1 DUKW “ A long journey” During the Second World War the allies required a vehicle to be used during invasions from the sea, both in the Pacific and European theatres of war and would be able to move equipment from ships across the beach to supply dumps behind the beach-heads. One of the vehicles developed was the DUKW. The DUKW prototype is based on the US army CCKW 2.5 ton army truck, which was already in service. The DUKW utilised the same 6 wheel drive and chassis arrangement as the original truck but instead of a standard body it was fitted with a boat like body and a propeller drive system. DUKW is actually the letter codes used by the manufacturer to denote individual features of the vehicle. D denotes Year of first production (1942) U denotes Utility or Universal K denotes All-wheel drive W denotes Tandem mounted driven rear axles Today you can still see the DUKW in operation, brightly painted as tourist vehicles in places as far afield as London, England to Rotarua, New Zealand. 2 Conception It’s a long time now since I first got interested in building an amphibious model which would be able to move between land and water under its own traction. I looked at many different options ranging from the Stalwart six wheel drive truck to the WWII Buffalo tracked vehicle. Eventually after seeing the DUKW in Rotarua I decided on the WWII DUKW Amphibious truck. After some further research, looking at the Deans mouldings, and models of the DUKW built by others as shown on the internet I decided I would build the hull myself from wood and utilise ‘Robbe’ Axles and wheels for the road running gear. As a base for all initial measurements I used the ‘Italeri’ 1/35th scale plastic kit number 6392. I also wanted my model to be as realistic and faithful to scale as I could. During my research I had found some modellers had made their models extra large in some areas. As an example I found one model which had a higher bonnet (about 25mm higher) and no dropped load deck (load deck level with main deck). This had been done to accommodate the drive motors and batteries that the builder had fitted. I knew that trying to be faithful to the original would be difficult but did not realise how long the challenge would take. Mechanics The final scale of my model is approximately 1/11th, which is a bit of an odd scale but this was dictated by the ‘Robbe’ axle track width and the diameter of the Robbe Tyres used. The model is entirely built from scratch and initially I based all measurements on the Italeri plastic kit. 3 The photo above shows the wooden hull after being fitted with the axles and wheels. The suspension system is made so as to follow the original prototype in the design and operation as far as was possible. I used brass blocks and plates to mount the axle springs to the wooden hull. The tandem rear axles swing on blocks which swivel on brass mountings fitted to the brass plates. The springs are mounted above the axles as per the original and tie bars hold the bottom of the axle in place. This allows full movement of each axle. PTFE bushes are fitted between the spring end loops on all 3 axles and the fixed mounting screws to allow their free movement without wear. 4 Once I had the road wheels in place I could then mount the propeller drive system and rudder. The above photo shows the external end of the water drive system and rudder. Internally the next stage was to make up both the road drive mechanism which would couple with the axles and the water drive system which would couple to the propeller shaft. 5 The road drive system consists of a lay shaft mounted in 2 bearing blocks, (each fitted with 2 ball races and PTFE seals) mounted centrally in the hull. Each end of the lay shaft then drives the front and rear axles. The centre of the lay shaft which is internal to the boat is fitted with a tooth belt pulley. The motor is a 540 size motor fitted to a planetary gearbox fitted with another tooth belt pulley. A tooth belt couples the drive to the lay shaft. The road drive system and space below the load deck dictated that the only logical space left to fit the water drive motor would be in the bows. Again I used a standard 540 size motor and a second planetary gearbox since the propeller would be 50mm in diameter, but the bow location of the motor was a long way from the end of the fitted propeller shaft. The problem was solved by fitting a second propeller shaft within the hull coupled to the gearbox and the external shaft by two universal couplings. 6 Problems Once I had progressed to having the hull nearly complete I needed more information on the detailed fitting around the model so decided to visit the Imperial War Museum at RAF Duxford . However on seeing their original DUKW I realised to my horror that the ‘Italeri’ kit did not show some of the details correctly. The picture at RAF Duxford shows the solid tarpaulin hoops which were not a part of the’ Italeri ‘kit I had, but more concerning was the winch arrangement at the rear, The ‘Italeri ‘kit shows the winch and its mounting brackets mounted parallel with the main deck. However inspection of the real thing showed that in fact it is mounted at an angle to the main deck. I realised this was to allow the drive from the main gearbox power take-off to the winch to couple up without undue misalignment. As I had already made a set of winch mounting brackets , which were now wrong this set me back until I could get the winch arrangement correct. Armed with the fact that the Italeri kit was not 100% accurate I set about gathering a lot more information from text books, museum visits and the internet as well. This all took time and the project was on the shelf for quite a while before I was happy to proceed. After quite a while doing research I also realised that the exhibit at Duxford was not fitted with lights in the same place as they would have been for wartime use. They had been modified for modern road use. 7 Detailing The picture shows the model with the winch now mounted correctly