TRIZ Invention Solutions For Optimising Production Yield By Ab. Rashid Omar Amkor Technology is known as one of the world’s largest providers in contract semiconductor assembly and test services. It was founded in 1968 and is wellrecognised as a pioneer of the Integrated Circuit (IC) assembly and test for outsourcing. Being the largest semiconductor manufactures in outsourcing services around the globe, it has also become as one of the leading technological leaders in semiconductor manufacturing industry. The company has established a strategic manufacturing partnership with more than 300 of world’s leading semiconductor companies and electronic Original Equipment Manufacturers (OEMs). Amkor Technology has become more sustainable in the long-run through this strategy. This is supported by the fact of rapid growth in product development. Furthermore, Amkor Technology has also invested extensively in acquisition of sophisticated facilities and advanced technologies. This is an essential element that brings Amkor Technology into the next phase of innovation. Amkor Technology in Malaysia which is located in Selangor assists Power Discrete semiconductor companies with high quality packaging and test services. Its power discrete centre has more than 40 years of experience with a built up in manufacturing floor space of 24,155m2 and is accredited by the Japanese Automotive Certified. Whereas Amkor Technology Malaysia Sdn Bhd (ATM) was incorporated in 1973 and has total manpower of 1,800 employees. ATM produces a wide range of products including electronic components, integrated circuits and transistors. As a recognition of its commitment towards quality and in its pursuit for excellence, ATM has been awarded with six certifications, namely TS-16949, ISO-9001, ISO-9002, OHSAS-18001, ISO-14001 and SONY Green Partner industry standards. This is in line with its aim to be the Center of Excellence for power discrete packaging. Better Yield Leads To Higher Productivity It is very much believed by ATM that high productivity will lead to high yield in all level of the production lines. In addition to this, the management at ATM also holds on to its belief that ambiance is vital to all employees. Nevertheless, productivity drives ATM to adapt the concept of ‘right at the first time’ which is expected to reduce defect cases in production lines. At ATM, the reject cases are closely monitored as it has a significance on the total production output every month. In addition to this, it was identified that two crucial aspects in producing output with quality were high machine efficiency rate and low in Turnaround Time (TAT). Consequently, they understand that work efficiency will eliminate wastages and add value to work process itself. Therefore, ATM has always promoted innovation among its employees to ensure their employees are not left behind and are able to think beyond boundaries. ATM has paved Innovation and Creative Circle (ICC) as a platform for the implementation of ideas working towards a more structural and systematic work process. Consequently, ATM has chosen ICC projects to accelerate productivity and quality, ensure time efficiency and minimise cost of production. Implementation Of TRIZ Technique In Accelerating The Process Of Generating New Ideas One of the most essential production lines is DD2B. DD2B is the process that involves marking and packing the final products which are placed at the end of the whole production line. DD2B usually achieved a performance of 97.8 percent. However, in 2014, it was identified that DD2B performed below the targeted yield value of 98.6 percent. This was highlighted by the management during the monthly division meeting. The mark/pack workflow consists of nine processes. Based on the six month data (Jan-June 2014) that was collected, it was recorded that the number of defects produced was 22,017 pieces per month which was equivalent to 1.16 percent of marking defect rate. The benchmark value for this rate was 0.36 percent from IC production line. In order to overcome the problem, a team of six young outstanding employees were selected to come up with a plan. This team which was known as My Team, aimed to reduce 70 percent of high defect rate which amounts to 6,605 pieces per month. The team also targeted to increase yield value rate from 97.8 percent to 98.6 percent. Following that, the team set an objective to reduce the appearance defect rate from 142.7kiloRM to 42.8kiloRM by December 2014. The ICC project started with the process mapping of mark/pack machine work flow in which helped the team to understand and identify the root cause of this issue. The team further used the Fishbone diagram and Cause & Effect matrix for root causes verification. Based on the findings, My Team further used 5W+2H technique and concluded that the problem of high defects were contributed from the mark/pack machine. They further learnt that the chuck unit or mechanical part in the machine was not clamped to the device properly. This made the position of the chuck divergent with the device. Furthermore, the heavy friction movement during clamping has led to an Page 2 unstable slide bearing movement. In addition to this, the technician had made improper adjustment as there was no Standard of Procedure (SOP) for references. Next, was the issue of poor visibility as