figure also reveals that the Hg emissions from Unit 3 trended slightly downward during the CaBr2 addition period, possibly because of unit operations (e.g., load and SCR operational parameters) or changes in PRB coal characteristics. If the downward trend in Hg emissions from Unit 3 resulted from a change in coal characteristics, this merits investigating because Unit 4 also burned the same coal during this period. Figure 4.13 indicates that Hg emissions varied widely on both units but that the magnitude of the variability was more pronounced on Unit 3. Br/Hg ratios were not held 148 constant during the test. The Br/Hg variability results both from changes in coal Hg content and for variations in Br concentration (wt ppm on the dry coal) which varied by a maximum factor of 2 and 25, respectively. (See Appendix B for coal data.) The extent of coal Hg concentration variability Hg remains unknown because of the lack of information. During Phase III, only 11 discrete coal Hg content measurements were made. Figure 4.13 Hourly average Hg emissions concentration (µg/m3) from Miller Unit 3 and Unit 4 from September 1, 2010, through January 30, 2011, which includes the bromine addition test period from October 1 through December 19. Hg emissions data were not available from December 20 through December 31. A = calcium bromide addition begins. B = Unit 4 outage. No bromide was injected during start-up. C = Missing data from dataset. 149 The known minimum Br/Hg ratio (lb/lb) of 250 occurred on December 16, 2010 when the Br concentration was 8 wt ppm on the dry coal and when the coal Hg content was 0.032 ppm. The maximum known Br/Hg ratio of 1,666 occurred on October 7, 2010 when the Br concentration was 50 wt ppm on the dry coal and when the coal Hg content was 0.03 ppm. During the test, the CaBr2 liquid flow rate was maintained at a constant rate, even during periods of low load; that is the CaBr2 addition rate was held constant while the coal flow changed. The constant addition rate of CaBr2 while load was allowed to fluctuate caused Br concentration variability. The results of testing in Phases IIA and IIB showed that Br/Hg ratios in excess of 250 do not result in higher fractions of Hg oxidation and that Br/Hg ratios below 3,000 do not adversely affect Hg oxidation at the wet FGD inlet. During Phase III, the varying Br/Hg ratios observed were between 250 and 3,000; therefore, Hg oxidation was optimized. Figure 4.14 focuses on the Unit 4 average hourly Hg emissions, and includes data regarding load (MW) and Br concentration (wt ppm on the dry coal), which are plotted chronologically. During the Phase III program, Unit 4 was operated in normal dispatch mode; in other words, the load was allowed to vary as needed to meet electricity demand. During the addition of CaBr2, Hg emissions were low, with an average Hg emission concentration of 0.26 µg/m3 and with a standard deviation of 0.15 µg/m3. As expected, the Hg emissions were not adversely affected by Br concentration variability. Additionally, changes in unit operating load did not appear to affect Hg emissions. As Figure 4.14 shows, when CaBr2 addition began, a corresponding reduction in Hg emissions occurred immediately. The hourly average Hg emission concentrations before and after the CaBr2 addition were much higher. Once the CaBr2 addition ceased, 150 the Hg emissions returned to approximately the same magnitude as those levels seen before CaBr2 addition commenced. A more detailed discussion regarding load variability and its effect on hourly average Hg emissions behavior is contained in 4.5.3. Figure 4.14 Hourly average Hg emissions concentration (µg/m3); Br concentration (wt ppm on the dry coal); and load (MW) from Miller Unit 4 from September 1, 2010 through January 30, 2011, which includes the CaBr2 addition test period from October 1 through December 19. Hg emissions data were not available from December 20 through December 31. Figure 4.15 provides a closer viewpoint of Unit 4 average hourly Hg emissions and the effect of Br concentration. The majority of hourly average Hg emissions fall below 0.5 µg/m3, and a small number of hourly averages exceed 1 µg/m3. The variability 151 in Hg emissions does not appear tied to Br concentration since the variability in the Hg emissions continued during a November period when the Br concentration was more consistent. 4.0 Hg Emissions Br Concentration 60 3.5 Hg Emissions (ug/m3) 3.0 40 2.5 2.0 30 1.5 20 1.0 Br Concentration (wt ppm on the dry coal) 50 10 0.5 0.0 0 9/28 10/12 10/26 11/9 11/23 12/7 Date Figure 4.15 Hourly average Hg emissions concentration (µg/m3) and Br concentration (wt ppm on the dry coal) from Miller Unit 4 from October 1 through December 19, 2010. Includes a Unit 4 outage from December 6 through 9, 2010. CaBr2 was not added during start-up after the outage. CaBr2 was returned to service at a lower addition rate after the unit reached full load. The variability in Hg emissions could indicate a measurement artifact, operational issues, or normal variability in emissions. Although not a major concern because of the smaller number of instances, the hourly average Hg emissions above 1 µg/m3 are noteworthy 152 because, despite the fact that compliance is based on a 30-day rolling average, the MATS rule requires that Hg emissions are below 1.2 lb/TBtu (approximately 1.15 µg/m3 at Plant Miller Unit 4). On Saturday, December 5, 2010, Unit 4 was taken offline for an unplanned outage of approximately 40 h. CaBr2 was not added during the start-up of the unit to observe uncontrolled Hg emissions. After start-up operations ceased, the Br concentration was reduced by half each day until the end of the test program. Figure 4.16 contains a plot of the hourly average Hg emissions shortly before and after the Unit 4 outage in December. Figure 4.16 Hourly average Hg emissions concentration (µg/m3) and Br concentration (wt ppm on the dry coal) on Miller Unit 4 from December 4 through December 19, 2010, which includes short boiler outage. 153 The figure reveals that hourly average Hg emissions during the start-up of Unit 4 exceeded those found before the outage (1.75 µg/m3 and 0.25 µg/m3, respectively). At a Br concentration of 10 wt ppm on the dry coal, the hourly average Hg emissions remained at a level comparable to those seen before the outage. The Br concentration was reduced further, and a corresponding increase in hourly average Hg emissions variability was observed. 4.5.2 Impact of Coal Characteristics The quality of coal delivered to a site varies with time, even in situations such as that found at Plant Miller, which exclusively fires PRB coal from the same region. The coal can vary in a number of constituents that could have affected the results of this research program. Such coal constituents include Hg content, halogen content, and, sulfur content. An analysis of baseline Hg emissions revealed that the amount of oxidized Hg present, could in fact, be a function of these factors. Statistical and graphical methods were used to determine the effect of coal characteristics on Hg emissions. The analysis of coal variability of Hg emissions included a comparison of Unit 3 hourly average Hg emissions during the CaBr2 addition period, with Unit 3 hourly average Hg emissions observed the month before and the month after the CaBr2 addition period. This examination of the Unit 3 hourly average emissions provided insights into the ways in which coal characteristics might have changed during the CaBr2 addition period. Also, an analysis of Unit 4 hourly average Hg emissions when CaBr2 was not added highlighted the impact of specific coal changes on Unit 4. Differences found in Hg emissions from Unit 3 and Unit 4 would highlight the impacts of coal variability. 154 4.5.2.1 Unit 3 Coal Impact Analysis The impact of coal characteristics on Hg emissions was evaluated by a t-test of Unit 3 Hg emissions data, which were comprised of CaBr2 addition condition (i.e., on/off) as an independent variable and Unit 3 hourly average Hg emissions as the dependent variable. As noted earlier, CaBr2 was not added to Unit 3. The use of CaBr2 addition condition (i.e., on/off) as the independent variable effectively segregates the Unit 3 hourly average Hg emissions data into the two periods of interest. The Unit 3 data were not normally distributed (see Appendix C for normality analysis). The lack of normality was not sufficiently severe to affect t-test applicability. Table 4.11 provides summary information regarding the Unit 3 hourly average Hg emissions dataset. Table 4.11 Unit 3 Hourly Average Hg Emissions Descriptive Statistics During CaBr2 Addition Period on Unit 4 and Not During CaBr2 Addition Period on Unit 4 Unit 4: CaBr2 Off September 1-30 / January 1-30 Unit 4: CaBr2 On October 1-December 19 1,493 1,735 Mean (µg/m ) 3.14 2.91 Standard deviation (µg/m3) 1.14 1.00 Statistic No. of Samples 3 An independent t-test was done to determine the significance of mean differences during the two periods. Cohen d was computed to determine the magnitude of effect. Additionally, the partial eta squared was computed as an additional means measuring the magnitude of effect. 155 The equality of the means of the hourly average Hg emissions (µbromine,test = µbromine,no) was assumed to test the null hypothesis. The null hypothesis was rejected, t(3226) = 6.116, p < .001, with Unit 3 hourly average Hg emissions greater during periods when CaBr2 was not being added to Unit 4 than during the period when CaBr2 was being added to Unit 4. In other words, the Unit 3 Hg emissions during September and January were greater than the Unit 3 Hg emission from October through December. The Cohen’s d calculated value was 0.215, which translates to a low degree of effect (Weinberg and Abromowitz, 2008). The partial eta squared was 0.011, which translates to a low degree of effect (Barnette, 2006). The results of the t-test can be found in the Appendix D. The results show that Hg emissions on Unit 3 differ during the two periods (CaBr2 on and CaBr2 off on Unit 4). The magnitude of the effect was small. There was an unexplained change during these two periods that resulted in a difference in hourly average emissions. 