at the right angle to the deck. To assemble it I used tiny brass 10BA & 12BA (about 1mm diameter) nuts & bolts (some of these required threads tapping carefully into other components). The light housing to the left of the winch in this picture is for one of the two rear lights. The diameter of this rear light housing is 10mm with an 8mm diameter internal diameter. If I were to fit working lights into the housings I would need really small lights since on one side there are 3 lights (Blackout brake and 2 blackout convoy lights) and on the other 4 lights ( Service marker & Service brake & 2 blackout convoy markers), more on this later. Also in this picture you can see the channels which form part of the hatch cover. These were cut from plastic mouldings and glued to the wooden hatch cover with Super-Acrylic glue, which I must say is excellent if you want to glue dissimilar materials like these. 8 The above picture shows the bonnet and front lights. Again I used plastic channels stuck to the wood with Super acrylic. The light housings were all machined on my ‘Cowells’ 90 lathe from brass and are, from left to right, Blackout marker, Main Headlight, Main Headlight , Blackout marker, Blackout headlight. The blackout markers have a 4mm diameter internal diameter and the main headlights are 13mm. Luckily the markers only require a single light source as does the blackout headlight. The main headlights require two, (one for main and one for dip). 9 This picture shows the main driving cab with the dashboard, driving levers and steering wheel. The dashboard was made with wood, fitted with circular thin ply cut outs glued on for the dials, and brass components for the switches & knobs. The steering wheel and driving levers were also made from brass. The curved cab sides protecting the air intake louvers at each side of the cab were made by laminating three layers of very thin ply around a former and then carefully cutting the shape out. 10 Lighting. I wanted to try and make the lighting system work as per the original and so set about trying to find small light sources which I might be able to use. I could have used wheat-germ filament lamps but the problem with these would be, if they blew, they would not be easy to replace. I have always used LEDs for lighting as these are much more able to withstand rough treatment than a filament lamp. The problem I had was that the smallest I could find were still too large to be able to fit four of them within an 8mm diameter hole for the rear lights. Then after much searching I found the answer, NANO LEDs. Above is a picture of a NANO LED shown on 5mm grid lined paper. Also in the picture are the LED dropping resistor and a PTFE mounting which I machined to fit the LED into. This was to allow it to be insulated and fitted into the 4mm Blackout marker brass lamp housing. NANO LEDs were marketed by a company in Freemantle, Australia and they come fitted with thin enamelled copper wires already soldered onto the 1mm diameter (YES you did read right ... 1mm diameter) LEDs. These were ideal for what I wanted as they came in several different colours, Prototype White, Sunny White, Red and Amber. You can tint the white lamps with paint if you require any other colour. Here is a link to the supplier’s website page. http://www.dccconcepts.com/index_files/Prewired08mm0603SMTLEDs.htm. They are available in the UK and I got mine from ‘Gaugemasters’ at Ford near Arundel who have a mail order website as well as a shop. 11 I also machined PTFE housings for the blackout headlight and the two rear light housings. For the front headlights I machined some clear acrylic rod to the required shape. Each machined item of PTFE or acrylic was then carefully drilled with a 1mm hole and each LED was then glued into position with clear epoxy. The enamel wires were sleeved with small heat shrink tubing to protect them from any scraping which might remove the insulating enamel covering of the wire. On the rear lights there was a problem with the LEDs shining through the white PTFE when either the upper service/brake or lower blackout marker pairs were on. The Blackout & Service lamps are never on together on the prototype and this would not look right. The answer was to carefully cut a slot with a ‘Dremel’ mini cutting disc horizontally across the PTFE housing and glue in a plasticard shroud with Super acrylic between the upper and lower halves of the housing. This solved the problem very well. While I now had all the LEDs fitted they still required their individual dropping resistors to be wired in and a switching system to control them to be made up. I decided to make up a Vero-board with the dropping resisters fitted to them together with any additional protection diodes and reverse current flow diodes. I made up one board for the bow lights and another for the stern lights. The LED wires were not long enough to reach as far as I needed so I had to solder extension enamel wires onto the existing and then fit additional heat shrink tubing to protect the extensions. The ends of the enamel wires were then soldered to the appropriate connection post of the Veroboards. Each Vero-board was fitted with a DIL pin connector and fitted into a homemade plasticard case. 12 The picture shows the completed bow resistance board wired to the enamel wire ends. To the left of the board are the pins for the 6 pin DIL connection which will interface with the switching relay system. To control the LEDs I used five radio controlled switching relays from Active Robots. After spending time engineering how they would need to be wired I fitted five of the Servo relay 1Amp switches into a plasticard box that I made up. This also had DIL pin connections fitted inside the end of the box so that it would be easy to connect them with the resistance boxes using prewired 6 way ribbon jumper cables from ‘ Technobots’ in Totton. 