there was insufficient lighting. This happened due to the dust that was accumulated at the lamp surface which actually prevented adequate lighting. Lighting is a crucial aspect as the inspection unit needed light for product inspection. Further studies showed that the dust accumulated at the lamps was produced during the daily operations of other functional areas. However, the air shooter was unable to remove or clear the dust from the lamp surface. acronym, for “Theory of Solving Problem Solving”) is a problem solving and brainstorming technique that has been growing in popularity, especially among design engineers. The team applied the six TRIZ inventive principles and engaged with internal engineers and specialists. Through this technique, they were able to derive new, creative and innovative solutions especially through their exclusive experiences and knowledge. Furthermore, the team created new invention of an air shooter design for removing dust that is accumulated at the lamp surface. The table below shows the root causes, proposed solutions and action taken to resolve the problem of high in appearance defects. These findings were used by the team to generate ideas for improvement through several brainstorming sessions. The team used TRIZ inventive technique to develop new solution for chuck unit. TRIZ (Russian Root Cause Proposed Solution Action Taken Chuck Unit did not clamp the device properly due to the chuck position did not parallel with the device To change the chuck position from top 1. The team developed new design of of the chuck table to bottom side of chuck unit changing from vertical chuck table (from vertical to movement to horizontal movement horizontal movement) 2. A Poka Yoke Jig was developed for : Setting accuracy of the position on clamper Setting the gap without device between chuck base to chuck clamper Standardising all the chucks alignment The insufficient lighting was due to the dust accumulated at lamp surface Redesign the air shooter 3. Changed the old design of single direction of air shooter to rectangle block of multiple air shooters that suitable with the lamp surface area length Seven outlets air shooter with 3mm diameter each 300 of angle Page 3 THE NINE PROCESSES IN THE MARK MACHINE WORKFLOW TRIZ INVENTION SOLUTIONS Solutions for chuck unit 1. New design of chuck unit from vertical to horizontal Solution to remove dust 3. Rectangle block of multiple air shooters 2. New jig for setting the chuck position Page 4 Three improvements including new design of chuck unit, a poke yoke jig as well as multiple air shooter aided in achieving the target. The reduction in defect rate achieved by the team was acknowledged by the management. As a role model of innovation, My Team has applied these initiatives to other machine model and other departments as well. This is to accelerate the process of reducing the defect rate in other production lines. Thus, it is no doubt that ICC drives an organisation towards improvement and greater achievements in the future with the right atmosphere, approach and especially teamwork spirit. Analysis Of ICC Project In ATM Previously, it was recorded that an average of 22,017 pieces with defect were produced in the DD2B production line every month. After incorporating ICC initiatives, the team managed to reduce the defects to 6,545 which indicates 70 percent improvement in defect cases. Not only that, this has brought a positive impact to the marking defect rate as it has reduced to 0.35 percent from 1.16 percent previously. Consequently, the yield performance has also improved to 98.6 percent and the team is able to reach the target of this ICC project. My Team also conducted an opinion survey to evaluate the effectiveness of the project among the team members. This survey covers six elements which focuses on teamwork, responsibility, discipline, confidence, communication and quality control (Likert scale of 1 to 5). The survey showed that there was an improvement of 1.17 where the overall evaluation actually increased from 3.50 to 4.67. This actually reflects on the motivation among the team members towards their work spirit. Others benefits are as follows: `Spin-off’ of the improvement items to other machine model in other departments; Standardisation in process flow and schedule of other machine for part adjustment; and Showcases the best practices, in-house competition, appreciation and innovative exhibition week In addition to this, the cost of purchasing parts has also reduced to RM5,840 as compared to RM17,496 previously. This project also benefitted the company in terms of cost saving such as labor, machine and production cost during the implementation stage. The actual cost saving for this project constituted to RM421,311. Hence, it is no doubt that ICC initiatives have succeeded in reducing operation costs, defect cases and increasing work efficiency which drive towards output optimisation. COMPARISON BEFORE AND AFTER ICC IMPLEMENTATION Number of appearance defects : Before : 22,017 pieces After : 6,545 pieces Marking defect rate: Before : 1.16% After : 0.35% Yield performance: Before : 97.8% After : 98.6% Cost of parts: Before : RM17,496 After : RM5,840 Team score: Before : 3.5 points After : 4.67 points Cost saving: Before : 0 After : RM421,311 Page 5
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