4.5.2.2 Unit 4 Coal Impact Analysis To evaluate the impact of coal characteristics on Unit 4 hourly average Hg emissions, an independent t-test was completed by using data from Unit 4 during September 2010 and January 2011, when CaBr2 was not being injected. The Unit 4 average hourly Hg emissions were the dependent variable with the time period of the measurement as the independent variable. The Unit 4 data were not normal. (See Appendix C for normality analysis.) The lack of normality was not sufficiently severe to 156 affect t-test applicability. Table 4.12 provides a summary of the descriptive statistics for the data. The equality of the two average hourly Hg emission means (µ4, September = µ4, January) was tested as the null hypothesis. The null hypothesis was rejected, t(1395) = 7.835, p < .001. The difference in Unit 4 hourly average Hg emission means during September 2010 and January 2011 was statistically significant. Cohen’s d calculated value was 0.41, which translates to a low degree of effect (Weinberg and Abramowitz, 2008). The partial eta squared was determined as 0.042, also a low degree of effect (Barnette, 2006). The results of the t-test can be found in the Appendix D. Table 4.12 Unit 4 Hourly Average Emissions Descriptive Statistics During September 2010 and January 2011 Unit 4: CaBr2 Off September 1-30 Unit 4: CaBr2 Off January 1-30 Sample size 690 707 Mean 2.54 2.18 Standard deviation 1.04 0.67 Statistic 4.5.2.3 Coal Impact Analysis Summary The analyses from both Unit 3 and Unit 4 showed that coal characteristics did change during Phase III testing. During January 2011, the lowest mean hourly average Hg emission mean was 2.18 µg/m3 that occurred on Unit 4 in January 2011. Even at this low concentration, Unit 4 was out of compliance with the MATS rule Hg limit. Because 157 the lowest Hg emission average exceeded the MATS rule Hg limit, the effect of coal characteristics was determined to be minor. 4.5.3 Impact of Load Unit load represents a real-time measure of a number of factors that affect Hg oxidation such as, mass flow of coal, fly ash, unburned carbon, halogens, and Hg; operating temperatures of the SCR, air heater and cold-side ESP; and residence times in the SCR, air preheater, cold-side ESP and wet FGD. For example, as load decreases, SCR temperature decreases, and flue gas residence times in environmental control equipment increase both of which are positive influences of Hg oxidation. In another example, as coal mass flow decreases the wet FGD concentration of transition metals and halogens decreases and those factors can adversely impact oxidized Hg retention. Understanding these individual factors are important, for this analysis, any significant differences in hourly average Hg emissions are attributed to changes in unit load. An ability to exclude or properly qualify the influence of other factors on Hg emissions ensures that differences in Hg emissions can be positively attributed to CaBr2 addition. A focused evaluation of CaBr2 addition performance on Hg emissions supports the decision to combine the impact of other factors on Hg emissions into a single independent variable (i.e., load). For the analysis, unit load data were grouped into three separate categories: Category 1, Load > 600 MW; Category 2, 500 MW < Load < 600 MW; and Category 3, Load < 500 MW. Once data grouping was complete, graphical and descriptive statistical 158 methods were used to determine whether differences in hourly average Hg emissions were observed. Three test cases were analyzed: • Case 1: CaBr2 Off − Unit 3, September 1, 2010, through January 30, 2011. • Case 2: CaBr2 Off − Unit 4, September 1-30, 2010, and January 1-30, 2011. • Case 3: CaBr2 On − Unit 4, October 1-December 15, 2010. 4.5.3.1 Case 1: Unit 3 Load Analysis The Unit 3 hourly average Hg emissions from September 1 to January 30 were coded with a load category. Table 4.13 summarizes the Unit 3 Hg emissions data sorted by load category and lists number of samples, mean Hg emission concentration, and Hg emission standard deviation. Table 4.13 Unit 3 Hourly Average on Hg Emissions Descriptive Statistics From During Various Load Conditions From September 1st 2010, Through January 30, 2011 Category 1 Load < 600 MW Category 2 500 MW < Load < 600 MW Category 3 Load < 500 MW No. of samples 2,948 194 82 Mean (µg/m3) 3.15 1.86 0.64 Standard deviation (µg/m3) 0.99 0.63 0.45 Statistic This table shows that Unit 3 operated at or above 600 MW 90% of the time and hourly average Hg emissions decreased with load. A number of factors could explain this phenomenon, such as flue gas temperature and system residence time; however data are 159 not provided here to support clear and substantiated arguments. Although hourly average emissions decreased with load, the magnitude of the standard deviation relative to the mean increased. For categories 1 and 2, the ratio of the mean to the standard deviation was roughly 3 but for category 3 the ratio was 1.4. This suggests that, when adjusted for the mean, the Hg emissions in Category 3 were more than twice as variable. Figure 4.17, a graphical representation of the Unit 3 Hg emissions versus load category, conveys how the hourly average Hg emissions decreased as a function of load. Figure 4.17 Hourly average Unit 3 Hg emissions as a function of unit load (1, Load > 600 MW; 2, 500 MW < Load < 600 MW; 3, Load < 500 MW); the figure includes data from September 1, 2010, through January 30, 2011. 160 With each successive category moving from the left of the figure to the right, the hourly average Hg emissions are lower. The box for each category represents the 75% 25% quartiles with a line in the box representing the median. For each successive category the 75% - 25% quartiles is below the same quartile range in the immediately higher category. Clearly, both Table 4.13 and Figure 4.17 illustrate that Unit 3 hourly average Hg emissions vary as a function of load. 4.5.3.2 Case 2: Unit 4 Load Analysis Table 4.14 provides a summary of Unit 4 hourly average Hg emissions during the period when CaBr2 was not added. In this table, the data are sorted by load category, and lists the number of samples, mean Hg emissions and Hg emissions standard deviation. Table 4.14 Unit 4 Average Hourly Hg Emissions Descriptive Statistics of Various Load Conditions From September 1-30, 2010, and From January 1-30, 2011 Statistic Category 1 Category 2 Load > 600 MW 500 MW < Load < 600MW Category 3 Load < 500 MW Sample size 1,355 31 11 Mean (µg/m3) 2.40 1.05 1.37 Standard deviation (µg/m3) 0.86 0.90 0.99 The information in Table 4.14 indicates that hourly average Hg emissions decreased from Category 1 to Category 2 and increased from Category 2 to Category 3. Since the magnitude of the standard deviation was close to the magnitude of the mean for 161 Category 2 and 3, the variability of the Hg emissions was larger. Unit 4 operated in the high load category 97% of the time. This provides a large dataset to draw conclusions. The other two categories collectively represent only 3% of the samples and may be insufficient in size from which to draw conclusions. The magnitude of Hg emissions in the lowest load category reached 58% of Category 1 and 130% of the Category 2 emission values. Figure 4.18 provides a graphical representation of Unit 4 average hourly Hg emissions without CaBr2 addition by load category. Figure 4.18 Unit 4 hourly average Hg emissions as a function of unit load (1, Load > 600 MW; 2, 500 MW < Load < 600 MW; 3, Load < 500 MW); the figure includes Unit 3 Hg wet FGD stack emissions data from September 1-30, 2010, and from January 1-30, 2011. 162 As previously described, Hg emissions did decrease from the high-load condition to the low-load condition. The variation of Hg emissions are much wider on Unit 4 without CaBr2 addition when compared with Unit 3, but the magnitude of Unit 3 Hg emissions were higher. The figure does show a wide range of hourly average of Hg emission for the lower load condition. For the same period, this behavior is much different from what was observed on Unit 3. Table 4.14 and Figure 4.18 illustrate that, similar to Unit 3, Hg emissions decreased from the high-load condition to the mid-load condition. For Unit 4, the emissions did increase from the mid-load condition to the low-load condition. The sample sizes for mid and low-load conditions are small (31 and 11 respectively) and may lack sufficient samples to support substantiate conclusions. 4.5.3.3 Case 3: Analysis of Unit 4 Load During CaBr2 Addition Period The impact of load on hourly average Hg emissions during the CaBr2 addition period were particular noteworthy. Table 4.15 summarizes the Unit 4 Hg emissions data sorted by load category and includes number of samples, mean Hg emission concentration, and Hg emission standard deviation. 163 Table 4.15 Unit 4 Hourly Average Hg Emissions Descriptive Statistics of Various Load Conditions From October 1 Through December 19, 2010 Statistic Sample size Mean (µg/m3) Standard deviation (µg/m3) Category 1 Load > 600 MW Category 2 500 MW < Load < 600 MW Category 3 Load < 500 MW 1154 78 66 0.245 0.139 0.152 0.133 0.078 0.10 Unit 4 operated above 600 MW 89% of the time. The table reveals that Hg emissions were low across all load categories during CaBr2 addition and that variability within each category was low. Figure 4.19 contains a plot of Unit 4 hourly average Hg emissions during periods of CaBr2 addition by load category. Table 4.15 and Figure 4.19 show that, with CaBr2 addition, hourly average Hg emission values are much lower and do not vary as a function of load. The standard deviation was roughly equal to the mean, however, because of the low magnitude of the Hg emissions themselves, this variation is not significant. 