Experience of Energy Management System and Monitoring in Hatien-1 Cement Company (Vicem Hatien) Presented by Hoang Kim Cuong Deputy General Director Hatien-1 Cement JSC. www.efficiency-from-germany.info 1 Experience of Energy Management System and Monitoring in Hatien-1 Cement Company (Vicem Hatien) Presented by Hoang Kim Cuong Deputy General Director Hatien-1 Cement JSC. 23.3.2015 Ho chi Minh City 2 Outline General Kinds of used energy Energy cost Management Implementation Long-term plan Conclusion Energy cost Kinds of used energy Energy Effect 3 General • • • • Since 1964 2 plants, 4 cement grinding terminals Employees: 2.870 Production capacity: – Clinker: 4,5 million tpy – Cement: 7 million tpy • Standards ISO 9001: 2008; ISO 14001: 2004; OHSAS 18001: 2007 4 SITE MAP CAMRANH GRINDING TERMINAL BINHPHUOC CEMENT PLANT PHUHUU GRINDING TERMINAL KIENLUONG CEMENT PLANT LONGAN GRINDING TERMINAL THUDUC GRINDING TERMINAL 5 6 Kinds of energy using Oil from cashew HFO, 3% nut shell, 6% DO, 1% Other, 2% Electricity 32% Coal 55% 7 Energy Cost Product Energy cost / ex-work cost Clinker Cement 60% … 70% 5% … 10% Energy type Consumption rate Target better cost Electrical energy for producing clinker 64 … 85 kWh/T 65 60 … 65 kWh/T Anthracite Coal 760 … 900 kCal/kg clinker 760 720 kCal/kg 33 (VRM) 40 (BM) 33 (VRM) 40 (BM) Electrical Energy for 34 … 45 producing cement kWh/T cement 8 Frequency Power consumption Frequency 55 Heat Consumption 110 50 Min max Avg Median 45 57.8 76.7 69.0 69.0 Min max Avg Median 100 90 40 606 975 774 767 80 35 70 30 60 25 50 20 40 15 30 10 20 5 10 0 0 950 925 900 875 850 825 800 90 775 kWh/T clinker 85 750 80 725 75 700 70 675 65 650 60 625 55 600 50 kCal/kg clinker Histogram of energy consumption of Binhphuoc Cement Plant for clinker production - 2014 9 Power consumption for Cement Grinding & frequency Despatch 55 Min max Avg Median 50 45 17.0 65.6 33.7 32.5 Power price (average), at 110 kV for production vnd us cent 40 35 1 600 30 1 400 25 1 200 20 1 000 15 800 10 5 0 Loesche’s Vertical Roller Mill Binhphuoc Cement Plant Histogram 2014 55 50 45 40 35 30 25 20 kWh/T cement 7 6 5 4 600 3 400 2 200 1 0 0 10 Management Awareness of energy saving to all employees Upgrading technology Optimizing operation Modern technology during project time Looking other fuels as alternative fuels for combustion, Reducing fossil fuels Making products with low energy consumption 11 Solutions • Establish energy management system in each plant • Monitoring energy consumption of production lines by daily report, studying abnormal things to solve Entry Result Report Chart 12 Solutions • Executing energy audit by independent service following government regulation, training for internal energy audit • Establishing energy management team in each plant. • Starting ISO 50001 from 2015 13 Implementation Measurement • Making category of loads according to the energy unit • Installing power meters for recording • Connect to the control system for online monitoring in each plant “If you can’t measure it, you can’t manage it” 14 Implementation Optimizing and improving the operation Keep equipment operating at designed capacity or more, not running at no-load or low load, avoid to start / stop many time. Increase the productivity of the ball mill by optimization of the ball quantity. Select the materials with good and correct quality. Produce Portland Cement Blended (PCB-40 PCB-50) to reduce clinker. Mixing the components of raw materials in a correct proportion to reduce heat energy (coal) for combustion. 15 Implementation Control operation Assure that equipment operating properly, avoid operation in rush hour for some equipment. Shut down the bag filter if production line stops. Establish the bag filter operates in automatic according to pressure difference Assure that power factor above 0,9 in order to reducing the inactive power Optimize the compressed air system by centralizing the control system and monitoring losses 16 Implementation Optimize the operation parameter Study experience among internal departments, with other cement plants frequently in order to find the optimized parameter. 17 Implementation Enhancement of innovation Encourage everyone give ideas for upgrading equipment. Improving the cooling water of air compressor at cement grinding and packing area, change the electrical motor from 37 kW to 5,5 kW for a pump. Redesign the chute, not use chain conveyor under the chute (7,5kw), lengthen the rubber conveyor instead. 18 Implementation Enhancement of innovation Installing the variable frequency converter for conveyor 2E1BC1. The power reduces from 120 kW to 66 kW. Saving energy and keep the thickness of material layer to be stable for PGNAA, ensure the analysis exactly 19 Implementation Increase the maintenance skill Training to the maintenance team in order to decreasing the maintenance time. Apply preventive maintenance, solve all the repeated problem thoroughly 20 Implementation Lighting and air conditioner Lighting: reduce the number of lights reasonably, assembly the automatic equipment for turning on / off the lighting. Office: open window for sun light, turn off the equipment in the room when no anyone in the room. Air conditioners: set at 25oC .. 26oC for people and for equipment room. Step by step to change lighting with energy saving lamps 21 Implementation Solution for cost saving Alternative fuels that are using in Ha Tien 1: Using a part of Indonesia anthracite coal (high/medium volatile substance, cheaper price) for producing clinker. Oil from cashew nut husk to replace HFO for combustion in the kiln at Kienluong Cement plant Using FO-R (recycle product from wasted rubber) to replace DO at Binhphuoc cement plant Using cashew nut husk (after extracting oil) as an alternative fuel in Binhphuoc cement plant 22 Implementation Solution for cost saving Using rice husk to replace HFO at Phuhuu grinding Terminal. Use wasted heat from kiln to heat the coal mill instead of HFO at Kienluong cement plant These do not save energy but reduce energy cost and contribute to reduce CO2 emissions. 23 Implementation Typical unit price of some fuels - 2015 unit: vnđ/kCal, including logistic cost, no VAT HFO DO FO-R Cashew oil Rice husk Coal 3c Indo. Coal Cashew nut shell 1.3 1.6 1.4 1.1 0.57 0.44 0.38 0.3 1.9 2.3 1.8 1.3 HCM City Binh Binh phuoc phuoc Kien luong 0.4 HCMC Phuhuu Binh phuoc Binh phuoc Binh phuoc 24 Long-term plans Continue to study “Variable frequency converter” to regulate the flow of the fans instead of dampers. Optimize the production process, Looking for the optimization software for operation of the rotary kiln. Upgrade technology: replace planet cooling system with clinker grate cooler. Improving the preheater of old kiln, use high efficiency burner for old clinker production line at Kienluong plant. Study of mineral additives to use for combustion in the kiln to reducing the heat consumption. 25 Long-term plans Study to burn other wastes. Implement the project of waste heat recovery system to generate electricity for new kiln at Kienluong plant and Binhphuoc plant. This will save about 15% electrical energy for each plant. 26 Conclusion Cost saving is different from energy saving, but both of these are directed to use energy efficiently Hatien-1 always thinks about energy saving and efficiency, gradually optimizing and improving energy efficiency Use energy saving and efficiency will be increasing the competitiveness of enterprises. It also contributes to reducing CO2 emissions, towards the goal of sustainable development of enterprises. 27 28
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