13 Relay box showing the DIL connection pins can be seen to the right of the box 14 Photo of the service headlights on main beam Batteries. Since space inside the model is at a premium I needed to choose batteries that would give me a reasonable duration on both water and land drive systems and also fit within the available space. I decided to use a 7.2 volt system on both the water and land drive and bought twelve 3800mah NiMh 7/5A size cells from ‘Cellpack solutions’. These were made into two 6 cell packs and fitted to the left side of the hull between the front and rear wheel wells. The lighting also required a small battery and for this I used a 6V pack of AAA 800maH Eneloop cells from ‘Overlander’. The radio is also powered from a 4.8V AA pack of 1000maH Eneloop cells, Motors Both the water drive and land drive systems were fitted originally with 3 pole light wound standard 540 motors. Speed controllers Both the water drive and land drive systems are fitted with Microgyros FR40 Electronic speed controllers. 15 Radio. I have fitted an 8 channel ‘Spektrum’ 2.4Ghz. radio to the model. The transmitter is fully programmable and this allows me to fine tune and mix all the individual channel settings to get the correct performance from the systems fitted. My Radio is set up for Mode 4 operation. Channels are allocated as follows; Stick or channel To ESC, Servo or relay function Left Vertical (Throttle) Water drive motor Left Horizontal (Aileron) Right Vertical (Elevator) Land Drive motor Right Horizontal (Rudder) Water Rudder Gear Land Steering Aux 1 Service/Blackout lights selection Aux 2 Main headlight Dip/Main selection Aux 3 Brake lights 16 Testing on the water After checking the balance of the model in the bath and after adding some additional ballast the model was finally ready for its maiden trip on the water in 2013. The full size maximum water speed for the DUKW was 6.3MPH and the model has more than enough performance to meet a scale speed. Steering of the full size original was done using the steering wheel which operated both the front road wheel steering and the rudder in tandem. The model follows the same principal for its steering. The model seems to be able to steer better in one direction than the other and this is probably due to the dual effect of the torque from the large propeller and the tunnel in which it is mounted. The original probably suffered the same problem. Testing on the road The full size maximum road speed for the DUKW was 50MPH and the model is able to reach a reasonable speed to match the scale. 17 One problem found with the model was that with the motor I had originally fitted it would not climb any reasonable incline, so I decided to fit a more powerful motor. First I tried a Spirit 600 30turn motor but this still seemed insufficient, so I then researched higher torque motors and have now fitted a Novak 55turn Rock Crawler motor. The 55turn motor gave a much better climbing speed but I was experiencing problems with some strange noise in the drive system. I found that one of the axles appeared to have a damaged gear within the differential so I removed the axle and dismantled and inspected it. I found that two of the differential bevel gears were metal and two were plastic. The plastic gears had some teeth stripped. I bought a new differential from the ‘Robbe ‘website and when it arrive it had 4 metal bevel gears. The plastic gears had been upgraded in the time since I first purchased the original axles so I ordered some more for the other two axles and changed them too. The noise has disappeared and performance was better but after a short while of road running the system would not pull away or climb very well. I decided to test the pushing power with a pair of scales mounted against a wall and slowly increasing the motor power when in contact with the scales. With an ammeter fitted to the wiring and watching both the scales and the ammeter I found that after a while of pushing at full stick output the power started to drop away. The battery supply system seemed to be limiting the output available. I changed the cables in the system to a larger size of 2.5mm to reduce any undue resistance in the system but the power still dropped off after initially being OK. I checked all the connectors in the power system but these were not causing the power loss, so I decided to try a different set of batteries. I used a 7.2V sub C pack that I use for my model tanks and this proved to be OK with no power loss, in fact the power output went up and the maximum speed went up. So it seemed that the original batteries I had chosen were the problem, so I went back to the internet and researched the internal resistance of the NiMh 7/5A cells. I found that the internal resistance was typically 13-24 milli-ohms with a maximum rated output of 11.4Amp. The sub C cells however had an internal resistance of only 5-8milli-ohms with a rated output at 30Amp. So I had to replace the road drive batteries and have managed to just fit 6 new sub C cells into the model. Further testing will be required, but it looks much more promising since speed pickup has increased and I have now had to reduce the maximum throttle output to keep the top speed down. Much more to do There is still more work that can be done on the model although it looks the part and operates OK as it is now. A canvas cover could be made for the load area, with another slightly different hoop still being required for the back of the cab area and further fittings and detailing to the deck and side would add to the scale appearance. Conclusion I had to carry out all research, design and building from scratch. The majority of the model is made from wood, with brass for mechanical & other items, PTFE for bushings and a small amount of plastic strip for detailing where required. 18 In summary, this model has taken a long while from conception and through the building process but I am very happy to have managed to get the model as far as I have. Hhowever I know that when I look at it there are still items that I know need to be completed.
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