164 Figure 4.19 Unit 4 hourly average Hg emissions as a function of unit load (1, Load > 600 MW; 2, 500 MW < Load < 600 MW; 3, Load < 500 MW); the figure includes Unit 4 wet FGD outlet Hg emissions data from October 1 through December 19, 2010. 4.5.3.4 Summary During CaBr2 addition, Unit 4 hourly average Hg emissions did not vary with load category. Without the addition of CaBr2, hourly average Hg emissions from Unit 3 proved sensitive to unit load, whereas Unit 4 Hg emissions were also sensitive to unit load but to a lower extent. For the evaluation of CaBr2 addition on Hg emission, the impact of load on Unit 4 Hg emissions are insignificant. 165 4.5.4 Impact of Calcium Bromide Addition Evaluating the ability of CaBr2 addition to reduce hourly average Hg emissions on Unit 4 involved using statistical methods to compare hourly average Hg emissions with and without CaBr2 addition. Table 4.16 provides descriptive statistics of Hg emissions from Unit 4, with data divided into the two periods of interest. Table 4.16 Unit 4 Hourly Average Hg Emissions Descriptive Statistics During Periods With and Without CaBr2 Addition CaBr2 Off September 1-30 / January 1-30 CaBr2 On October 1-December 19 1,434 1,688 Mean (µg/m ) 2.32 0.26 Standard deviation (µg/m3) 0.92 0.15 Statistic Sample size 3 An independent t-test was completed using Unit 4 hourly average Hg emissions as the dependent variable and CaBr2 addition (on/off) as the independent variable. The magnitude of effect was computed via the Cohen d test statistic. Partial eta squared was determined as an additional measure of magnitude of effect. The equality of the means (µbromine,test = µbromine,no) was tested as the null hypothesis, which was rejected. A significant difference existed for Unit 4 hourly average Hg emissions, t(3120) = 90.947, p < .01, with Hg emissions greater during periods when CaBr2 was not being added to the coal. Cohen’s d was 3.12, which 166 translates to a large magnitude of effect (Weinberg and Abromowitz, 2008). Partial eta squared was 0.726, which also translates to a high magnitude of effect (Barnette, 2006). The result statistically establishes that the hourly average Hg emissions during CaBr2 addition are lower from hourly average Hg emissions without CaBr2 addition. A large magnitude of the effect was found, that is the independent variable was responsible for the difference in Hg emissions. 4.5.5 Comparison of Hg Emissions From Unit 3 and Unit 4 The analytical protocol included conducting a paired t-test to determine if Unit 3 hourly average Hg emissions and Unit 4 hourly average Hg emissions were equal (µ3,no bromine = µ4,with bromine) during the period in which CaBr2 was added to Unit 4 but was not added to Unit 3. The null hypothesis was rejected, t(1259) = 112.980, p < .01. The Unit 3 hourly average Hg emissions were greater than Unit 4 Hg emissions during CaBr2 injection on Unit 4. 4.5.6 Br/Hg Ratio Impact on Hg Removal Performance Table 4.17 is a summary of Br/Hg ratios during Phase III. The available information is limited; coal Hg concentration data was available for only 11 test days. The minimum daily Br concentration (wt ppm on the dry coal) for the days coal data were available were used to calculate a conservative value of the Br/Hg ratio (lb/lb). During Phase III, the lowest known Br/Hg ratio (lb/lb) of 258 was observed on December 16, 2010. Figure 4.16 shows low Hg emissions (0.5 µg/m3) for that day. 167 Table 4.17 Phase III Br/Hg Ratio Summary Based on Hg Content Measured in the Coal and Minimum Observed Daily Br Concentrations (wt ppm on the dry coal) Minimum Daily Br Concentration (wt ppm on the dry coal) Br/Hg Ratio (lb/lb) Date Coal Sample Taken Sample Hg Content (wt ppm) 9/29/10 1 0.072 1.3a 18 a 9/30/10 2 0.061 1.3 21 10/7/10 3 0.032 22.2 694 10/14/10 4 0.045 17.1 380 10/21/10 5 0.050 20.4 408 10/28/10 6 0.054 17.9 331 11/11/10 7 0.049 18.9 386 11/17/10 8 0.048 16.9 352 11/22/10 9 0.036 17.2 479 11/29/10 10 0.044 17.8 405 12/16/10 11 0.031 8.0 258 a. Coal Br concentration used during period without CaBr2 addition. The calculated Br/Hg ratio of 258 exceeds the Br/Hg >250 recommendation for full Hg oxidation. The Br/Hg ratios for the other testing days having known coal Hg content were above 250. The Unit 4 average Hg emissions during Phase III were 0.26 µg/m3. The combination of these two facts supports the minimum Br/Hg ratio of 250 (lb/lb) when a well-designed and maintained SCR is present. 4.5.7 Summary The null hypothesis that Hg emissions with and without CaBr2 addition are the same has been rejected at the 99% confidence level. In addition, statistical methods were 168 used to demonstrate that CaBr2 addition was responsible for the reduction of Unit 4 Hg emissions. In addition the following general conclusions were drawn: • During Phase III, changes in coal characteristics impacted hourly average Hg emissions on Unit 3 and Unit 4 but its impact was found to be minimal and did not affect the evaluation of CaBr2 injection technology. • Load changes on Unit 3 and Unit 4 affected Hg emissions during periods without CaBr2 addition. During low load (i.e., <500 MW), Hg emissions on Unit 3 were below 0.7 µg/m3. The impact of low load operations on Unit 4 Hg emissions was less pronounced. • Unit 4 Hg emissions decreased significantly during periods of CaBr2 addition. • Unit 4 Hg emissions had a mean of 0.26 µg/m3 and a standard deviation of 0.156 µg/m3 during the 83-day period when CaBr2 was added to the dry coal. Unit 4 Hg emissions had a mean of 2.32 µg/m3 and a standard deviation of 0.92 µg/m3 when CaBr2 was not added to the coal. 4.6 Hypothesis 5: Hg Emission Rates Achieved During the Use of CaBr2 Addition Are Sufficiently Low to Meet the MATS Rule Hg Limit of 1.2 lb/TBtu on a 30Day Rolling Average 4.6.1 Overview Phase III hourly average Hg emissions data were used to determine the effectiveness of CaBr2 addition in reducing Hg emissions as a compliance tool for achieving the MATS Hg limit of 1.2 lb/TBtu using a 30-day rolling average. The protocol included using two approaches to test the hypothesis. In the first approach, Unit 169 4 hourly average emissions were converted from a concentration basis to an input basis emission rate, using EPA Method 19, and plotted alongside the 1.2 lb/TBtu compliance limit. If all of the hourly emission rate averages were below the 1.2 lb/TBtu limit, then the hypothesis would be deemed proven. In the second approach, 30-day rolling Hg emission averages from Unit 3 and Unit 4 were computed and chronologically plotted alongside the 1.2 lb/TBtu compliance limit. For Unit 4, if all the 30-day rolling Hg emission average were below the 1.2 lb/TBtu, the hypothesis was deemed proven. Additionally, the Wilcox Rank Sign test was used to compare Unit 3 and Unit 4 30-day rolling Hg emissions averages and determine whether Hg emission rates from the two units were statistically different. In addition to the testing of the hypothesis, a simulation of a 7-day CaBr2 addition system outage was completed by appending Unit 4 Hg emissions data from September 1, to September 8, 2010, to the existing 30-day rolling Hg emission averages and additional 30-day rolling Hg emission averages were computed. Plotting the data enabled quantification of the impact the 7-day outage on 30-day rolling Hg emission averages. 4.6.2 Unit 4 Hourly Average Hg Emission Rate Analysis Figure 4.20 shows chronological plot of Unit 4 hourly average Hg emission rate (lb/TBtu). The figure includes Br concentration (wt ppm on dry coal) and the MATS rule Hg limit of 1.2 lb/TBtu. At the extreme left, the figure illustrates a period without CaBr2 addition to the coal. Once CaBr2 was added, the Hg emissions decrease was immediate. 170 Variable Load Reduced bromine Stable Load Figure 4.20 Chronological plot of Phase III Unit 4 hourly average Hg emissions rate (lb/TBtu) and Br concentration (wt ppm on dry coal) during the 83-day CaBr2 injection test. In the absence of CaBr2 addition, the Hg emission rate exceeds the proposed MATS rule limit. Once CaBr2 was added on October 1, the Hg emission rate falls well below the 1.2 lb/TBtu limit. The Br concentration (wt ppm on the dry coal) was variable during the entire test period. The addition rate of CaBr2 solution was held constant while unit load was allowed to vary to meet electricity demand. This caused the Br concentration on the coal to vary. The Br concentration variability is clearly observed in Figure 4.20. While the Br concentration did vary with load, the Hg emission rate did not vary correspondingly. The figure illustrates two periods, one in which the Br concentration varied widely and one period during which the Br concentration was fairly constant. These are labeled in the figure as periods of variable and stable load. During 171 the two periods the variability of Hg emissions remained unchanged indicating that the Hg emissions and Br concentration were not strongly linked. This suggests that sufficient bromine was present to ensure sufficient Hg oxidation and that any extra bromine did not result in a decrease in Hg emissions. For the entire CaBr2 injection period low Hg emissions are observed. In a few instances in late October, the emission rate does exceed the 1.2 lb/TBtu limit. After an unplanned outage on December 6, 2010, the Br concentration was reduced from 20 wt ppm to 10 wt ppm, then to 8 wt ppm, and then to 2 wt ppm. With the Br concentration reduced, the Hg emission rate began to exceed 1.2 lb/TBtu more frequently. This finding suggests that, although CaBr2 addition effectively reduced Hg emissions, the Br concentration must be maintained at a minimum level to achieve the desired results. Because a few hourly Hg emission rate averages occurred that exceeded the MATS limit of 1.2 lb/TBtu, additional analysis is needed to verify the hypothesis. 4.6.3 Unit 3 and Unit 4 30-Day Hg Emission Rate Analysis Figure 4.21 is a chronological plot of 30-day rolling Hg emission rate averages from Unit 3 and Unit 4 and includes a vertical line representing the 1.2 lb/TBtu MATS rule Hg limit. As the figure shows, at no point during the 83-day test did the Unit 4 30day rolling Hg emission averages exceed the MATS rule Hg limit of 1.2 lb/TBtu. In fact, the rolling average remained well below the limit each day. Unit 4 had a maximum 30day rolling Hg emissions average of 0.41 lb/TBtu and a minimum 30-day rolling Hg emissions average of 0.21 lb/TBtu. The Unit 4 30-day rolling averages included 172 instances of uncontrolled emissions during a start-up condition when the CaBr2 addition system was not in service. The observed behavior for Unit 3 differed. At no point during Phase III did the magnitude of the Unit 3 30-day rolling average fall below the MATS rule Hg limit. Figure 4.21 does show a downward trend in Hg emissions, but this trend did not bring Unit 3 below the MATS rule compliance limit. Figure 4.21 Chronological plot of Phase III Unit 4 and Unit 3 daily and 30-day rolling Hg emissions rate (lb/TBtu). 173 A statistical comparison of Unit 4 and Unit 3 30-day rolling averages was completed using the Wilcox Ranked Sign Test. The observed difference between both measurements is statistically significant and the null hypothesis that the means were equal was rejected. Details of the Wilcox Ranked Sign test can be found in Appendix D. 4.6.4 Seven-day CaBr2 Addition System Outage Simulation Figure 4.22 was created by adding 7 days of daily average Hg emission rate data from September 1-7, 2010, to the end of the Unit 4 Phase III CaBr2 addition Hg emissions rate data and new 30-day rolling Hg emission averages were computed. Figure 4.22 Seven-day simulation of CaBr2 injection system outage combining Phase III Unit 4 30-day rolling Hg emissions rate data with Unit 4 daily Hg emissions rate data during September 1-7, 2010. The resulting plot represents the impact of higher emissions on MATS rule compliance. 174 The choice of the 7 days added to the data received no special consideration, and it is assumed that the 7 days selected typify, from an Hg emissions standpoint, all other 7day periods. The simulation was done to mimic a response in 30-day rolling Hg emission averages if the CaBr2 addition system was unavailable for 7 days. Equipment outages are an infrequent but normal part of operating a power plant. A CaBr2 outage could result from the lack of availability of CaBr2 or equipment failure. The 7-day period represents an extreme case because CaBr2 systems are mechanically simple and a temporary system to treat a full-scale system could be assembled from off-the-shelf components within a few days. Shortages of CaBr2 can be effectively managed with a conservative procurement program (i.e., storing large volumes of chemical onsite). The chemical is readily available, and only 208 L (55 gallons) of 52% CaBr2 solution are needed to treat a 720 MW unit operating at full load for an entire day at Br concentration of 20 wt ppm on the dry coal. Figure 4.22 illustrates the effect of higher daily Hg emissions on 30-day rolling Hg emission averages by the loss of the CaBr2 addition system. As expected, the system outage adversely affected the 30-day rolling Hg emission averages, which increased to a final value of 1.20 lb/TBtu, exactly equal to the MATS rule Hg limit. Utilities typically desire to operate with emissions well below regulatory limit at all times, which is typically referred to as compliance margin. If a utility wanted to maintain a 20% compliance margin, then the effective MATS rule compliance limit would become 0.96 lb/TBtu. If a 20% compliance margin is added as a constraint here, a 5-day CaBr2 system outage could be supported. 175 4.6.5 Summary The hypothesis is true; CaBr2 addition lowered Hg emission sufficiently to meet the MATS Hg limit of 1.2 lb/TBtu on a 30-day rolling average. Unit 4 had a range of 30day rolling Hg emission averages from a maximum value of 0.41 lb/TBtu and a minimum value of 0.21 lb/TBtu, which included an instance of uncontrolled emissions during a start-up event when the CaBr2 addition system was not in service. Additionally, short periods without CaBr2 addition could be allowed without exceeding the MATS rule Hg limit; in fact, Miller Unit 4 could support a 5-day continuous CaBr2 addition system outage and still maintain a 20% compliance margin. 4.7 Hypothesis 6: The Presence of an SCR Can Greatly Reduce the Application Cost of CaBr2 Injection Technology and Dramatically Improve the Cost Benefit of Utilizing the Approach When Compared to Activated Carbon Injection into an Existing Cold-side ESP 4.7.1 Economic Analysis of CaBr2 Addition The results of this research were used to compare the MATS rule compliance cost of employing CaBr2 addition with the compliance cost of activated carbon injection into an existing cold-side ESP. Table 4.18 is a summary of CaBr2 addition information used to determine usage cost. In addition to using the assumptions in Table 4.18, the economic analysis included information from Table 4.6 that yielded results for two cases. For Case 1, with an SCR in service, a yearly volume of 16,461 gallons of 52 wt% CaBr2 solution with an associated chemical cost of $208,774 was determined. For Case 2, without an SCR, a 176 yearly volume of 197,534 gallons of 52 wt% CaBr2 solution with an associated chemical cost of $2,505,293 was found. Table 4.18 Financial and Miller Unit 4 Operation Assumptions Used to Calculate Yearly CaBr2 Chemical Costs Item Value Units 10 lb/TBtu 800,000 lb/h 8,500 Btu/lb Unit capacity factor 0.9 Dimensionless Br/Hg ratio case 1 250 lb/lb Br/Hg ratio case 2 3,000 lb/lb CaBr2 solution cost 0.90 $/lb solution PRB coal Hg content Full load coal flow rate Coal higher heating value 4.7.2 Economic Analysis of Activated Carbon Injection (ACI) into a Cold-side ESP After a number of research and development programs sponsored by the Department of Energy National Energy Technology Laboratory (DOE NETL) were completed, Jones, et al. (2007) published consolidated findings regarding the technical and commercial viability of Hg control technologies. This report included cost information related to the use of ACI to remove Hg from the flue gases of various coal types, including PRB. ACI into a cold-side ESP has been demonstrated as a viable option for achieving 90% Hg reduction from PRB coal (Jones et al., 2007). This fact 177 enables determination of the relative efficacy of using CaBr2 addition as a cost-effective option for MATS rule compliance by comparing the cost of these two options. Table 4.19 lists the assumptions used to determine the cost of ACI into an existing cold-side ESP to achieve compliance with the Hg portions of the MATS rule. Using the assumptions in Table 4.18 reveals a yearly mass flow of 3,756,883 lb of activated carbon at a cost of $3,569,039. Table 4.19 Financial Assumptions Used to Calculate Activated Carbon Costs for One Year of Operation at Miller Unit 4 With a 90% Hg Capture Goal When the Unit Operated With a 90% Capacity Factor Item Value Units 2,850,000 acfm Average activated carbon concentrationb 2.79 lb/Macf Unit capacity factor 0.90 Dimensionless 0.95 $/lb Cold-side ESP inlet flue gas volumea Activated carbon cost b 3 6 3 Notes: acfm = actual ft /min; Macf = 10 ft . a. Average gas volume measured during Phase I Method 17 testing. b. Value from Jones, et al. (2007) to achieve 90% Hg removal on PRB coal. 4.7.3 Comparison Cost of 90% Hg Control Jones et al. (2007) calculated the total direct cost for the ACI system, including equipment cost, cost of materials and labor associated with site integration, applicable taxes, and installation cost. Each approach (e.g. activated carbon injection and CaBr2 injection) requires an injection/addition system to introduce its active component to the flue gas stream. Jones et al. (2007) calculated a total direct cost range of $3.82/kW to 178 $16.02/kW (2006 dollars) for ACI-related equipment. NRDC (2011) estimated a $2/kW capital cost for CaBr2 addition equipment. The total direct cost were ignored in this financial analysis, which likely favored the ACI approach and provided a conservative estimate for any cost savings associated with CaBr2 addition. This analysis also involved ignoring the balance of plant impact costs because little is known about these costs associated with CaBr2 addition. Jones et al. (2007) described substantial balance of plant costs associated with ACI. These costs stemmed mainly from the loss of fly ash sales for concrete admixture usage. Jones et al. (2007) estimated a roughly 2.5-fold increase in the $/lb Hg removed when the loss of fly ash sales was considered. With an assumed fly ash total avoided cost value of $35/ton (fly ash sales income and landfill avoidance cost) a $7M value was computed for fly ash sales if the PRB coal arriving at Plant Miller was 8% ash and, 80% reported to the cold-side ESP. Larrimore et al. (2008) reported that CaBr2 addition would not preclude the use of fly ash within concrete admixtures. The decision to ignore the balance of plant effects again likely favors the ACI approach and provided a conservative estimate for any cost savings associated with CaBr2 addition. Table 4.20 contains a summary of the cost of CaBr2 addition to achieve 90% Hg control with and without an SCR present and includes the cost of ACI into an existing cold-side ESP. The table includes only the reagent costs (chemical or carbon) and excludes total direct costs and balance of plant impacts. It was assumed that these exclusions favored ACI systems and provided a conservative comparison of the approaches. 179 A significant differential exists between the costs of using CaBr2 addition with an SCR in service and those incurred without an SCR. In comparison with the reagent cost of ACI, the lower expense of either CaBr2 addition approach yields significant financial savings. Table 4.20 Comparison of CaBr2 and Activated Carbon Injection Reagent Costs Associated With 90% Hg Removal From a Boiler Burning PRB Coal With an SCR/Cold-side ESP/Wet FGD or Cold-side ESP/Wet FGD Configuration Br/Hg Ratio (lb/lb) CaBr2 Yearly Cost ($M) Activated Carbon Injection Rate (lb/Macf)a Activated Carbon Yearly Cost ($M) Cold side ESP and Wet FGD 3,000 2.505 2.79 3.57 SCR/Cold-side ESP and Wet FGD 250 0.208 2.79 3.57 Note: Macf =106 ft3. a. activated carbon rate based on the use of chemically treated carbon. 4.7.4 Summary The presence of an SCR reactor greatly reduces the application cost of CaBr2 addition. With an SCR, the chemical reagent costs were an order of magnitude less. In both cases of CaBr2 injection with and without an SCR, the compliance cost proved less when compared to activated carbon injection into an existing cold-side ESP. The financial analysis excluded total direct and balance of plant impact costs, but these costs are likely much greater for activated carbon injection therefore the difference in costs is likely much wider than shown here. 180 The analysis supported the hypothesis; the cost of compliance with the MATS rule using CaBr2 injection is lower than compliance costs associated with using activated carbon injection into an existing cold-side ESP. 181 CHAPTER 5 INTERPRETATIONS AND RECOMMENDATIONS The study consisted of a three-phase program conducted at Alabama Power Company’s Plant Miller Unit 4, a 700 MW PRB coal-fired power plant equipped with an SCR, cold-side ESP and wet FGD, to evaluate the effectiveness of CaBr2 injection at oxidizing and removing elemental Hg from flue gas. The goal was to determine whether CaBr2 injection reduced emissions sufficiently to comply with the Hg portion of the MATS rule limit of 1.2 lb/TBtu on a 30-day rolling average. The work yielded the following conclusions: • The Plant Miller Unit 4 SCR possesses positive attributes that promote Hg oxidation, including a space velocity less than 2,000 h-1, relative NOx activity (K/Ko) greater than 0.7, and an operating temperature of 310 to 380 °C. However, baseline Hg oxidation levels were insufficient to support MATS rule compliance without additional technology, primarily because PRB coal halogen content does not support high levels of Hg oxidation. • CaBr2 injection promotes Hg oxidation levels in excess of 90%, and the presence of the SCR decreases ten-fold the amount of CaBr2 required to achieve these levels of oxidation. 182 • The presence of ammonia in the SCR has a minor affect on Hg oxidation. A slightly higher concentration of bromine in the flue gas mitigates this effect. • The relative NOx activity (K/Ko) plays an active role in the oxidation of mercury across the SCR. As the relative NOx activity ratio (K/Ko) decreases, a higher concentration of bromine in the flue gas is needed to compensate for less active catalyst. • Combined with a well functioning SCR, a Br/Hg ratio > 250 (lb/lb) results in Hg oxidation and removal efficiencies exceeding 90%, if the captured Hg is not reemitted from the wet FGD sump. For a non-SCR application, a Br/Hg ratio > 3,000 (lb/lb) is recommended for similar Hg oxidation and removal efficiencies. • Reemission of captured Hg represents a source of compliance risk for Hg oxidation and capture techniques such as CaBr2 injection. Mercury reemissions are a function of many wet FGD slurry parameters such as sulfite concentration, chlorine and bromine concentrations, solid and liquid Hg concentrations, and ORP. Significant Hg reemission events were not observed during this investigation. • During the 83-day calcium bromide injection evaluation period, Unit 4 hourly average mercury emissions had a mean of 0.26 µg/m3, with a standard deviation of 0.16 µg/m3. During the 30 days before and after the evaluation period, Unit 4 hourly average mercury emissions had a mean of 2.32 µg/m3 and a standard deviation of 0.92 µg/m3. 183 • A statistically significant difference, t(3120) = 90.95, p < 0.01, existed between hourly average Hg emissions with and without CaBr2 injection. A Cohen’s d statistic value of 3.12 demonstrated that the CaBr2 was largely responsible for the reduction of Hg emissions. • Changes in coal characteristics and operational factors such as unit load and SCR ammonia flow rate affect Hg emissions but were shown to have minor effects, when compared to the impact of CaBr2 injection. • CaBr2 injection lowers Hg emissions sufficiently to meet the MATS rule limit of 1.2 lb/TBtu on a 30-day rolling average. During the 83-day long-term evaluation, Unit 4 had a maximum 30-day rolling average Hg emission of 0.41 lb/TBtu and a minimum 30-day rolling Hg average emission of 0.21 lb/TBtu. The 30-day rolling averages included a start-up and shutdown event during which emissions were uncontrolled. During the same 83-day period Hg emissions on Unit 3, which is similar to Unit 4, were twice the MATS rule limit. • Unit 4 could support a 5-day continuous CaBr2 injection system outage and still maintain a MATS rule compliance margin of 20%. • The cost of using CaBr2 injection to achieve compliance with the MATS rule is lower than the cost associated with using activated carbon injection into an existing cold-side ESP. Yearly CaBr2 chemical costs are $208,774 with an SCR and $2,505,293 without an SCR. In comparison, sorbent costs for activated carbon injection into an existing cold-side ESP would be $3,569,039. 184 CHAPTER 6 IMPLICATIONS FOR FURTHER RESEARCH During the study, an opportunity did not exist to vary independent variables to determine their effects on Hg oxidation behavior; neither did the study parameters enable detailed research into the nature of Hg reemission from the wet FGD sump. Both areas have implications in managing compliance risk for utilities. The following work is proposed to address these concerns: • Additional fundamental work is needed to understand the impact of SO2 concentration on Hg oxidation via the chlorine and bromine Griffin reactions. Vosteen et al. (2006) clearly articulated that Hg oxidation via bromine is impacted less by SO2 than Hg oxidation via chlorine, but it is at some point impacted nevertheless. Other experience, reported by Ghorishi et al. (2005), Silcox et al. (2008), Buitrago et al. (2010), Niksa et al (2010), Smith et al. (2011), and Otten et al. (2011) yielded conflicting findings concerning the impact of SO2 on Hg oxidation with bromine, with some authors reporting that SO2 does impact bromine-assisted Hg oxidation and others concluding that SO2 does not affect bromine-assisted Hg oxidation. To resolve this variation in results, it is suggested that researchers conducting bench-scale experiments include in their studies variable SO2 concentration, homogeneous 185 and heterogeneous (native and SCR-based) oxidation pathways, and replication of the power plant flue gas temperature profile from the economizer outlet to the wet FGD inlet, that is vary simulated flue gas temperatures from 700 to 55 °C. The upper temperature would represent economizer inlet conditions and the lower temperature would represent wet FGD inlet conditions. Simulated flue gas SO2 concentrations should be representative of 0.3 to 2.5 wt % sulfur coals at a minimum. • More fundamental work is needed to increase understanding of the role of the NOx relative catalyst activity ratio (K/Ko) in Hg oxidation. Even though Dranga et al. (2012) described the importance of ammonia and catalyst activity on Hg oxidation, technology users need additional guidance. Quantification of the relationship between relative catalyst activity (K/Ko) and Hg oxidation would allow users to properly manage their SCR catalyst purchases to minimize NOx emissions and maximize Hg oxidation. • More fundamental work is needed regarding the parameters that affect Hg reemission from wet FGD sumps. The relationships among factors that govern Hg reemission remain incompletely understood, and this lack of technical understanding hampers the ability of users to control Hg emissions by leveraging the solubility of oxidized Hg. Although Blythe et al. (2008) and Omine et al. (2010) provided a framework with which to better understand Hg reemission, the industry has not yet obtained sufficient wet FGD chemistry data to confirm the observations of researchers. The lack of full-scale, realtime wet FGD inlet and outlet flue gas Hg measurements leaves utilities 186 without sufficient information to correlate Hg reemission events and wet FGD chemistry data. A coordinated effort between fundamental and applied researchers will result in substantial progress in this area. • More fundamental work is needed to describe the mechanisms that control Hg partitioning between solid and liquid phases in a wet FGD after the oxidized Hg has been captured. An increase in understanding would provide utilities with the knowledge necessary to better manage Hg remission risk. • Future full-scale CaBr2 injection tests should include taking coal samples daily, to determine coal Hg content. The Br/Hg ratio (lb/lb), a key parameter controlling Hg oxidation has not been a focus of previous research at fullscale. Because this ratio provides a proper basis on which to compare results from different testing programs, parametric and continuous injection tests should be designed around this parameter, rather than just the mass flow rate of CaBr2 or Br concentration on the coal. 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Fuel Processing Technology 88: 929-34. 198 APPENDIX A PHASES I, IIA, IIB, AND III BASELINE MERCURY OXIDATION INFORMATION 199 APPENDIX A PHASES I, IIA, IIB, AND III BASELINE MERCURY OXIDATION INFORMATION Phase Equipment Configuration Measurement Location Total Hg Concentration (µg/Nm3) !!"#$#%&$ !!"!#$ Measurement Average Period (Hr:Min) Measurement Technique I A SCR Inlet 10.80 0.42 12 SCEM I A SCR Outlet 13.80 0.44 12 SCEM I A Wet FGD Inlet 8.20 0.59 12 SCEM I A SCR Inlet 12.60 0.17 10 SCEM I A SCR Outlet 11.20 0.17 10 SCEM I A Wet FGD Inlet 9.30 0.62 10 SCEM I A SCR Inlet 8.20 0.13 13 SCEM I A SCR Outlet 7.50 0.58 13 SCEM I A Wet FGD Inlet 6.00 0.58 13 SCEM I A SCR Inlet 10.80 0.33 10 SCEM I A SCR Outlet 8.70 0.32 10 SCEM I A ESP Inlet 7.10 0.41 10 SCEM I A Wet FGD Inlet 7.20 0.57 10 SCEM I A SCR Inlet 12.30 0.15 10 SCEM I A SCR Outlet 10.10 0.17 10 SCEM I A ESP Inlet 8.70 0.40 10 SCEM I A Wet FGD Inlet 8.60 0.66 2 SCEM I A Wet FGD Inlet 9.50 0.56 2 OH I A Wet FGD Inlet 11.80 0.64 2 OH I A Wet FGD Inlet 11.90 0.67 2 OH IIA C Wet FGD Inlet 5.20 0.64 2 OH IIA C Wet FGD Inlet 5.22 0.62 2 OH IIA C Wet FGD Inlet 6.88 0.61 2 OH IIA B SCR Inlet 13.60 0.15 10 SCEM IIA B SCR Outlet 4.60 0.41 6 SCEM IIA B SCR Inlet 12.00 0.05 6 SCEM IIA B SCR Outlet 5.10 0.50 6 SCEM IIA B SCR Inlet 13.20 0.06 5:45 SCEM IIA B SCR Outlet 8.00 0.57 5:45 SCEM IIA B SCR Inlet 16.70 0.05 5 SCEM 200 Phase Equipment Configuration Measurement Location Total Hg Concentration (µg/Nm3) !!"#$#%&$ !!"!#$ Measurement Average Period Measurement Technique IIA B SCR Outlet 11.90 0.23 5 SCEM IIA B SCR Outlet 8.00 0.37 6 SCEM IIA C Wet FGD Inlet 5.40 0.46 9:30 SCEM IIA C Wet FGD Inlet 7.70 0.35 10 SCEM IIA C Wet FGD Inlet 4.40 0.54 10 SCEM IIA C Wet FGD Inlet 8.00 0.57 4:15 SCEM IIA C Wet FGD Inlet 9.40 0.46 4:15 SCEM IIA C Wet FGD Inlet 7.30 0.51 6 SCEM IIA C Wet FGD Inlet 4.30 0.52 9 SCEM IIA C Wet FGD Inlet 5.20 0.46 9 SCEM IIA B Wet FGD Inlet 8.40 0.81 6 SCEM IIA B Wet FGD Inlet 10.50 0.65 5 SCEM IIA B Wet FGD Inlet 16.50 0.85 6 SCEM IIB A Wet FGD Inlet 4.67 0.53 2 OH IIB A Wet FGD Inlet 5.11 0.54 2 OH IIB A Wet FGD Inlet 4.80 0.49 2 OH IIB A Wet FGD Inlet 5.57 0.54 2 OH IIB A Wet FGD Inlet 4.40 0.29 8 SCEM IIB A Wet FGD Inlet 4.30 0.42 8 SCEM IIB A Wet FGD Inlet 5.60 0.46 8 SCEM III A Wet FGD Inlet 6.40 0.55 2 OH III A Wet FGD Inlet 4.97 0.52 2 OH III A Wet FGD Inlet 4.76 0.56 2 OH 201 APPENDIX B PHASES I, IIA, IIB, AND III COAL MERCURY CONCENTRATION 202 APPENDIX B PHASES I, IIA, IIB AND III COAL MERCURY CONCENTRATION Phase I Phase IIA Phase IIB Phase III Sample Hg Concentration Hg Concentration Hg Concentration Hg Concentration (wt ppm) (wt ppm) (wt ppm) (wt ppm) 1 0.048 0.058 0.062 0.074 2 0.107 0.041 0.070 0.061 3 0.056 0.046 0.105 0.030 4 0.085 0.058 0.060 0.043 5 0.057 0.045 0.055 0.047 6 0.091 0.054 0.058 0.052 7 0.059 0.057 n/a 0.047 8 0.080 0.045 n/a 0.051 9 n/a n/a n/a 0.034 10 n/a n/a n/a 0.049 11 n/a n/a n/a 0.032 Adapted from Table B-8 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2007 p. B-7. Copyright 2007 by EPRI. Reprinted with permission. Adapted from Table 33 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. 3-51. Copyright 2009 by EPRI. Reprinted with permission. Adapted from B-13 “The Evaluation of Calcium Bromide for Mercury Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2009 p. B-14. Copyright 2009 by EPRI. Reprinted with permission. Adapted from Table B-14 “Three-Month Evaluation of Furnace Addition of Calcium Bromide for Mercury Emissions Control at Southern Company’s Plant Miller” by Dombrowski, K. et al., 2011 p. B-16. Copyright 2011 by Southern Company Serivces. Reprinted with permission. 203 APPENDIX C NORMALITY ANALYSIS 204 APPENDIX C.1 NORMALITY OF UNIT 3 HOURLY MERCURY EMISSIONS DURING JANUARY 2011 Appendix C.1 includes the analysis for determining the normality of Unit 3 hourly average Hg emissions data from January 1, 2011, through January 30, 2011, while CaBr2 was not being added to Unit 4. Figure C.1 is a histogram of Unit 3 hourly averaged Hg emissions during the period of interest. The histogram plots frequency of Hg emissions in particular concentration ranges. The graph includes a line representing the frequency of a normal distribution. Figure C.1 Histogram of Unit 3 hourly average Hg emissions (µg/m3) from January 1-30, 2011, while CaBr2 was not added to the coal on Unit 4. 205 The histogram shows that the data are nearly normal. The most frequently observed hourly average Hg emissions appear near the center of the distribution, and the data do not appear skewed. Additionally, the frequency magnitudes appear near the normal distribution. Figure C.2 charts expected cumulative probability versus observed cumulative probability (P-P plot). A normal dataset would have a P-P plot that is a straight-line, in other words, observed values for the data equal the expected values of normally distributed data. Figure C.2 Normal expected cumulative probability versus observed cumulative probability (P-P Plot) of Unit 3 hourly average Hg emissions (µg/m3) from January 1, 2011, to January 30, 2011, while CaBr2 was not added to the coal on Unit 4. 206 Figure C.2 shows that observed cumulative probability is close to expected cumulative probability with small variations. At some points, within the P-P plot, the observed behavior exceeds predicted behavior, at some points the converse is true. Nevertheless, the data are nearly normal using the graphical methods in Figures C.1 and C.2. Table C.1 provides summary information regarding the Unit 3 hourly averaged Hg emissions during January 1-30, 2011. The table includes the mean, standard deviation, skewness, kurtosis, and the Jarque-Bera (JB) statistic. Skewness measures the asymmetry of the data around the mean. The skewness of a normal distribution is zero. Kurtosis measures the fraction of outliers in a distribution (i.e., whether the data are peaked or flat relative to a normal distribution). A large value means that the dataset is peaked about the mean, and a low value indicates relatively flat values about the mean. A normal distribution has a kurtosis value of 3. The SPSS value of kurtosis is adjusted for normality (i.e., K-3), therefore a value of zero indicates a normal distribution. The JB statistic is a measure of normality, follows a Chi-squared distribution with a degree of freedom of 2, and can be used to quantitatively test for normality. The summary statistics tabulated in Table C.1 does not support the conclusion drawn from Figures C.1 and C.2 that the data are nearly normally distributed. The values of skewness and kurtosis are close to zero but are slightly negative, indicating more of the data points are above the mean and that the frequencies are below the normal distribution. This distribution is slightly flatter than a normal distribution. Table C.1 Summary Statistics of the Unit 3 Hourly Average Hg Emissions (µg/m3) from January 1, 2011, to January 30, 2011, while CaBr2 was Not Added to the Coal on Unit 4. 207 Statistic Value Unit Sample size 719 n/a Mean 2.6434 µg/m3 Standard deviation 1.0136 µg/m3 Kurtosisa -0.012 n/a -0.635 n/a 12.09 n/a Skewness Jarque-Bera (JB) b Note: a. Kurtosis calculated by SPSS has been adjusted. A value of zero represents a normal distribution. b. Jarque-Bera statistic formula has been adjusted for excess kurtosis. The JB statistic is large (12.09). After applying the Chi-squared distribution (df = 2) the hypothesis that Unit 3 hourly average Hg emissions from January 1-30, 2011, were normal was rejected (p < .01). 208 APPENDIX C.2 NORMALITY OF UNIT 3 HOURLY MERCURY EMISSIONS DURING SEPTEMBER 2010 Appendix C.2 includes the analysis for determining the normality of the Unit 3 hourly average Hg emissions data from September 1-30, 2010, while CaBr2 was not being added to Unit 4. Figure C.3 is a histogram of the Unit 3 hourly averaged Hg emissions during the period of interest. The histogram plots the frequency of Hg emissions in particular concentration ranges. The graph includes a line representing the frequency of a normal distribution. Figure C.3 Histogram of Unit 3 hourly average Hg emissions (µg/m3) from September 130, 2010 while CaBr2 was not added to the coal on Unit 4. 209 The histogram shows that the data are nearly normal but do not exhibit normal behavior. The most frequently observed hourly average Hg emissions are near the center of the distribution, and the distribution appears to have a long tail with more of the data values above the mean, this would indicate positive skewness. Figure C.4 charts an expected cumulative probability versus observed cumulative probability (P-P plot). A normal dataset would have a P-P plot that is a straight line; that is observed values equal the expected values of a normally distributed dataset. Figure C.4 Normal expected cumulative probability versus observed cumulative probability (P-P Plot) of Unit 3 hourly average Hg emissions (µg/m3) from September 1-30, 2010 while CaBr2 was not added to the coal on Unit 4. 210 Figure C.4 shows that observed cumulative probability is close to expected cumulative probability with some variations. At some points, within the P-P plot, the observed behavior exceeds predicted behavior and at some points the converse is true, nevertheless the data are nearly normal using the graphical methods in Figures C.3 and C.4. Table C.2 provides summary information regarding the Unit 3 hourly averaged Hg emissions during September 1-30, 2010. The table includes the mean, standard deviation, skewness, kurtosis, and the JB statistic. Skewness measures the asymmetry of the data around the mean, and the skewness of a normal distribution is zero. Kurtosis measures the fraction of outliers in a distribution (i.e., whether the data are peaked or flat relative to a normal distribution). A large value means the dataset is peaked about the mean, and a low value indicates relatively flat values about the mean. A normal distribution has a kurtosis value of 3. The SPSS value of kurtosis is adjusted for normality (i.e., K-3), therefore a value of zero indicates a normal distribution. The JB statistic is a measure of normality, follows a Chi-squared distribution with a degree of freedom of 2, and can be used to quantitatively test for normality. The summary statistics tabulated in Table C.2 support the conclusions drawn from Figures C.3 and C.4 that the data are not normally distributed. A large positive value of skewness (2.334) indicates that a majority of the data points are above the mean, and a negative value of kurtosis indicates that the distribution is flatter than a normal distribution. 211 Table C.2 Summary Normality Statistics of Unit 3 Hourly Average Hg Emissions (µg/m3) from September 1-30, 2010, While CaBr2 Was Not Added to the Coal on Unit 4. Statistic Value Unit Sample size 695 n/a Mean 3.8239 µg/m3 Standard deviation 0.8283 µg/m3 Kurtosisa -0.862 n/a 2.334 n/a 244 n/a Skewness Jarque-Bera (JB) b Note: a. Kurtosis calculated by SPSS has been adjusted. A value of zero represents a normal distribution. b. Jarque-Bera statistic formula has been adjusted for excess kurtosis. The JB statistic is large (244). When the Chi-squared Distribution (df = 2) was used, the hypothesis that the Unit 3 hourly average Hg emissions from September 1-30, 2010, were normal was rejected. 212 APPENDIX C.3 NORMALITY OF UNIT 3 PHASE III HOURLY MERCURY EMISSIONS Appendix C.3 includes the analysis for determining the normality of the Unit 3 Hg hourly average emissions data from October 1, 2010, through December 19, 2010, during the addition of CaBr2 to the coal on Unit 4. Figure C.5 is a histogram of the Unit 3 hourly averaged Hg emissions during the period of interest. The histogram plots the frequency of Hg emissions in particular concentration ranges. The graph includes a line representing the frequency of a normal distribution. Figure C.5 Histogram of hourly average Unit 3 Hg emissions (µg/m3) from October 1, 2010, to December 19, 2010 during CaBr2 addition to the coal on Unit 4. 213 Figure C.5 shows that the data are near normal. The most frequently observed hourly average Hg emissions are near the center of the distribution and the tails are even on both sides of the mean. There does appear to be a slightly higher number of observed data points to the left of the mean so the data may be slightly negatively skewed. Figure C.6 plots expected cumulative probability versus observed cumulative probability (P-P plot). A normal dataset has a P-P plot that is a straight-line meaning; that is observed values equal the expected values of a dataset that is normally distributed. Figure C.6 Normal expected cumulative probability versus observed cumulative probability (P-P plot) of Unit 3 hourly average Hg emissions (µg/m3) from October 1, 2010, through December 19, 2010 during CaBr2 addition to the coal on Unit 4. 214 Figure C.6 shows that the Unit 3 hourly averaged Hg emissions from October 1, 2010 through December 19, 2010, exhibited near normal behavior. Table C.3 provides summary information regarding the Unit 3 hourly averaged Hg emissions from October 1, 2010 through December 19, 2010. The table includes the mean, standard deviation, skewness, kurtosis, and the JB statistic. Skewness measures the asymmetry of the data around the mean, and the skewness of a normal distribution is zero. Kurtosis measures the fraction of outliers in a distribution (i.e., whether the data are peaked or flat relative to a normal distribution). A large value means the dataset is peaked about the mean, and a low value indicates relatively flat values about the mean. A normal distribution has a kurtosis value of 3. The SPSS value of kurtosis is adjusted for normality (i.e., K-3), therefore a value of zero indicates a normal distribution. The JB statistic is a measure of normality, follows a Chi-squared distribution with a degree of freedom of 2, and can be used to quantitatively test for normality. The summary information in Table C.3 supports the conclusions drawn from Figures C.5 and C.6; the data are nearly normally distributed, with the exception of the JB statistic. The values of both skewness and kurtosis are near zero. The slightly negative value of skewness means that more of the data points in the dataset fall below the mean of 2.904 µg/m3 than fall above the mean. The skewness is very difficult to observe visually from Figure C.5. 215 Table C.3 Summary Normality Statistics of Unit 3 Hourly Average Hg Emissions (µg/m3) from October 1, 2010 through December 19, 2010 During CaBr2 Addition to the Coal on Unit 4. Statistic Value Unit Sample size 1,738 n/a Mean 2.904 µg/m3 Standard deviation 1.005 µg/m3 Kurtosisa -0.023 n/a -0.192 n/a 10.7 n/a Skewness Jarque-Bera (JB) b Note: a. Kurtosis calculated by SPSS has been adjusted. A value of zero represents a normal distribution. b. Jarque-Bera statistic formula has been adjusted for excess kurtosis. The JB statistic is low, with a value of 10.7. Using the Chi-squared distribution (df = 2) led to the rejection of the hypothesis that the Unit 3 hourly average Hg emissions from October 1, 2010 through December 19, 2010, were normal (p < .05). Although Figures C.5 and C.6 appear to indicate nearly normal dataset, the use of statistical methods caused the hypothesis that the dataset is normal to be rejected. 216 APPENDIX C.4 NORMALITY OF UNIT 4 HOURLY MERCURY EMISSIONS DURING JANUARY 2011 Appendix C.4 includes the analysis for determining the normality of the Unit 4 hourly average Hg emissions data from January 1-30, 2011, while CaBr2 was not being added to Unit 4. Figure C.7 is a plotted histogram of the Unit 4 hourly average Hg emissions during the period of interest. The histogram plots frequency of Hg emissions in particular concentration ranges. The graph includes a line representing the frequency of a normal distribution. Figure C.7 Histogram of Unit 4 hourly average Hg emissions (µg/m3) from January 1-30, 2011, while CaBr2 was not added to the coal on Unit 4. 217 Figure C.7 shows that the data are not normal and that a cluster of values surrounds the mean, which will likely mean that the kurtosis will be positive. The most frequently observed hourly average Hg emissions appear slightly to the right of the center of the distribution that is the data appear to be positively skewed. Figure C.8 plots an expected cumulative probability versus observed cumulative probability chart (P-P plot). A normal dataset has a P-P plot that is a straight line; that is observed values equal the expected values of a normally distributed dataset. Figure C.8 Normal expected probability versus observed probability (P-P Plot) of hourly average Unit 4 Hg emissions (µg/m3) from January 1-30, 2011, while CaBr2 was not added to the coal on Unit 4. 218 Figure C.8 shows that, for the most part, the observed values equal the expected values for a normal distribution. The exception occurs towards the left portion of the distribution, where the observed values occur more often than expected. This behavior can be observed also in Figure C.8 when the frequency bins are above the normal curve in the histogram. In Figure C.7 and C.8, the dataset appears nearly normal. Table C.4 provides summary information regarding Unit 4 hourly average Hg emissions during January 1-30, 2011. The table includes the mean, standard deviation, skewness, kurtosis, and the JB statistic. Skewness measures the asymmetry of the data around the mean, and the skewness of a normal distribution is zero. Kurtosis measures the fraction of outliers in a distribution (i.e., whether the data are peaked or flat relative to a normal distribution). A large value means the dataset is peaked about the mean, and a low value indicates relatively flat values about the mean. A normal distribution has a kurtosis value of 3. The SPSS value of kurtosis is adjusted for normality (i.e., K-3), therefore a value of zero indicates a normal distribution. The JB statistic is a measure of normality, follows a Chi-squared distribution with a degree of freedom of 2, and can be used to quantitatively test for normality. The summary statistics tabulated in Table C.4 support the conclusions drawn from Figures C.7 and C.8 that the data are not normally distributed. The kurtosis was positive a result that supports the earlier assertions derived from Figure C.7; also the data was peaked around the center. Additionally, the conclusions drawn from the figures support the likelihood that the distribution was positively skewed. 219 Table C.4 Summary Statistics of the Hourly Average Unit 4 Hg Emissions (µg/m3) from January 1-30, 2011, While CaBr2 Was Not Added to the Coal. Statistic Value Unit Sample size 707 n/a Mean 2.1820 µg/m3 Standard deviation 0.6712 µg/m3 Kurtosisa 0.775 n/a Skewness 0.081 n/a Jarque-Bera (JB)b 18.46 n/a Note: a. Kurtosis calculated by SPSS has been adjusted. A value of zero represents a normal distribution. b. Jarque-Bera Statistic formula has been adjusted for excess kurtosis. The JB statistic was large (18.46). Using the Chi-squared distribution (df = 2) resulted in the rejection of the hypothesis that the Unit 4 hourly average Hg emissions from September 1-30, 2010, were normal. The nearly normal appearance from Figures C.7 and C.8 is not supported statistically. 220 APPENDIX C.5 NORMALITY OF UNIT 4 HOURLY MERCURY EMISSIONS DURING SEPTEMBER 2010 Appendix C.5 includes the analysis for determining the normality of the Unit 4 hourly average Hg emissions data from September 1-30, 2010, while CaBr2 was not being added to Unit 4. Figure C.9 is a histogram of the Unit 4 hourly averaged Hg emissions during the period of interest. The histogram plots frequency of Hg emissions in particular concentration ranges. The graph includes a line representing the frequency of a normal distribution. Figure C.9 Histogram of Unit 4 hourly average Hg Emissions (µg/m3) from September 130, 2010, while CaBr2 was not added to the coal on Unit 4. 221 Figure C.9 shows that the data are not normal. The most frequently observed hourly average Hg emissions appear to the right of the center of the distribution and the frequency magnitudes appear to be below the normal distribution curve so a low value for kurtosis is expected. Figure C.10 charts expected cumulative probability versus observed cumulative probability (P-P plot). A normal dataset has a P-P plot that is a straight line; that is observed values equal the expected values of a normally distributed dataset. Figure C.10 Normal expected cumulative probability versus observed cumulative probability (P-P Plot) of Unit 4 hourly average Hg emissions (µg/m3) from September 1- 30, 2010, while CaBr2 was not added to the coal on Unit 4. 222 Figure C.10 shows a departure from normal behavior at the center of the distribution. This departure can be observed in Figure C.9 when the magnitude of the frequency bins is above the normal distribution curve. After this point, the P-P plot returns to ideal normal behavior. It should be expected that the skewness of the dataset will be large and positive and that the kurtosis will be near zero, indicating a flatter than normal distribution curve. Table C.5 provides summary information regarding the Unit 4 hourly averaged Hg emissions during September 1-30, 2010. The table includes the mean, standard deviation, skewness, kurtosis, and the JB statistic. Skewness measures the asymmetry of the data around the mean, and the skewness of a normal distribution is zero. Kurtosis measures the fraction of outliers in a distribution (i.e., whether the data are peaked or flat relative to a normal distribution). A large value means the dataset is peaked about the mean, and a low value indicates relatively flat values about the mean. A normal distribution has a kurtosis value of 3. The SPSS value of kurtosis is adjusted for normality (i.e., K-3), therefore a value of zero indicates a normal distribution. The JB statistic is a measure of normality, follows a Chi-squared distribution with a degree of freedom of 2, and can be used to quantitatively test for normality. The summary statistics tabulated in Table C.5 support the conclusions drawn from Figures C.9 and C.10 that the data are not normally distributed. The kurtosis was slightly negative which supports the earlier assertions from Figures C.9 and C.10. 223 Table C.5 Summary Statistics of the Unit 4 Hourly Average Hg Emissions (µg/m3) from September 1-30, 2010, while CaBr2 was not added to the coal on Unit 4. Statistic Value Unit Sample size 690 n/a Mean 2.5493 µg/m3 Standard deviation 1.0447 µg/m3 Kurtosisa -0.390 n/a Skewness -0.662 n/a Jarque-Bera (JB)b 30.09 n/a Note: a. Kurtosis calculated by SPSS has been adjusted. A value of zero represents a normal distribution. b. Jarque-Bera statistic formula has been adjusted for excess kurtosis. The JB statistic is large (30.09). Using the Chi-squared distribution (df =2 ) resulted in the rejection of the hypothesis that the Unit 4 hourly average Hg emissions from September 1, 2010, through September 30, 2010, were normal. 224 APPENDIX C.6 NORMALITY OF UNIT 4 PHASE III HOURLY MERCURY EMISSIONS Appendix C.6 includes the analysis for determining the normality of the Unit 4 Hg emissions data from October 1, 2010, through December 19, 2010, during CaBr2 addition. Figure C.11 is a plotted histogram of the Unit 4 hourly averaged Hg emissions during the period of interest. The histogram plots frequency of Hg emissions in particular concentration ranges. The graph includes a line representing the frequency of a normal distribution. Figure C.11 Histogram of Unit 4 hourly average Hg emissions (µg/m3) from October 1, 2010, through December 19, 2010, during CaBr2 addition to the coal on Unit 4. 225 Figure C.11 shows that the data were not normal. The most frequently observed hourly average Hg emissions are near the center of the distribution, but slightly to the left of the mean but has a long tail to the right. The dataset is pinned on the left end of the axis because values below zero cannot occur. Figure C.12 charts expected cumulative probability versus observed cumulative probability (P-P plot). A normal dataset has a P-P plot that is a straight line; that is observed values equal the expected values of a normally distributed dataset. Figure C.12 Normal expected cumulative probability versus observed cumulative probability (P-P plot) of Unit 4 Hg hourly average emissions (µg/m3) from October 1, 2010, through December 19, 2010, during CaBr2 addition to the coal on Unit 4. 226 Figure C.12 shows that, at times, the observed behavior occurs more often than expected and that at other times, observed behavior is less than expected. This figure demonstrates that the dataset does not exhibit normal behavior. Table C.6 provides summary information regarding the hourly averaged Hg emissions from Unit 4 during October 1, 2010, through December 19, 2010. The table includes the mean, standard deviation, skewness, kurtosis, and the JB statistic. Skewness measures the asymmetry of the data around the mean, and the skewness of a normal distribution is zero. Kurtosis measures the fraction of outliers in a distribution (i.e., whether the data are peaked or flat relative to a normal distribution). A large value means the dataset is peaked about the mean, and a low value indicates relatively flat values about the mean. A normal distribution has a kurtosis value of 3. The SPSS value of kurtosis is adjusted for normality (i.e., K-3), therefore a value of zero indicates a normal distribution. The JB statistic is a measure of normality, follows a Chi-squared distribution with a degree of freedom of 2, and can be used to quantitatively test for normality. The summary information in Table C.6 supports the conclusions drawn from Figures C.11 and C.12 that the data are not normally distributed. The large value for kurtosis (18.304) demonstrates numerically that the data set is peaked about the mean and drops sharply at the edges. This behavior is easily observed in Figure C.11. The positive value of skewness indicates that more values in the dataset fall to the left of the mean and that the distribution has a long tail to the right of the mean. 227 Table C.6 Summary Normality Statistics of the Unit 4 Hourly Average Hg Emissions (µg/m3) from October 1, 2010, to December 19, 2010, During CaBr2 Addition to the Coal on Unit 4 Statistic Value Unit Sample size 1,689 n/a Mean 0.2605 µg/m3 Standard deviation 0.1568 µg/m3 Kurtosisa 18.304 n/a 2.871 n/a 25,898 n/a Skewness Jarque-Bera (JB) b Note: a. Kurtosis calculated by SPSS has been adjusted. A value of zero represents a normal distribution. b. Jarque-Bera statistic formula has been adjusted for excess kurtosis. The JB statistic is large (25,898). Using the Chi-squared distribution (df =2 ) resulted in the rejection of the hypothesis that the Unit 4 hourly average Hg emissions, during October 1, 2010, through December 19, 2010, were normal. 228 APPENDIX D STATISTICAL TEST RESULTS 229 APPENDIX D.1 INDEPENDENT T-TEST RESULTS FROM COMPARING UNIT 3 MERCURY EMISSIONS WITH AND WITHOUT CALCIUM BROMINE ADDITION ON UNIT 4 Hypothesis Tested µBr = µNo,Br Table D.1 Output From SPSS Testing The Hypothesis If Unit 3 Hg Emissions During CaBr2 Addition On Unit 4 Are Equal To Unit 3 Hg Emissions Without CaBr2 Addition On Unit 4. Data Consists Of Hourly Hg Emission Averages Taken From September 1, 2010, Through January 30, 2011. Table D.2 Output from SPSS Providing Sample Size, Mean, and Standard Deviation of Unit 3 Hg Emissions During Phase III, Pre-testing and Post-test Periods Grouped by CaBr2 Condition. Data Consists Of Hourly Hg Emission Averages Taken From September 1, 2010, Through January 30, 2011. 230 APPENDIX D.2 INDEPENDENT T-TEST RESULTS FROM COMPARING UNIT 4 MERCURY EMISSIONS WITHOUT CALCIUM BROMINE ADDITION ON UNIT 4 Hypothesis Tested µSeptember = µJanuary Table D.3 Output From SPSS Testing The Hypothesis If Unit 4 Hourly Average Hg Emissions During Period Without CaBr2 Addition (September 1-30, 2010) Are Equal To Unit 4 Hourly Average Hg Emissions Period Without CaBr2 Addition (January 1-30, 2011). Table D.4 Output From SPSS Providing Sample Size, Mean, And Standard Deviation of Phase III Unit 4 Hourly Average Hg Emissions One Month Before (September 1-30, 2010) And After (January 1-30, 2011). 9 Denotes September And January Is Denoted By 1. 231 APPENDIX D.3 INDEPENDENT T-TEST RESULTS FROM COMPARING UNIT 4 MERCURY EMISSIONS WITH AND WITHOUT CALCIUM BROMINE ADDITION ON UNIT 4 Hypothesis Tested µBr = µNo,Br Table D.5 Output From SPSS Testing The Hypothesis If Unit 4 Hourly Average Hg Emissions During Period Without CaBr2 Addition On Unit 4 (September 1-30, 2010, and January 1-30, 2011) Are Equal To Unit 4 Hourly Average Hg Emissions During Period With CaBr2 Addition On Unit 4 (October 1, 2010, Through December 19, 2010). Table D.6 Output From SPSS Providing Sample Size, Mean, And Standard Deviation of Unit 4 Hourly Average Hg Emissions During Period Without CaBr2 Addition On Unit 4 (September 1-30, 2010, and January 1-30, 2011) And Unit 4 Hourly Average Hg Emissions During Period With CaBr2 Addition On Unit 4 (October 1, 2010 Through December 19, 2010) 232 APPENDIX D.4 PAIRED T-TEST RESULTS FROM COMPARING UNIT 3 AND UNIT 4 MERCURY EMISSIONS DURING CALCIUM BROMINE ADDITION ON UNIT 4 Hypothesis Tested µ3 U4,Br = µ4 U4,Br Table D.7 Output From SPSS Testing The Hypothesis If Unit 3 Hourly Average Hg Emissions During Period With CaBr2 Addition On Unit 4 (October 1, 2010, Through November 30, 2010) Are Equal To Unit 4 Hg Emissions During Period With CaBr2 Addition On Unit 4 (October 1, 2010, Through November 30, 2010). Table D.8 Output From SPSS Providing Sample Size, Mean, And Standard Deviation Of Unit 3 Hourly Average Hg Emissions During Period With CaBr2 Addition On Unit 4 (October 1, 2010, Through November 30, 2010) And Unit 4 Hourly Average Hg Emissions During Period With CaBr2 Addition On Unit 4 (October 1, 2010, Through November 30, 2010) 233 APPENDIX D.5 WILCOX RANKED SIGN TEST RESULTS FROM COMPARING UNIT 3 AND UNIT 4 30-DAY ROLLING AVERAGE MERCURY EMISSION RATE DURING CALCIUM BROMINE ADDITION ON UNIT 4 Hypothesis Tested µ3 U4,Br = µ4 U4,Br Figure D.9 Output from SPSS testing the hypothesis if Unit 3 Hg emission rate 30-day rolling averages during period with CaBr2 addition on Unit 4 (October 1, 2010, through November 30, 2010) were equal to Unit 4 Hg emission rate 30day rolling averages during period with CaBr2 addition on Unit 4 (October 1, 2010, through November 30, 2010) using the Wilcox Signed Rank Test. 234
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